Event Notification Report for April 7, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/06/2000 - 04/07/2000 ** EVENT NUMBERS ** 36053 36868 36870 36871 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Hospital |Event Number: 36053 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNIVERSITY OF CT HEALTH CENTER |NOTIFICATION DATE: 08/21/1999| |LICENSEE: UNIVERSITY OF CT HEALTH CENTER |NOTIFICATION TIME: 14:31[EDT]| | CITY: FARMINGTON REGION: 1 |EVENT DATE: 08/20/1999| | COUNTY: STATE: CT |EVENT TIME: 17:45[EDT]| |LICENSE#: 0613022 AGREEMENT: N |LAST UPDATE DATE: 04/06/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PETER ESELGROTH R1 | | |JOE HOLONICH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KEN PRICE | | | HQ OPS OFFICER: WILLIAM POERTNER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE MEDICAL MISADMINISTRATION | | | | On 8/20/99, a possible medical misadministration occurred at University of | | CT Health Center located in Farmington, Conn. The physician prescribed a | | dose of 13 millicuries P-32 (Chromic Phosphate) for a lung cancer patient. | | After injection, it was determined that only 6.9 millicuries of P-32 had | | been injected. The physician issued a revised written directive for 7 | | millicuries of P-32 based on the patients condition. | | | | (Call the NRC Operations Center for a licensee contact telephone number.) | | | | * * * RETRACTION REPORTED BY KEN PRICE ON 04/06/00 AT 1622 EDT TAKEN BY | | MACKINNON * * * | | | | The licensee is retracting this event after discussions with NRC Region 1 | | (David Dwyer). The Physician changed the written directive for the amount | | of dose that the patient was to have received. Therefore, this event is not | | reportable and is being retracted. NRC R1DO (Jack McFadden) and NMSS EO | | (John Hickey) notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 36868 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: U.S. NAVY |NOTIFICATION DATE: 04/05/2000| |LICENSEE: U.S. NAVY |NOTIFICATION TIME: 13:00[EDT]| | CITY: YUMA REGION: 4 |EVENT DATE: 04/04/2000| | COUNTY: STATE: AZ |EVENT TIME: 15:30[MST]| |LICENSE#: 45-23645-01NA AGREEMENT: Y |LAST UPDATE DATE: 04/06/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BILL JONES R4 | | |STEVE CAHILL R2 | +------------------------------------------------+SCOTT MOORE NMSS | | NRC NOTIFIED BY: CDR. GARY HIGGINS | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STRONTIUM/YTTRIUM SOURCE LOST TO LANDFILL | | | | A generally licensed strontium/yttrium source, 500 mCi, from an 'In Flight | | Blade Inspection System' was improperly placed in a dumpster which in turn | | was dumped at a regular land fill. The U.S. Navy is investigating the | | incident and trying to determine where and how deep the source is in the | | land fill. | | | | The U.S. Navy notified NRC Region 2 (M. Fuller) and intends to notify the | | State of Arizona. | | | | ****************** UPDATE AT 0814 ON 04/06/00 FROM GARY HIGGINS TO LEIGH | | TROCINE ****************** | | | | The licensee called to provide the following correction to the original | | report: | | | | The licensee reported that they were provided with an incorrect activity for | | the missing source. They were originally informed that the activity was 500 | | mCi when in fact the actual activity was 500 �Ci. | | | | The licensee notified the NRC Region 2 office (Mike Fuller). The NRC | | operations officer notified the R2DO (Cahill), R4DO (Jones), and NMSS EO | | (Sturz). | | | | (Call the NRC operations officer for a licensee contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36870 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 04/06/2000| | UNIT: [] [2] [] STATE: GA |NOTIFICATION TIME: 12:38[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 04/06/2000| +------------------------------------------------+EVENT TIME: 10:00[EDT]| | NRC NOTIFIED BY: BARRY COLEMAN |LAST UPDATE DATE: 04/06/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEVE CAHILL R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | GROUP 1 ISOLATION OCCURRED DURING MAIN TURBINE CONTROL TESTING WHICH CAUSED | | THE REACTOR COOLANT SAMPLE VALVES TO CLOSE. | | | | During performance of Main Turbine Control testing, a Group 1 isolation | | occurred which caused Reactor Coolant sample valves 2B31 F019 & F020 (0.75" | | line; 1.0" valves) to close. One of the jumpers installed during the Main | | Turbine Control test made the Main Turbine Logic think that the generator | | was tied to the line. This caused the Main Turbine speed control to go to | | 1800 RPM because the main turbine speed control was selected to 1800 RPM | | instead of all valves closed. When the operator reset the Main Turbine, | | all 4 Main Turbine Stop Valves opened as a result of the speed control being | | selected to 1800 RPM. A Group 1 isolation occurred due to the Main Turbine | | stop valves opening coincident with a low Main Condenser Vacuum. Only the | | Reactor Coolant Sample Valves closed. Main Steam Isolation valves and the | | Main Steam line drain valves remained closed during the Group 1 isolation. | | The licensee is continuing the Main Turbine Control Test. | | | | | | The NRC Resident Inspector was notified of the event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36871 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 04/06/2000| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 14:02[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 04/06/2000| +------------------------------------------------+EVENT TIME: 12:05[EDT]| | NRC NOTIFIED BY: JOHN LAMB |LAST UPDATE DATE: 04/06/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JACK MCFADDEN R1 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SPENT FUEL POOL STORAGE RACKS BORAFLEX DEGRADING. | | | | | | An evaluation of a preliminary report on the Spent Fuel Pool storage racks | | Boraflex testing determined that degradation is occurring. Some racks might | | not be able to receive fuel and ensure the Technical Specification | | requirement of maintaining Keff <= to 0.95 with un-borated water could be | | assured. Administrative controls will ensure that Keff is maintained <= to | | 0.95. The design of the fuel racks was to allow full core off-loads for the | | term of the license. | | | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021