Event Notification Report for March 15, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/14/2000 - 03/15/2000 ** EVENT NUMBERS ** 36791 36792 36793 36794 36795 36796 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36791 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 03/14/2000| | UNIT: [1] [] [] STATE: AR |NOTIFICATION TIME: 03:11[EST]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 03/14/2000| +------------------------------------------------+EVENT TIME: 00:05[CST]| | NRC NOTIFIED BY: ALAN SMITH |LAST UPDATE DATE: 03/14/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID GRAVES R4 | |10 CFR SECTION: |BRUCE BOGER NRR | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 82 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 MANUALLY TRIPPED FOLLOWING A FAILURE OF THE MAIN TURBINE GOVERNOR | | VALVES CONTROL SYSTEM | | | | "The Unit 1 Reactor was manually tripped following a failure of the main | | turbine governor valves control system. This failure resulted in the main | | turbine governor valves inadvertently going closed. At the time of the | | event, Unit 1 was at 82% power and proceeding to 100% power following the | | completion of maintenance outage 1P-00-2. | | | | "Unit 1 has been stabilized in Hot Shutdown (550 degrees F, 2125 psig, and | | the reactor is subcritical). No radioactive releases have occurred nor are | | any planned." | | | | Prior to the transient the turbine governor valve position limit was acting | | erratically. All control rods fully inserted. Following the trip, primary | | pressure increased to 2300 psig. Three(3) of eight(8) mainsteam (MS) | | safeties lifted and reseated on each MS header. Also, Bus "1H1" which | | supplies power to two Reactor Coolant Pumps (RCPs) was slow in transferring | | to the startup transformer. This resulted in both "P32A" and P32C" RCPs | | tripping. The 1H1 bus remained energized during the transient. | | | | Unit 1 is currently removing decay heat using RCPs "P32B" and P32D" (one | | operating in each reactor coolant loop) with steam discharging to the Main | | Condenser. All safety-related equipment including the Emergency Diesel | | Generators (EDGs) is available, if needed. I&C is investigating the cause | | of the governor valves' control system failure and the Relay Department is | | evaluating the slow bus transfer. | | | | The licensee informed the NRC Resident Inspector and the State of Arkansas. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36792 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 03/14/2000| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 04:01[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/14/2000| +------------------------------------------------+EVENT TIME: 00:35[EST]| | NRC NOTIFIED BY: BILL HARRIS |LAST UPDATE DATE: 03/14/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |EDWARD MCALPINE R2 | |10 CFR SECTION: |BRUCE BOGER NRR | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL PHASE "A" AND CONTAINMENT VENT ISOLATION INITIATED DUE TO SHUTDOWN | | LOSS OF COOLANT ACCIDENT (LOCA). | | | | "Unit 1 was in Mode 5 with Cycle 10 refueling outage in progress. At 0017 | | on 3/14/00 with RCS temperature at 145 F and RCS pressure at 330 psig. Unit | | 1 entered Abnormal Operating Procedure R.02 (Shutdown LOCA) due to | | decreasing pressurizer level. A manual Phase A and Containment Vent | | Isolation were initiated at 0035 as required by procedure. The loss of RCS | | coolant was initially contained in the Pressurizer Relief Tank (PRT) until | | the PRT rupture disc ruptured. At 0125, AOP R.02 was completed and plant | | conditions were stabilized with RCS temperature at 156 F and RCS pressure at | | 145 psig. At present there is no RCS leakage, plant conditions are stable, | | and suspected cause is the RHR suction or discharge piping relief valve. | | Investigation is in progress." | | | | The transient lasted approximately 30 minutes. The licensee suspects that | | when RCS pressure was lowered per the AOP, the relief valve reseated. There | | is no estimate of the lost RCS inventory at this time. | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36793 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 03/14/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 08:40[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 03/13/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 22:25[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/14/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |JOHN JACOBSON R3 | | DOCKET: 0707001 |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: E.G. WALKER | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NON-CFR REPORT INVOLVING ACTUATION OF A SAFETY SYSTEM DUE TO A VALID | | SIGNAL | | | | "At 2225 on 03/13/00, the PSS office was notified that a primary condensate | | alarm was received on the C-333A position 2 North autoclave Water Inventory | | Control System (WICS). The WICS system is required to be operable while | | heating in mode 5 according to TSR 2.2.4.2. The autoclave was checked | | according to the alarm response procedure, removed from service and the | | Water Inventory Control System was declared inoperable by the Plant Shift | | Superintendent. Troubleshooting was initiated and is continuing in order to | | determine the reason for the alarm. | | | | "The safety system actuation Is reportable to the NRC as required by Safety | | Analysis Report, section 8.9, table 1 criteria J.2, Safety System actuation | | due to a valid signal as a 24-hour event notification. | | | | "The NRC resident inspector has been notified of this event." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36794 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: DEPARTMENT OF THE ARMY |NOTIFICATION DATE: 03/14/2000| |LICENSEE: DEPARTMENT OF THE ARMY |NOTIFICATION TIME: 14:52[EST]| | CITY: ROCK ISLAND REGION: 3 |EVENT DATE: 03/13/2000| | COUNTY: STATE: IL |EVENT TIME: 12:00[CST]| |LICENSE#: 12-00722-06 AGREEMENT: Y |LAST UPDATE DATE: 03/14/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN JACOBSON R3 | | |DAVID GRAVES R4 | +------------------------------------------------+FRITZ STURZ NMSS | | NRC NOTIFIED BY: HAVENNER | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE DEPARTMENT OF THE ARMY REPORTED A CHEMICAL AGENT DETECTOR (CAD) WAS LOST | | AT FT. HOOD, TX. | | | | A M43A1 CAD CONTAINING 250 MICROCURIES OF AM-241 WAS LOST FOLLOWING A FIELD | | TRAINING EXERCISE AT FT. HOOD, TX. THE DEVICE WAS RUN OVER BY A VEHICLE ON | | 3/1/00 AND UPON RETRIEVAL, THE PIECES WERE PLACED IN TWO OPAQUE PLASTIC BAGS | | AND TAKEN BACK TO THE INSTALLATION WHERE IT WAS DETERMINED (ON 3/7/00) THEY | | HAD BEEN LOST. IT IS BELIEVED THAT THE TWO BAGS WERE DISCARDED WITH THE | | TRASH IN THE ON-POST LANDFILL. A SEARCH OF THE LANDFILL WAS IMPLEMENTED, | | BUT THE BAGS COULD NOT BE FOUND. SINCE THE GENERAL PUBLIC DOES NOT HAVE | | ACCESS TO THIS LANDFILL, THE ARMY HAS TERMINATED ITS SEARCH. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36795 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 03/14/2000| | UNIT: [] [2] [] STATE: GA |NOTIFICATION TIME: 16:12[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/14/2000| +------------------------------------------------+EVENT TIME: 13:18[EST]| | NRC NOTIFIED BY: UNDERWOOD |LAST UPDATE DATE: 03/14/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD AN ESF ACTUATION WHILE PERFORMING A LEAK RATE TEST. | | | | While performing leak rate testing on 2E11-F041D, Drywell Pressure Sensing | | Line Isolation Valve, a High Drywell Pressure Signal was received resulting | | in the following actuations: | | | | Reactor Scram Signal (RPS),(no rod motion) | | Unit 1 and Unit 2 Standby Gas Treatment System actuation, | | Unit 1 Reactor Building Ventilation isolation. | | | | Group 2 Isolation of: | | Drywell Sump Isolation Valve (2G11-F004), | | Post Accident Sampling Valve (2E41-F121), | | Fission Product Monitor Valve (2D1 l-F072), and | | Unit 1 and Unit 2 Refueling Ventilation Isolation. | | | | Other valves did not activate on the Group 2 Isolation signal from High | | Drywell Pressure because they were out of service for refueling outage | | maintenance activities. | | | | Investigation is ongoing as to the cause of this event. | | | | All systems have been returned to normal status. | | | | The NRC Resident Inspector will be notified. | | | | Refer to related event #36796. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36796 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 03/15/2000| | UNIT: [] [2] [] STATE: GA |NOTIFICATION TIME: 00:58[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/14/2000| +------------------------------------------------+EVENT TIME: 22:45[EST]| | NRC NOTIFIED BY: BRUCE BUTLER |LAST UPDATE DATE: 03/15/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - ESF ACTUATIONS DURING A RELAY REPLACEMENT CAUSED BY AN ELECTRICAL SHORT - | | | | | | While replacing the relay for TIP withdrawal & RHR valve #2A71B-K5C in | | Reactor Protection System relay panel #2H11-P609, an electrician caused an | | electrical short which resulted in the following: | | | | - Units 1 & 2 Standby Gas Treatment System actuation (1A, 1B, 2A and 2B | | trains/fans started) | | - Units 1 & 2 Outboard [B] Reactor Building Ventilation System isolation | | - Units 1 & 2 Outboard [B] Refueling Floor Ventilation System isolation | | - Discovered Group 2 Outboard Post Accident Sampling Isolation Valve | | #2E41-F121 closed | | - Discovered Group 2 Outboard Fission Product Monitor Valve #2D11-F072 | | closed | | | | The licensee is investigating the cause of this event. | | | | The licensee plans to return the above systems and components to normal | | status as soon as possible. | | | | The licensee plans to notify the NRC Resident Inspector. | | | | Refer to related event #36795. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021