Event Notification Report for March 6, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/03/2000 - 03/06/2000 ** EVENT NUMBERS ** 36660 36662 36707 36750 36751 36752 36753 36754 36755 36756 36757 36758 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36660 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 02/04/2000| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 17:14[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 02/04/2000| +------------------------------------------------+EVENT TIME: 16:39[EST]| | NRC NOTIFIED BY: M VASELY |LAST UPDATE DATE: 03/03/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TONY DIMITRIADIS R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 99 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VALIDITY OF ASSUMPTIONS FOR THE 30 MINUTE NITROGEN BACKUP SUPPLY IN QUESTION | | | | | | During the review of Consolidated Edison calculation FIX-0030-02, Nitrogen | | Backup Supply for control of Auxiliary Feedwater Flow Control Valves, | | Turbine Driven Auxiliary Feedwater Pump, and Atmospheric Steam Dump | | Controls, questions arose as to the validity of the assumption statements | | that resulted in the design basis for 30 minutes of nitrogen could not be | | sustained. The assumptions are in the process of being validated. A third | | nitrogen bottle has been placed in backup alignment to maintain the 30 | | minute requirement. | | | | 3 of the 6 Nitrogen Backup Bottles are now valved in instead of 2. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * UPDATE AT 0936 ON 03/03/00 BY PHIL SANTINI TO JOLLIFFE * * * | | | | Additional licensee engineering review has determined that the Nitrogen | | Backup Supply for control of Auxiliary Feedwater Flow Control Valves, | | Turbine Driven Auxiliary Feedwater Pump, and Atmospheric Steam Dump Controls | | does meet the design basis as documented in licensee calculation | | FIX-0030-02. | | | | Thus, the licensee desires to retract this event. | | | | The licensee notified the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R1DO Jim Trapp. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36662 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/05/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 08:42[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/04/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 20:00[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/03/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |TONY VEGEL R3 | | DOCKET: 0707001 |JOE HOLONICH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC WALKER | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CRITICALITY ACCIDENT ALARM SYSTEM HORN FAILED SURVEILLANCE | | | | At 1600 on 02-04-2000 the PSS was informed of the failure of a criticality | | accident alarm system (CAAS) air horn to sound during the performance of | | surveillance testing. The cause of the failure was determined to be debris | | in the air line fouling the flow path for the horn. Subsequently, after | | this horn was repaired and the air horn line blown out, another air horn on | | the same branch line became clogged and would not sound sufficiently. This | | horn was also repaired and its line blown out. The system was retested | | satisfactorily and declared operable at 2245 on 02-04-00. It is possible | | that the system would not have performed its intended safety function if it | | had been required to before it was declared inoperable. | | | | This event is reportable under 10 CFR 76.120(c)(2) as an event in which | | equipment required by the TSR is disabled or fails to function as designed. | | | | The NRC Senior Resident Inspector has been notified of this event. | | | | * * * UPDATE ON 3/3/00 @ 1732 BY WALKER TO GOULD * * * RETRACTION | | | | THIS EVENT HAS BEEN RETRACTED. Subsequent testing of the C-337A CAAS horn | | system with the subject horn valved out, has shown that the CAAS meets the | | requirements for audibility in this area without this horn. Engineering | | Evaluation EV-C-812-00-003 Rev. 0 was completed to document the conclusions | | of this testing. | | | | The NRC Resident inspector was informed. | | | | The Reg 3 RDO(Jordan) and NMSS EO(Sherr) were notified. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36707 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/18/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:03[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/18/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: [EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/03/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |BRUCE JORGENSEN R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | At 1335 hours on 02/17/00 a see and flee emergency was initiated at the | | X-330 building Tails position #1. The see and flee was Initiated as a result | | of a process gas release from the pigtail on Tails position #1. The release | | was large enough to exceed the capacity of portable mini-gulper staged In | | the area. The mini-gulper is used to divert and contain any small releases | | that may occur during pigtail connect/disconnect operations. The release of | | process gas caused a valid actuation of the pyrotronics smokehead safety | | system. The pyrotronics smokeheads and pigtail line isolation safety systems | | operated as designed during this event. | | | | UPDATE AT 1445EST ON 3/300 FROM KURT SISLER TO S.SANDIN * * * | | | | The Regulatee is retracting this report based on the following: | | | | "Nuclear Regulatory Affairs has reviewed the basis for Portsmouth Event | | Report Notification PTS-2000-017, 'X-330 Tails Withdrawal, Pyrotronics | | Smokehead Actuation due to PG Release Exceeding the Capacity of the Gulper', | | and determined that the event should be retracted. (Reference problem report | | PR-PTS-00.-0096S). | | | | "On February 17, 2000 at 1335 hours, an outgassing occurred during the | | connection of an empty cylinder at Tails position 1. The outgassing was | | attributed to pressure inside the evacuation manifold due to a cylinder | | burping operation which had just been completed at Tails position 3. When | | position 3 was burped, the 1-inch diameter evacuation piping and the | | position 1 pigtail, which was valved into the evacuation header, would have | | been exposed to UF6 at above atmospheric pressure. When the burping | | operation was completed, the position 3 evacuation was valved off and UF6 | | withdrawal was restarted. | | | | "The operator proceeded to complete the connection of a new cylinder at | | position 1. The operator, who was wearing appropriate personal protective | | equipment, cracked open and closed the pigtail safety valve per procedure, | | to evacuate the small space between the cylinder safety valve and the | | pigtail safety switch, which plugs the safety valve when it is not connected | | to a cylinder This exposed the space to UF6. As the operator began to | | remove the pigtail safety switch, he observed smoke which was contained by | | the gulper. The operator closed the valve and attempted to tighten fittings. | | When the pigtail safety valve was again cracked open and closed to evacuate | | the line, smoke exceeded the capacity of the gulper to contain the release | | and set off both Pyrotronics smokeheads above position 1. The pigtail safety | | valve was already closed and the Pigtail Line Isolation System closed the | | manifold safety valve at position 1 automatically. The event was initially | | determined to be reportable as a Safety System actuation of the Pigtail Line | | Isolation System in accordance with the Safety Analysis Report Section 6.9, | | Table 6.9-1, J.2. | | | | "The TSR 2.5.3.4 Basis Statement indicates that the purpose of the Pigtail | | Line Isolation System is to minimize a release of liquid UF, due to pigtail | | failure during a withdrawal (Modes II and III). Since the pigtail was | | isolated from the liquid UF, system while the cylinder was being connected, | | Tails Withdrawal position 1 was in preparation mode (Mode I) and the Pigtail | | Line Isolation System safety function was not required. | | | | "The reporting criteria in Table 6.9-1, J.2 states that an actuation is | | reportable for events having the potential for significant impact on the | | health and safety of personnel. Events having the potential for significant | | impact are those events where actual plant conditions existed that the | | system was designed to protect against. Since position 1 was not in a Mode | | for which the safety system was required to be operable, this event has been | | determined to not be reportable to NRC. Accordingly, this was not a valid | | actuation of a safety system. The event notification PTS-2000-017 may be | | retracted." | | | | Operations informed the NRC Resident Inspector and the DOE Site | | Representative. Notified R3DO(Jordan) and NMSS(Cool). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36750 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 03/03/2000| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 10:38[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/03/2000| +------------------------------------------------+EVENT TIME: 09:50[EST]| | NRC NOTIFIED BY: KEVIN SMALL / KEN HILL |LAST UPDATE DATE: 03/03/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |LEN WERT R2 | |10 CFR SECTION: |TAD MARSH NRR | |AAEC 50.72 (a) (1) (I) EMERGENCY DECLARED |FRANK CONGEL IRO | |NOCM COMM ASST BRIEF |KEN CIBOCH FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - UNUSUAL EVENT DECLARED DUE TO LOSS OF OFFSITE POWER TO 4 kV EMERGENCY | | BUSES (REFER TO EVENT #36751 AND EVENT #36752 FOR ADDITIONAL INFORMATION.) - | | | | | | At 0950 on 03/03/00, with Unit 1 in a refueling outage, the licensee | | declared an Unusual Event due to a loss of offsite power to 4 kV emergency | | buses E-1 and E-2 due to a mispositioned switch during relay testing. All | | four emergency diesel generators (two for each unit) started; both Unit 1 | | EDGs are in operation powering buses E-1 and E-2. Shutdown cooling was lost | | but has been restored; spent fuel pool temperature is normal at 83�F. The | | licensee has suspended all fuel movement and is restoring power to systems | | that lost power. Unit 1 is stable. Unit 2, which is at 100% power, is | | unaffected by this event. | | | | The licensee notified the NRC Resident Inspector and state and local | | officials. | | | | * * * UPDATE ON 3/3/00 @ 1226 BY HILL TO GOULD * * * | | | | WHILE ATTEMPTING TO COME OUT OF THE LOSS OF OFF SITE POWER CONDITION, THE | | PLANT HAD AN OVERCURRENT ALARM ON THE D/G-2, AND THEY LOST POWER FROM THE | | NORMAL AND EMERGENCY POWER SOURCES TO THE E-2 BUS AT 1200. THIS IN TURN | | RESULTED IN THE LOSS OF SHUT DOWN COOLING. SHUTDOWN COOLING WAS RESTORED | | AT 1218 WITH MINIMAL TEMPERATURE INCREASE. THEY ALSO HAD THE HALON SYSTEM | | ACTUATION IN THE D/G BASEMENT AREA. THE CAUSE OF THIS MAY HAVE BEEN RELATED | | TO THE GROUND ON THE E-2 BUS. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. THE REG 2 RDO(WERT), NRR EO(HANNON), | | AND IRO(CONGEL) WERE NOTIFIED. | | | | * * * UPDATE ON 3/3/00 @ 1615 * * * COMMISSIONER'S ASSISTANTS BRIEF | | | | MALLETT(BRIEFER), MARSH(NRR EO), REYES(RA), EASLICK(RI), COLLINS(NRR), | | MILLER(IRO), WERT(RDO), WIENS(NRR), BEECHER(PA), LOHAS(SP), FAULKNER(IP), | | SATORIUS(EDO), BATES(SECY), CHAN(CHAIRMAN MESERVES' ASST), OLENCZ(COMM. | | DICUS' ASST), SHARFEY(COMM. MCGAFFIGAN'S ASST), CASTLEMAN(COMM. DIAZ'S | | ASST), AND McCABE(COMM. MERRIFIELD"S ASST). | | | | * * * UPDATE ON 3/3/00 @ 1844 FROM JOLICOEUR TO GOULD * * * | | | | NOUE TERMINATED AT 1840 DUE TO RESTORING POWER FROM NORMAL OFF-SITE SOURCES | | TO THE E-1 AND E-2 BUSSES. | | | | The NRC Resident Inspector was notified. | | | | REG 2 RDO(WERT), NRR EO(HANNON), IRO(CONGEL), AND FEMA(STIENDRUF) WERE | | NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36751 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 03/03/2000| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 13:25[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/03/2000| +------------------------------------------------+EVENT TIME: 09:31[EST]| | NRC NOTIFIED BY: JESTER |LAST UPDATE DATE: 03/03/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LEN WERT R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD ESF ACTUATION DURING THE LOSS OF OFFSITE POWER EVENT. (REFER | | TO EVENT #36750 AND EVENT #36752 FOR ADDITIONAL INFORMATION.) | | | | With Brunswick Unit 1 shutdown for refueling at approximately 09:31 on | | 3/3/00 while performing procedure TM-TTBUS1A (Trip Testing of 230KV Bus 1A) | | a loss of power to the Unit 1 BOP 4160 and emergency busses occurred. This | | caused an automatic start of 4 diesel generators with diesels number 1 and 2 | | loading and restoring power to their respective emergency busses. Unit 1 | | received a group 8 isolation signal that caused a loss of shutdown cooling. | | Core alterations were secured and shutdown cooling was reestablished at | | 09:52. A small rise in reactor coolant temperature occurred (89�F was the | | maximum) and the coolant system did not approach boiling temperatures. Six | | group isolation signals occurred with various valves closing depending on | | initial (pre-event) position. | | | | The following actuations occurred: 4 Diesel generators started, Reactor | | Building HVAC isolated, Standby | | Gas trains started, and an RPS trip occurred (no rod motion occurred due to | | all rods being inserted). | | Systems and components performed as designed based on initial assessment of | | the event. An Unusual Event | | was declared at 09:50 (event #36750) due to a loss of offsite power to the | | emergency busses. | | | | At approximately 12:00 an actuation of the diesel building fire protection | | halon system occurred with an isolation of the control building ventilation | | system. A subsequent loss of emergency bus E2 occurred due to a trip of | | DG#2, which resulted in a second loss of shutdown cooling on Unit 1. Group | | isolations similar to those occurring initially also occurred. Shutdown | | cooling was reestablished at 12:18. The plant is stable and investigation | | into the cause of the DG trip is underway. The plant fire brigade responded | | and found no immediate evidence of a fire. | | | | The NRC Resident Inspector was notified along with state and local | | officials. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36752 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 03/03/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 14:29[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/03/2000| +------------------------------------------------+EVENT TIME: 13:57[EST]| | NRC NOTIFIED BY: HILL |LAST UPDATE DATE: 03/03/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LEN WERT R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |99 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR SHUT DOWN DUE TO ENTERING TS 3.0.3. LCO ACTION STATEMENT. (REFER TO | | EVENT #36750 AND EVENT #36751 FOR ADDITIONAL INFORMATION.) | | | | At 1300 hours, Unit 2 entered Technical Specification 3.0.3 due to the loss | | of diesel generator #2 while two off-site AC circuits were inoperable as | | required by Limiting Condition of Operation 3.8.1, Condition I. The loss of | | AC power and the diesel generator failure were previously reported in ENS | | #36751. At 1357 hours, Unit 2 reactor shutdown commenced from 100% power. | | | | INITIAL SAFETY SIGNIFICANCE EVALUATION: The significance of this occurrence | | is minimal. Sufficient redundant equipment remains operable such that no | | safety functions have been lost. Plant conditions are stable at this time. | | | | CORRECTIVE ACTION(S): Efforts to restore the inoperable equipment are in | | progress. Reference ENS # 36751 | | | | The NRC Resident Inspector was notified. | | | | * * * UPDATE ON 3/3/00 @ 2008 BY BELLER TO GOULD * * * | | | | PLANT EXITED THE 3.0.3 LCO AT 1756 WHEN THE UNIT 1 STARTUP AUX TRANSFORMER | | WAS USED TO POWER THE EMERGENCY BUSSES. THEY ARE STILL IN A 12-HOUR LCO | | ACTION STATEMENT TO RESTORE UNIT 1 UNIT AUXILLARY TRANSFORMER TO SERVICE OR | | BE IN HOT SHUTDOWN IN THE FOLLOWING 12 HOURS. POWER HAD BEEN REDUCED TO | | APPROXIMATELY 60%. | | | | THE NRC RESIDENT WAS INFORMED BY THE LICENSEE. THE NRC OPERATIONS OFFICER | | NOTIFIED THE R2DO (WERT). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36753 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 03/03/2000| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 15:56[EST]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 03/03/2000| +------------------------------------------------+EVENT TIME: 14:17[EST]| | NRC NOTIFIED BY: ROY GREEN |LAST UPDATE DATE: 03/03/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WAYNE LANNING R1 | |10 CFR SECTION: |JIM TRAPP R1 | |ARPS 50.72(b)(2)(ii) RPS ACTUATION |JOHN HANNON NRR | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 28 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM FOLLOWING A LOSS OF FEEDWATER SEAL INJECTION FLOW | | DURING PLANT SHUTDOWN | | | | "WHILE PERFORMING A NORMAL SHUTDOWN, THE REACTOR WAS MANUALLY SCRAMMED AT | | 1417EST DUE TO A LOSS OF SEAL WATER TO THE OPERATING FEEDWATER PUMP AND ITS | | POTENTIAL FAILURE. ALL RODS FULLY INSERTED. SUBSEQUENT TO THE MANUAL | | SCRAM, AN AUTOMATIC SCRAM WAS RECEIVED ON REACTOR WATER LEVEL 3. AN ATTEMPT | | WAS MADE TO MANUALLY INITIATE REACTOR CORE ISOLATION COOLING TO ASSIST WITH | | REACTOR WATER LEVEL CONTROL. THE RCIC SYSTEM FAILED TO INITIATE DUE TO A | | TRIPPED TRIP THROTTLE VALVE. AT 1420EST THE RCIC SYSTEM WAS DECLARED | | INOPERABLE. THE RCIC SYSTEM HAS BEEN RESTORED TO STANDBY. THE OPERATING | | FEEDWATER PUMP CURRENTLY REMAINS IN SERVICE AND SCRAM RECOVERY PROCEDURE AND | | REACTOR COOLDOWN ARE IN PROGRESS." | | | | FOLLOWING THE SCRAM MINIMAL SEAL INJECTION FLOW WAS AVAILABLE TO THE | | OPERATING FEEDWATER PUMP. DECAY HEAT IS CURRENTLY BEING REJECTED TO THE | | MAIN CONDENSER. | | | | THE NRC RESIDENT INSPECTOR WAS INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36754 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 03/03/2000| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 17:34[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 03/03/2000| +------------------------------------------------+EVENT TIME: 11:15[CST]| | NRC NOTIFIED BY: PFEFFER |LAST UPDATE DATE: 03/03/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE JORDAN R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ISOLATION CONTROLS FOR THE TIP GUIDE TUBE ARE NOT DESIGNED/QUALIFIED FOR | | SAFETY RELATED SERVICE. | | | | The Transverse Incore Probe (TIP) guide tube primary containment isolation | | controls are not designed or qualified for safety-related service. This | | could result in a condition outside the Design Basis of the plant because | | multiple failures could cause the undesirable opening of the TIP ball valves | | during a Design Basis Accident. However, the TIP valve and TIP Shear Valve | | Actuation circuits remain operable and continue to be capable of operating | | as containment isolation valves. The TIP Ball Valve power source is through | | the TIP Drive Mechanism. The TIP Ball Valves will be disabled by removing | | the power source from the drive Mechanism when the TIP system is not in use. | | The drive Mechanism power will be restored, under administrative controls, | | when the TIP system is required to be used. | | | | The NRC Resident Inspector will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36755 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 03/03/2000| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 17:42[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/03/2000| +------------------------------------------------+EVENT TIME: 16:30[EST]| | NRC NOTIFIED BY: NANCE |LAST UPDATE DATE: 03/03/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE JORDAN R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE DETERMINED A CONDITION FOUND WHICH COULD HAVE RESULTED IN THE | | PLANT BEING SERIOUSLY DEGRADED. | | | | As a result of an Engineering evaluation of all safety-related large bore | | piping, a number of as-built discrepancies were found with portions of the | | Unit 2 Residual Heat Removal, Safety Injection and Containment Spray piping | | systems. This analysis has concluded that these piping systems deviate from | | the design criteria USAS 831.1-1967, which is the code of record for the | | Cook Nuclear Plant. | | | | As the design and construction of the corresponding systems in Unit 1 are | | similar, this notification is being made for both units despite the fact | | that the Unit 1 review effort has not been completed. | | | | Though informal evaluations have concluded that the piping is unlikely to | | fail in a postulated seismic event, no formal analysis exists to support | | this conclusion. The engineering efforts to evaluate and resolve these | | issues are ongoing. | | | | Both units are currently in no Technical Specification Operating mode with | | both cores unloaded. | | | | The Resident Inspector will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36756 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 03/04/2000| | UNIT: [1] [] [] STATE: AL |NOTIFICATION TIME: 02:37[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 03/04/2000| +------------------------------------------------+EVENT TIME: 00:18[CST]| | NRC NOTIFIED BY: WESS CUMBEE |LAST UPDATE DATE: 03/04/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LEN WERT R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 0 Startup |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNEXPECTED AUTOMATIC AUXILIARY FEEDWATER PUMP START | | | | While passing through Mode 2 in the process of shutting down Unit 1 to enter | | refueling outage #16, the last running feedwater pump was secured without | | defeating the automatic start defeat switch on the balance of plant. This | | resulted in the automatic start of the 'B' motor-driven auxiliary feedwater | | pump. The other auxiliary feedwater pump was already running. | | | | The licensee stated that a procedure step was missed and that an occurrence | | report has been initiated to determine why the procedure step was missed. | | The licensee also stated that all systems functioned as required and that | | there was noting unusual or not understood. The unit is currently in Mode 3 | | (Hot Standby). | | | | The licensee notified the NRC resident inspector who was at the site | | observing the unit shutdown. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36757 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 03/04/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 11:05[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 03/04/2000| +------------------------------------------------+EVENT TIME: 08:45[EST]| | NRC NOTIFIED BY: TERRY BELTZ |LAST UPDATE DATE: 03/04/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JIM TRAPP R1 | |10 CFR SECTION: | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A REACTOR CORE ISOLATION COOLING (RCIC) FLOW CONTROL | | IRREGULARITY DURING THE PERFORMANCE OF SURVEILLANCE TESTING | | | | The following text is a portion of a facsimile received from the licensee: | | | | "A RCIC flow control irregularity was identified during quarterly RCIC | | surveillance testing. Upon reaching the required flow rate of 400 gpm, RCIC | | flow dipped to approximately 360 gpm for 1 - 2 minutes before stabilizing at | | 400 gpm. Engineering is evaluating this condition. In the interim, the | | RCIC system has been declared inoperable. The plant is in a 7-day | | [technical specification limiting condition for operation (LCO)]." | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36758 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 03/06/2000| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 02:39[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 03/05/2000| +------------------------------------------------+EVENT TIME: 22:00[CST]| | NRC NOTIFIED BY: STEVEN JOBE |LAST UPDATE DATE: 03/06/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE TO MEET DRYWELL-TO-SUPPRESSION CHAMBER LEAKAGE TEST ACCEPTANCE | | CRITERIA | | | | The following text is a portion of a facsimile received from the licensee: | | | | "The acceptance criteria specified for the DRYWELL-TO-SUPPRESSION CHAMBER | | LEAKAGE TEST was not met. The as-found value of 0.51 [inches] H2O/Min | | exceeded the operability value of <= 0.2 [inches] H2O/Min. Based on this, | | the operability of the drywell-to-suppression chamber vent pipes, vent | | header down corners, and vacuum breakers cannot be assumed. Primary | | containment was declared inoperable based on a failure to meet the | | requirements of [surveillance requirement (SR)] 3.6.1.1.2, Verify drywell to | | suppression chamber bypass leakage is equivalent to a hole < 1.0 inch in | | diameter." | | | | "[The unit] entered [limiting condition for operation (LCO)] 3.6.1.1, | | Condition A, requiring the restoration of primary containment to an operable | | status within 1 hour. If this required action is not met, Condition B.1 | | requires having the reactor in Mode 3 within 12 hours and B.2 requires | | having the reactor in Mode 4 within 36 hours." | | | | "Currently[, the unit is] in Mode 3 for commencing [a] planned refueling | | outage." | | | | "Engineering evaluation of test results is continuing, and the resident | | inspectors will be kept apprised." | | | | The licensee notified the NRC resident inspectors. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021