Event Notification Report for April 10, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/07/2000 - 04/10/2000 ** EVENT NUMBERS ** 36811 36872 36873 36874 36875 36876 36877 36878 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36811 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 03/17/2000| | UNIT: [1] [] [] STATE: AZ |NOTIFICATION TIME: 20:26[EST]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 03/17/2000| +------------------------------------------------+EVENT TIME: 17:30[MST]| | NRC NOTIFIED BY: BRAD ROBINSON |LAST UPDATE DATE: 04/07/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID GRAVES R4 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF NON-CONSERVATIVE RODDED RADIAL PEAKING FACTORS IN THE CORE | | PROTECTION CALCULATORS AND CORE OPERATING LIMIT SUPERVISORY SYSTEM FOR | | GROUPS 5 AND P | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 03/17/00 at approximately 1730 MST, Palo Verde Engineering determined | | that Non-conservative Rodded Radial Peaking Factors were installed in the | | Unit 1 Core Protection Calculators (CPC) and Core Operating Limit | | Supervisory System for Group 5 and Group P. During the course of normal | | operations, Group 5 could be inserted into the core in order to compensate | | for Axial Shape Index. With the current values of Rodded Radial Peaking | | Factors, Group 5 may be outside of its design basis. Control room operators | | have been briefed on contingency actions to prevent the unit from operating | | outside the design basis. At this time, only Unit 1 is impacted, and the | | investigation is continuing." | | | | The licensee plans to notify the NRC resident inspector. | | | | * * * UPDATE AT 0009 ON 3/18/00, BY BANKS RECEIVED BY WEAVER * * * | | | | "On 3/17/00 at 2122, conservative Rodded Radial Peaking Factors were | | installed in unit 1, Core Protection Calculators (CPCs) channels A, B, & C | | and Core Operating Limit Supervisory System for Group 5 and Group P. CPC | | channel D remains out of service for an unrelated issue, however, before the | | channel is placed back into service, the new conservative Rodded Radial | | Peaking Factor will be installed." | | | | The licensee informed the NRC resident inspector of this update. The | | Operations Center notified the R4DO (Graves). | | | | * * * RETRACTION ON 04/07/00 AT 1627 EDT BY DAN MARKS TAKEN BY MACKINNON * * | | * | | | | On 04/06/00, Palo Verde Engineering personnel completed an analysis of the | | impact of the non-conservative Rodded Radial Peaking Factors and concluded | | that sufficient margin existed such that the Core Operating Limit | | Supervisory System and Core Protection Calculators would have maintained | | their safety system function and would have tripped/alarmed as required to | | maintain the plant within its design basis. The evaluation demonstrated | | that sufficient margin would exit throughout the current operating cycle | | such that the specified acceptable fuel design limits would not have been | | violated. | | | | The NRC Resident Inspector was notified of this retraction by the licensee. | | R4DO (Jeff Shackelford) notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 36872 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ST LOUIS UNIVERSITY HOSPITAL |NOTIFICATION DATE: 04/07/2000| |LICENSEE: ST LOUIS UNIVERSITY HOSPITAL |NOTIFICATION TIME: 16:42[EDT]| | CITY: ST LOUIS REGION: 3 |EVENT DATE: 04/06/2000| | COUNTY: STATE: MO |EVENT TIME: 17:36[CDT]| |LICENSE#: 24-00196-07 AGREEMENT: N |LAST UPDATE DATE: 04/07/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |THOMAS KOZAK R3 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MARK HAENCHEN | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION | | | | A patient on a ventilator was being treated with a High Dose Radiation | | Remote Afterloader when the patient intervened causing a jarring motion | | which caused the patient's catheter to come part way out. The catheter came | | part way out after 13 of 14 dwell positions had been completed. Just before | | the commencement of the 14th dwell position the catheter was pulled out and | | the physicist immediately intervened and retracted the source such that the | | 14th dwell position was underdosed between 10 and 60%. The worst case is | | that the 14th dwell position, which was outside of the tumor volume, would | | have received as little as 40% of the original planned dose at that | | location. | | | | NRC Region 3 (Kevin Null) was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36873 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 04/07/2000| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 17:15[EDT]| | RXTYPE: [2] GE-4 |EVENT DATE: 04/07/2000| +------------------------------------------------+EVENT TIME: 14:00[EDT]| | NRC NOTIFIED BY: S. MAREK |LAST UPDATE DATE: 04/07/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS KOZAK R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | "C" MAIN STEAM LINE FAILS LOCAL LEAK RATE TEST DUE TO EXCESSIVE LEAKAGE | | | | During Local Leak Rate Testing (LLRT) of the "C" Main Steam Line, the | | as-found leakage could not be quantified. Technical Specification | | surveillance requirement, SR 3.6.1.3.12 limit of less than 100 scfh combined | | MSIV leakage rate for all four main steam lines when tested at greater than | | 25 psig was exceeded. Fermi 2 Main Steam Lines are equipped with a Main | | Steam Line Isolation Valve Leakage Control System (MSIVLCS) which is | | designed to maintain pressure between the MSIVs slightly above that of | | primary containment. Since the leakage could not be quantified, it could | | not be demonstrated that the leakage did not exceed the capacity of the | | MSIVLCS. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * UPDATE ON 04/07/00 AT 1836 EDT BY S. MAREK TAKEN BY MACKINNON * * * | | | | During LLRT of the "D" Main Steam Line, the as-found leakage could not be | | quantified. Technical Specification surveillance requirement, SR 3.6.1.3.12 | | limit of less than 100 scfh combined MSIV leakage rate for all four main | | steam lines when tested at greater than 25 psig was exceeded. Fermi 2 Main | | Steam Lines are equipped with a MSIVLCS which is designed to maintain | | pressure between the MSIVs slightly above that of primary containment. | | Since the leakage could not be quantified, it could not be demonstrated that | | the leakage did not exceed the capacity of the MSIVLCS. The "A" & "B" Main | | Steam Lines passed their LLRT. | | | | The NRC Resident Inspector was notified of this update by the licensee. | | R3DO (T. Kozak) was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36874 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 04/07/2000| | UNIT: [] [2] [] STATE: GA |NOTIFICATION TIME: 17:56[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 04/07/2000| +------------------------------------------------+EVENT TIME: 16:15[EDT]| | NRC NOTIFIED BY: BARRY COLEMAN |LAST UPDATE DATE: 04/07/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEVE CAHILL R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RECEIVED PARTIAL GROUP 1 (MSIVs) AND GROUP 2 (Primary Containment) OUTBOARD | | ISOLATIONS. | | | | Received a partial Group 1 and Group 2 outboard isolation which caused 13 | | outboard isolation valves to close. | | The following outboard isolation valves closed: 4 hydrogen and oxygen | | sample valves, 3 Fission Product Monitor sample valves, Drywell floor drain | | valve, Drywell equipment drain valve, Drywell Air Purge and Vent line | | valves, Primary Coolant Sample line valve, and a Main Steam Line drain | | valve. All the outboard valves belong to Group 1 except for the last two | | listed which belong to Group 2. Electricians were replacing covers on | | divisional separation wiring trays in the outboard isolation panel | | 2H11-P623. Insulation on a wire was damaged causing a fuse to blow. An | | evaluation is in progress to determined if the wire can be tapped or a new | | wire will be installed. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36875 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 04/07/2000| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 17:54[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 04/07/2000| +------------------------------------------------+EVENT TIME: 14:05[EDT]| | NRC NOTIFIED BY: RAYMOND L. LANDIS |LAST UPDATE DATE: 04/07/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JACK MCFADDEN R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BLOWN FUSE CAUSED A PARTIAL SYSTEM ISOLATION | | | | A partial system isolation occurred on the containment instrument gas system | | and the drywell chilled water system. The cause of the partial isolation is | | a blown fuse. | | | | At the time of this event, Unit 1 was in Operational Condition 5 undergoing | | refueling. There was no release of radiation or loss of vessel inventory or | | shutdown cooling. Proper system response is being verified. The fuse will | | be replaced and all valves will be placed back in their proper position. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36876 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 04/07/2000| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 18:07[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/07/2000| +------------------------------------------------+EVENT TIME: 10:14[CDT]| | NRC NOTIFIED BY: JOHN MILLIFF |LAST UPDATE DATE: 04/07/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JEFF SHACKELFORD R4 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POWER EXCURSION TO 104% OF THERMAL RATED POWER | | | | Power excursion to 104% occurred when a deaerator level channel was | | improperly removed from service for calibration and caused a loss of | | deaerator level and pressure control. This resulted in an increase in | | feedwater and steam flow to the deaerator, which in turn caused reactor | | power to increase above rated values. Operators took action to terminate | | the transient and stabilized Unit 2 at 99% power. The length of the | | excursion was approximately 3 minutes. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36877 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 04/07/2000| | UNIT: [] [] [3] STATE: CA |NOTIFICATION TIME: 19:11[EDT]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 04/07/2000| +------------------------------------------------+EVENT TIME: 15:33[PDT]| | NRC NOTIFIED BY: BILL CONKLIN |LAST UPDATE DATE: 04/07/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JEFF SHACKELFORD R4 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 100 Power Operation |74 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECHNICAL SPECIFICATION SHUTDOWN DUE TO A DROPPED CONTROL ELEMENT ASSEMBLY | | (CEA). | | | | On April 7, 2000, around 1319 PDT, an alarm was received for a control | | element drive mechanism control system timer. In response to this alarm, | | plant operators began moving control rod subgroup 20 to the "hold" bus (4 | | rods on the hold bus). Shortly thereafter, CEA #84 (a full length CEA and | | part of shutdown bank B) dropped into the reactor core. Technical | | Specification (TS) 3.1.5, "Control Element Assembly Alignment" requires all | | full length CEAs to be aligned to within 7 inches of all other CEAs in its | | group. If this requirement can not be met within 2 hours, Action B of TS | | 3.1.5 requires Southern California Edison to initiate a plant shutdown. | | | | Plant operators initiated actions to realign CEA #84 with the remainder of | | its group. However, to minimize potential adverse affects to the fuel, | | reactor engineers have recommended a CEA withdrawal rate which will not | | allow CEA #84 to be realigned with the remainder of its group within 2 hours | | allowed by TS 3.1.5. Consequently, at 1533 PDT, Southern California Edison | | initiated a power reduction of San Onofre Unit 3. | | | | At 1557 PDT, CEA #84 was realigned to within 7 inches of the remainder of | | its group before completion of plant shutdown. | | | | Southern California Edison believes there is no safety significance to this | | event as all system operated as required. The cause of this event is under | | investigation. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36878 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 04/09/2000| | UNIT: [1] [] [] STATE: AL |NOTIFICATION TIME: 12:32[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/09/2000| +------------------------------------------------+EVENT TIME: 10:00[CDT]| | NRC NOTIFIED BY: BILL ARENS |LAST UPDATE DATE: 04/09/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEVE CAHILL R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF BOTH VITAL BUSES DURING 'B' TRAIN LOAD SHED TESTING | | | | At 1000 CDT, during Unit 1 'B' train load shed testing (performed every 18 | | months during a refueling outage), the 'A' startup transformer tripped, | | resulting in a loss of offsite power to both trains of Unit 1 vital buses, | | the autostart of 'A' train emergency diesel generators (EDGs) which | | reenergized the 'A' train buses, and the sustained deenergization of the 'B' | | train vital buses. | | | | At the time of this event, Unit 1 was defueled, with the 'B' train service | | water system out of service and the 'B' train EDG unavailable to Unit 1. | | Both trains of Unit 1 vital power were aligned to the '1A' startup | | transformer as part of the load shed test that was in progress. The loss of | | the '1A' startup transformer coincided with, and appears to be associated | | with, the removal of a jumper from a 'B' train sequencer relay. | | Investigation of this apparent cause is continuing. | | | | The 'A' train vital buses were immediately restored to service by the 'A' | | train EDGs. | | | | At 1018 CDT, spent fuel pool cooling was manually restored. Spent fuel pool | | temperature remained at 98�F throughout this event. | | | | At 1019 CDT. the 'B' train buses were manually reenergized from the '1B' | | startup transformer. | | | | At 1053 CDT, the 'A' train buses were transferred from the EDGs to offsite | | power. | | | | Unit 2 remains at 100% power and is unaffected by this event. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021