Event Notification Report for March 14, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/13/2000 - 03/14/2000 ** EVENT NUMBERS ** 36709 36790 36791 36792 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36709 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/19/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 09:52[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/18/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 13:25[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/13/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |BRUCE JORGENSEN R3 | | DOCKET: 0707001 | | +------------------------------------------------+ | | NRC NOTIFIED BY: BEASLEY | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR NOTIFICATION - FAILURE OF THE UF6 RELEASE DETECTION SYSTEM | | | | At 1325 CST, on 2/18/00, the Plant Shift Superintendent (PSS) was notified | | of an air leak on the C-310 Cylinder Valve Closure System. The function of | | this system is to close the cylinder valve in the case of an actuation of | | the UF6 Release Detection and Isolation System Low Voltage ("New") System at | | the UF6 Withdrawal Stations. TSR 2.3.4.1 requires this system to be | | operable while operating in mod 2. At the time the leak was discovered, | | the air pressure on the Cylinder Valve Closure System was being maintained | | within allowed parameters. However due to the size of the leak, it was | | questionable as to if the system could maintain enough air pressure to | | perform its intended safety function, if it were called upon. After | | discussing with the C-310 building System Engineer, the PSS could not be | | provided with reasonable assurance of operability. The UF6 Release | | detection System was declared inoperable by the PSS, and repair of the | | system was initiated. TSR required LCO actions were implemented. Repair of | | the air leak was completed, and the UF6 Release Detection System was | | returned to Operable status at 1706 CST, on 2/18/00. | | | | This event is reportable under 10 CFR 7B.120(c)(2) as an event in which | | equipment required by the TSR is disabled or fails to function as designed. | | | | The NRC Senior Resident inspector has been notified of this event and the | | DOE on site representative was also informed. | | | | * * * UPDATE ON 3/13/00 @ 1438 BY WALKER TO GOULD * * * RETRACTION | | | | THIS EVENT HAS BEEN RETRACTED. Engineering Evaluation EN-C-826-00-018 | | concluded that the capacity of the backup nitrogen supply regulator was | | sufficient to provide for this backflow and loss of system air, and still | | capable of providing flow to close two cylinder valves simultaneously. | | Thus, the system was capable of performing its intended safety function | | using nitrogen had it been called upon during the time of the subject event | | and the 10CFR76.120 reporting criteria were not met. Given the results of | | this Engineering Evaluation, this event is being retracted. | | | | The NRC Resident Inspector was informed and the Reg 3 RDO(Jacobson) and NMSS | | EO(Smith) were notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36790 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 03/13/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 22:00[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 03/13/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 19:57[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/13/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |JOHN JACOBSON R3 | | DOCKET: 0707002 |THOMAS ESSIG NMSS | +------------------------------------------------+JOSEPH GIITTER IRO | | NRC NOTIFIED BY: MCCLEARY | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 4 HOUR 91-01 BULLETIN RESPONSE | | | | The Plant Shift Superintendent(PSS) was notified of two seal test buggies on | | the cell floor of the X-333 facility containing a vacuum pump whose oil | | reservoir volume was greater than the NCSA PLANT 069.A00 requirement of a 1 | | quart reservoir. Boundaries were placed around the buggies and the buggies | | were made inoperable to prevent use. The NCSE allows 3 quarts for normal | | operations and an analyses for 5 quart reservoir for "abnormal operations." | | Therefore, the safety significance is low since the pumps supplied by the | | manufacturer have a reservoir volume of more than 3 quarts due to a design | | modification. The site only had 4 pumps (two installed and two on the | | shelf) with this design modification. | | | | SAFETY SIGNIFICANCE OF EVENTS: | | | | The safety significance of this event is low. The NCSE evaluates a pump | | filled to a capacity of 5 quarts and shows the system to remain subcritical. | | NCSE- PLANT 031 .E03, for similar carts, modeled a cart with a 5 quart | | vacuum pump adjacent to another cart and found that the system to be | | subcritical with a Keff +2q (sigma) of 0.841. | | | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | | | The Kinney model vacuum pump has a volume capacity of less than 4 quarts. | | For a criticality to occur, a cart with a pump with a capacity of 5 quarts | | would have to be used. The chemical traps in front of the pump would have | | to be empty or saturated such that the pump oil becomes saturated with | | uranium, and a spacing violation would have to occur. | | | | | | CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | The controlled parameters in this NCSA are volume and interaction. | | | | | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE CRITICAL MASS): | | | | The carts are approved for use with 100% enriched material. The form of the | | material is uranium in oil. This system has been modeled and the Keff | | +2q(sigma) determined to be 0.841 for this upset. | | | | | | | | NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | The pump has been modified by the manufacturer to hold more than 3 quarts | | | | | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | Established conditions as required by the Anomalous Condition procedure. | | | | The double contingency cannot be established within 4 hours and is | | reportable. | | | | | | The NRC Resident Inspector and DOE Representative were notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36791 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 03/14/2000| | UNIT: [1] [] [] STATE: AR |NOTIFICATION TIME: 03:11[EST]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 03/14/2000| +------------------------------------------------+EVENT TIME: 00:05[CST]| | NRC NOTIFIED BY: ALAN SMITH |LAST UPDATE DATE: 03/14/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID GRAVES R4 | |10 CFR SECTION: |BRUCE BOGER NRR | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 82 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 MANUALLY TRIPPED FOLLOWING A FAILURE OF THE MAIN TURBINE GOVERNOR | | VALVES CONTROL SYSTEM | | | | "The Unit 1 Reactor was manually tripped following a failure of the main | | turbine governor valves control system. This failure resulted in the main | | turbine governor valves inadvertently going closed. At the time of the | | event, Unit 1 was at 82% power and proceeding to 100% power following the | | completion of maintenance outage 1P-00-2. | | | | "Unit 1 has been stabilized in Hot Shutdown (550 degrees F, 2125 psig, and | | the reactor is subcritical). No radioactive releases have occurred nor are | | any planned." | | | | Prior to the transient the turbine governor valve position limit was acting | | erratically. All control rods fully inserted. Following the trip, primary | | pressure increased to 2300 psig. Three(3) of eight(8) mainsteam (MS) | | safeties lifted and reseated on each MS header. Also, Bus "1H1" which | | supplies power to two Reactor Coolant Pumps (RCPs) was slow in transferring | | to the startup transformer. This resulted in both "P32A" and P32C" RCPs | | tripping. The 1H1 bus remained energized during the transient. | | | | Unit 1 is currently removing decay heat using RCPs "P32B" and P32D" (one | | operating in each reactor coolant loop) with steam discharging to the Main | | Condenser. All safety-related equipment including the Emergency Diesel | | Generators (EDGs) is available, if needed. I&C is investigating the cause | | of the governor valves' control system failure and the Relay Department is | | evaluating the slow bus transfer. | | | | The licensee informed the NRC Resident Inspector and the State of Arkansas. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36792 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 03/14/2000| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 04:01[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/14/2000| +------------------------------------------------+EVENT TIME: 00:35[EST]| | NRC NOTIFIED BY: BILL HARRIS |LAST UPDATE DATE: 03/14/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |EDWARD MCALPINE R2 | |10 CFR SECTION: |BRUCE BOGER NRR | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL PHASE "A" AND CONTAINMENT VENT ISOLATION INITIATED DUE TO SHUTDOWN | | LOSS OF COOLANT ACCIDENT (LOCA). | | | | "Unit 1 was in Mode 5 with Cycle 10 refueling outage in progress. At 0017 | | on 3/14/00 with RCS temperature at 145 F and RCS pressure at 330 psig. Unit | | 1 entered Abnormal Operating Procedure R.02 (Shutdown LOCA) due to | | decreasing pressurizer level. A manual Phase A and Containment Vent | | Isolation were initiated at 0035 as required by procedure. The loss of RCS | | coolant was initially contained in the Pressurizer Relief Tank (PRT) until | | the PRT rupture disc ruptured. At 0125, AOP R.02 was completed and plant | | conditions were stabilized with RCS temperature at 156 F and RCS pressure at | | 145 psig. At present there is no RCS leakage, plant conditions are stable, | | and suspected cause is the RHR suction or discharge piping relief valve. | | Investigation is in progress." | | | | The transient lasted approximately 30 minutes. The licensee suspects that | | when RCS pressure was lowered per the AOP, the relief valve reseated. There | | is no estimate of the lost RCS inventory at this time. | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021