The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for April 3, 2000

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           03/31/2000 - 04/03/2000

                              ** EVENT NUMBERS **

36737  36825  36849  36850  36851  36852  36853  36854  36855  36856  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36737       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MILLSTONE                REGION:  1  |NOTIFICATION DATE: 02/28/2000|
|    UNIT:  [] [2] []                 STATE:  CT |NOTIFICATION TIME: 23:29[EST]|
|   RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP           |EVENT DATE:        02/28/2000|
+------------------------------------------------+EVENT TIME:        23:09[EST]|
| NRC NOTIFIED BY:  STEVEN BAKER                 |LAST UPDATE DATE:  03/31/2000|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JIM TRAPP            R1      |
|10 CFR SECTION:                                 |                             |
|ASHU 50.72(b)(1)(i)(A)   PLANT S/D REQD BY TS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |97       Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TECH SPEC REQUIRED SHUTDOWN - BACKLEAKAGE FROM THE S/G TO THE AUXILIARY      |
| FEEDWATER SYSTEM.                                                            |
|                                                                              |
| Check valve leakage from the # 1 Steam Generator caused a rise in            |
| temperature in the discharge piping of the "A" auxiliary feedwater pump.     |
| The maximum allowed temperature is 190 degrees F.  The maximum temperature   |
| reached was 300 degrees F.  The licensee entered Tech Spec 3.0.3 at 1209 and |
| started slowly lowering power.    Injection with the "A" AFW pump reduced    |
| the temperature in the line below the limit.  The licensee is waiting to     |
| determine if the check valve has reseated.                                   |
|                                                                              |
| The licensee notified the NRC resident inspector, the town of Waterford and  |
| the state of Connecticut.                                                    |
|                                                                              |
| * * * UPDATE 0026 2/29/2000 FROM JOHN CLAIR TAKEN BY BOB STRANSKY * * *      |
|                                                                              |
| TS 3.0.3 was exited at 2338 2/28/2000. The unit is returning to rated power. |
| The NRC resident inspector will be informed of this update by the licensee.  |
| Notified R1DO (Trapp).                                                       |
|                                                                              |
| * * * RETRACTION 0833 3/31/2000 FROM KENNETH TRUSDALE TAKEN BY STRANSKY * *  |
| *                                                                            |
|                                                                              |
| "This call is to retract a call made on 2/28/2000 under 10 CFR 50.72         |
| regarding entry into Tech Spec Action Statement 3.0.3, as the plant was in a |
| condition prohibited by the Tech Specs. The original notification was made   |
| because the Shift Manager had indication that the auxiliary feedwater piping |
| temperature was above normal, and he did not have enough information or      |
| guidance at that time to determine that the auxiliary feedwater system was   |
| operable. As operability was indeterminate, the Shift Manager conservatively |
| assumed the auxiliary feedwater system was inoperable, which is a condition  |
| prohibited by the plant Technical Specifications. Subsequent research and    |
| investigation determined that the auxiliary feedwater system was operable    |
| throughout the event and the plant was not in a condition prohibited by the  |
| Technical Specifications.                                                    |
|                                                                              |
| "As the plant was not in a condition prohibited by the Technical             |
| Specifications, there was no requirement to enter Action Statement 3.0.3.    |
| The notification made on 2/28/2000 is withdrawn."                            |
|                                                                              |
| The NRC resident inspector has been informed of this retraction by the       |
| licensee. Notified R1DO (Evans).                                             |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36825       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: INDIAN POINT             REGION:  1  |NOTIFICATION DATE: 03/23/2000|
|    UNIT:  [2] [] []                 STATE:  NY |NOTIFICATION TIME: 13:11[EST]|
|   RXTYPE: [2] W-4-LP,[3] W-4-LP                |EVENT DATE:        03/23/2000|
+------------------------------------------------+EVENT TIME:        12:00[EST]|
| NRC NOTIFIED BY:  DENNIS CORNAX                |LAST UPDATE DATE:  03/31/2000|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LOUIS MANNING        R1      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| C-3 DEFECTS DETECTED DURING EDDY CURRENT INSPECTION OF STEAM GENERATORS      |
|                                                                              |
| Indian Point 2 is conducting eddy current testing of 100% of the steam       |
| generator (SG) tubes.  With about 90% of the inspection complete, SG-21 and  |
| SG-24 tubes have defects in greater than 1% of the tubes inspected.  SG-22   |
| and SG-23 have defects in much less than 1% of the tubes inspected.  The     |
| majority of the defects are at the support plate intersections and in row 2  |
| U-bends.  There are 41 indications in SG-21, 40 at the support plate and 1   |
| in the U-bend.  There are 39 indications in SG-24, 36 at the support plate   |
| and 3 in the U-bend.  In accordance with Technical Specification 4.13, these |
| defects result in a C-3 classification.  The testing will continue until     |
| 100% of the tubes are inspected.                                             |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
|                                                                              |
| UPDATE ON 3/31/2000 BY LAMB, RECEIVED BY WEAVER * * *                        |
|                                                                              |
| This report is being made as a follow up to previously reported event number |
| 36825.  At approximately 1500 today, the tube at Row 2 Column 69 in steam    |
| generator 24 failed the three delta pressure requirement during in-situ      |
| pressure testing being performed in accordance with NEI 97-06 guidelines to  |
| meet Technical Specification requirements.  The three delta pressure value   |
| was calculated to be 5118 psi, and with uncertainties applied, the test      |
| pressure was specified at 5173 psi.  Shortly after achieving 5173 psi for    |
| the required two seconds specified in the test, pressure was noted to        |
| rapidly drop indicating leakage.  No leakage was observed at a steam line    |
| test pressure of 2841 psi.  Therefore, that performance criterion was met.   |
|                                                                              |
| The licensee notified the NRC resident inspector.  The operations center     |
| notified the R1DO (Evans).                                                   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   36849       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  FLORIDA BUREAU OF RADIATION CONTROL  |NOTIFICATION DATE: 03/31/2000|
|LICENSEE:  J. B. COXWELL CONTRACTING, INC.      |NOTIFICATION TIME: 07:31[EST]|
|    CITY:  JACKSONVILLE             REGION:  2  |EVENT DATE:        03/31/2000|
|  COUNTY:                            STATE:  FL |EVENT TIME:             [EST]|
|LICENSE#:  FL 2904-1             AGREEMENT:  Y  |LAST UPDATE DATE:  03/31/2000|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CAUDLE JULIAN        R2      |
|                                                |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  JERRY EAKINS                 |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT - STOLEN MOISTURE/DENSITY GAUGE                       |
|                                                                              |
| The Florida Bureau of Radiation Control reported the theft of a Troxler      |
| Model 3430 moisture/density gauge (Serial Number 2904-1) from a state        |
| licensee. The theft occurred sometime between 0000 and 0600 on 3/31/2000     |
| from the parking lot of a motel in Jacksonville, FL. The gauge was stored in |
| its case, which was chained to the bed of a pickup truck. The chain was cut, |
| and both the gauge and case were taken. The theft has been reported to the   |
| Jacksonville Police Department. The state has requested that the licensee    |
| post a reward for the return of the gauge, and is helping the licensee to    |
| prepare a press release regarding this incident.                             |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36850       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 03/31/2000|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 15:10[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        03/31/2000|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:             [CST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  03/31/2000|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |RONALD GARDNER       R3      |
|  DOCKET:  0707001                              |BRIAN SMITH          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  ERIC WALKER                  |                             |
|  HQ OPS OFFICER:  DOUG WEAVER                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBB 76.120(c)(2)(ii)    EQUIP DISABLED/FAILS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| CRITICALITY ACCIDENT ALARM SYSTEM FAILURE DURING A TEST                      |
|                                                                              |
| At 1845 on 03-30-2000, during functional testing of C-746Q Criticality       |
| Accident Alarm System (CAAS), it was discovered that temperature control     |
| system on cluster "AD"  was unable to perform the ability to maintain the    |
| system above the manufacturer's fourteen degree Fahrenheit recommendation    |
| due to failure of a temperature switch.  The system was last tested on       |
| 12-30-99 and was determined to be functional at that time. In January of     |
| this year there were several days were outside ambient temperature dropped   |
| below fourteen degrees Fahrenheit and operability of system at those times   |
| cannot be reasonably determined.  Even though the failure was discovered     |
| during testing, it is possible that the system would not have performed its  |
| intended safety function if it had been required to since the last           |
| surveillance on 12-30-99.                                                    |
|                                                                              |
| This event is reportable under 10 CFR 76.120(c)(2) as an event in which      |
| equipment required by the TSR is disabled or fails to function as designed.  |
|                                                                              |
| The NRC Senior Resident Inspector has been notified of this event.           |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36851       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HARRIS                   REGION:  2  |NOTIFICATION DATE: 03/31/2000|
|    UNIT:  [1] [] []                 STATE:  NC |NOTIFICATION TIME: 15:40[EST]|
|   RXTYPE: [1] W-3-LP                           |EVENT DATE:        03/31/2000|
+------------------------------------------------+EVENT TIME:        14:48[EST]|
| NRC NOTIFIED BY:  MAURICE GRIFFIN              |LAST UPDATE DATE:  03/31/2000|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CAUDLE JULIAN        R2      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| A CONTRACT EMPLOYEE WAS INAPPROPRIATELY GRANTED UNESCORTED ACCESS.  ACCESS   |
| HAS BEEN SUSPENDED PENDING FURTHER INVESTIGATION.  THE LICENSEE WILL NOTIFY  |
| THE NRC RESIDENT INSPECTOR.  ADDITIONAL DETAILS ARE AVAILABLE FROM THE NRC   |
| OPERATIONS CENTER.                                                           |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36852       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FT CALHOUN               REGION:  4  |NOTIFICATION DATE: 04/01/2000|
|    UNIT:  [1] [] []                 STATE:  NE |NOTIFICATION TIME: 11:02[EST]|
|   RXTYPE: [1] CE                               |EVENT DATE:        04/01/2000|
+------------------------------------------------+EVENT TIME:        09:20[CST]|
| NRC NOTIFIED BY:  LARRY LEES                   |LAST UPDATE DATE:  04/01/2000|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |KRISS KENNEDY        R4      |
|10 CFR SECTION:                                 |                             |
|ASHU 50.72(b)(1)(i)(A)   PLANT S/D REQD BY TS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Hot Standby      |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TECH SPEC REQUIRED SHUTDOWN DUE TO EMERGENCY FEEDWATER STORAGE TANK LEVEL    |
| DECREASING BELOW TECH SPEC LIMIT                                             |
|                                                                              |
| THE PLANT ENTERED ABNORMAL OPERATING PROCEDURE (AOP) 30, "EMERGENCY FILL OF  |
| EMERGENCY FEEDWATER STORAGE TANK," AS A RESULT OF THE EMERGENCY FEEDWATER    |
| STORAGE TANK LEVEL FALLING BELOW TECH SPEC LOW LIMIT OF 91%.  THIS RESULTED  |
| IN ENTRY INTO TECH SPEC 2.0.1 WHICH DIRECTS PLACING THE PLANT IN HOT         |
| SHUTDOWN WITHIN 6 HOURS, LESS THAN 300 DEGREES F IN ANOTHER 6 HOURS AND IN   |
| COLD SHUTDOWN IN 30 HOURS.  AT THE TIME OF ENTRY INTO THIS TECH SPEC THE     |
| PLANT WAS ALREADY IN HOT SHUTDOWN.  ACTIONS TO REFILL THE EMERGENCY          |
| FEEDWATER STORAGE TANK WERE TAKEN BY OPENING THE CONDENSATE FILL LINE AND    |
| EMERGENCY FILLING.  FILLING WAS IN PROGRESS BEFORE GOING BELOW 91%, HOWEVER, |
| SYSTEM DEMAND WAS GREATER THAN THE MAKEUP ABILITY OF THE DEMINERALIZED WATER |
| SOURCE (STEAM GENERATOR WATER SUPPLY SWAPOVER).  LEVEL WAS ABOVE 91% AT      |
| 0944CST AT WHICH TIME AOP 30 AND TECH SPEC 2.0.1 WERE EXITED.                |
|                                                                              |
| THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR.                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36853       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FITZPATRICK              REGION:  1  |NOTIFICATION DATE: 04/01/2000|
|    UNIT:  [1] [] []                 STATE:  NY |NOTIFICATION TIME: 21:04[EST]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        04/01/2000|
+------------------------------------------------+EVENT TIME:        17:38[EST]|
| NRC NOTIFIED BY:  TOM PLUMPTON                 |LAST UPDATE DATE:  04/01/2000|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MICHELE EVANS        R1      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       26       Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| REACTOR SCRAM                                                                |
|                                                                              |
| During a planned power reduction, the recombiner was removed from service.   |
| The recombiner bypass valve shut, reason unknown, isolating all off gas      |
| flow.  Vacuum decayed as a result.  The main turbine was manually tripped,   |
| followed by an automatic reactor scram.                                      |
|                                                                              |
| Three rods did not indicate fully inserted immediately after the trip, but   |
| were later verified to be full in.  The recirculating pumps are running and  |
| steam is being dumped to the main condenser (vacuum was restored) to remove  |
| decay heat.                                                                  |
|                                                                              |
| The licensee informed the NRC resident inspector and will make a press       |
| release.                                                                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36854       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FERMI                    REGION:  3  |NOTIFICATION DATE: 04/01/2000|
|    UNIT:  [2] [] []                 STATE:  MI |NOTIFICATION TIME: 22:28[EST]|
|   RXTYPE: [2] GE-4                             |EVENT DATE:        04/01/2000|
+------------------------------------------------+EVENT TIME:        19:15[EST]|
| NRC NOTIFIED BY:  KEVIN DAHM                   |LAST UPDATE DATE:  04/01/2000|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |RONALD GARDNER       R3      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2     M/R        Y       23       Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| REACTOR SCRAM                                                                |
|                                                                              |
| On Saturday 4/1/2000, at 1200 hours, control room operators commenced a      |
| planned unit shutdown in preparation for refueling outage number 7.   At     |
| 1815 hours, the 'A' Reactor Recirculation Pump exhibited speed fluctuations  |
| and was tripped.  The crew conducted an evaluation to determine existing     |
| procedure guidance for operation at low power and low flow in a single loop  |
| configuration, and conservatively decided to shut down the reactor.  At 1915 |
| hours, the Reactor Operator placed the Reactor Mode Switch in Shutdown       |
| inserting a manual scram from 23% reactor power.  All control rods fully     |
| inserted.   All systems operated as expected, no safety/relief valves opened |
| and no ECCS systems initiated/actuated.                                      |
|                                                                              |
| The lowest reactor water level observed was 163 inches, normal operating     |
| band is 196 inches, all level three isolations (173 inches) came in as       |
| expected.  At present, reactor water level is operating in normal operating  |
| band and is being maintained on the startup level control valve.   No steam  |
| leaks noted.                                                                 |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36855       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FARLEY                   REGION:  2  |NOTIFICATION DATE: 04/02/2000|
|    UNIT:  [1] [2] []                STATE:  AL |NOTIFICATION TIME: 07:25[EDT]|
|   RXTYPE: [1] W-3-LP,[2] W-3-LP                |EVENT DATE:        04/02/2000|
+------------------------------------------------+EVENT TIME:        05:05[CDT]|
| NRC NOTIFIED BY:  BILL ARENS                   |LAST UPDATE DATE:  04/02/2000|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CAUDLE JULIAN        R2      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 1 HOUR SECURITY REPORT                                                       |
|                                                                              |
| UNESCORTED PROTECTED AREA ACCESS GRANTED INAPPROPRIATELY.  IMMEDIATE         |
| COMPENSATORY MEASURES TAKEN.  THE LICENSEE WILL INFORM THE NRC RESIDENT      |
| INSPECTOR.                                                                   |
|                                                                              |
| CONTACT THE HEADQUARTERS OPERATIONS CENTER FOR ADDITIONAL DETAILS.           |
|                                                                              |
| * * * UPDATE 0955EDT ON 4/2/00 FROM VINCE MURPHY TO S.SANDIN * * *           |
|                                                                              |
| THE LICENSEE PROVIDED ADDITIONAL SPECIFIC INFORMATION.  A REVIEW WILL BE     |
| PERFORMED ON MONDAY 4/3 TO DETERMINE REPORTABILITY.  NOTIFIED R2DO (JULIAN). |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36856       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HARRIS                   REGION:  2  |NOTIFICATION DATE: 04/02/2000|
|    UNIT:  [1] [] []                 STATE:  NC |NOTIFICATION TIME: 09:38[EDT]|
|   RXTYPE: [1] W-3-LP                           |EVENT DATE:        04/02/2000|
+------------------------------------------------+EVENT TIME:        09:17[EDT]|
| NRC NOTIFIED BY:  STAN LOWE                    |LAST UPDATE DATE:  04/02/2000|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNU                   |CAUDLE JULIAN        R2      |
|10 CFR SECTION:                                 |JOHN ZWOLINSKI       NRR     |
|AAEC 50.72 (a) (1) (I)   EMERGENCY DECLARED     |CHARLES MILLER       IRO     |
|                                                |CEGIELSKI            FEMA    |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNUSUAL EVENT DECLARED DUE TO LOSS OF THE EMERGENCY RESPONSE FACILITY        |
| INFORMATION SYSTEM (ERFIS) FOR GREATER THAN 4 HOURS                          |
|                                                                              |
| AT 0917EDT THE LICENSEE DECLARED AN UNUSUAL EVENT BASED ON EMERGENCY ACTION  |
| LEVEL (EAL) 6-2-1, "INABILITY OF ERFIS TO PERFORM ITS INTENDED FUNCTION FOR  |
| A CONTINUOUS PERIOD OF 4 HOURS."  BOTH THE "A" AND "B" PLANT PROCESS         |
| COMPUTERS WHICH SUPPLY INPUT DATA TO ERFIS WOULD NOT REBOOT FOR REASONS      |
| UNKNOWN.  ADDITIONAL INFORMATION TECHNOLOGY (IT) STAFF HAS BEEN BROUGHT IN   |
| TO RESOLVE THE FAILURE.  THE LICENSEE HAS IMPLEMENTED MONITORING ON          |
| REDUNDANT EQUIPMENT IN ACCORANCE WITH TECH SPEC REQUIREMENTS.  THE UNIT IS   |
| CURRENTLY STABLE AT 100% POWER.                                              |
|                                                                              |
| THE LICENSEE INFORMED STATE AND COUNTY AGENCIES AND WILL INFORM THE NRC      |
| RESIDENT INSPECTOR.                                                          |
|                                                                              |
| * * * UPDATE AT 1644 ON 4/2/00, BY LOWE RECEIVED BY WEAVER * * *             |
|                                                                              |
| The licensee terminated the Unusual Event at 1630 after having repaired and  |
| tested the ERFIS system.  The licensee informed the NRC resident inspector   |
| as well as state and county agencies.  The Operations Center notified the    |
| RDO (Julian), EO (Zwolinski) and FEMA (Cegielski).                           |
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Page Last Reviewed/Updated Thursday, March 25, 2021