Event Notification Report for January 31, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/28/2000 - 01/31/2000 ** EVENT NUMBERS ** 36552 36625 36638 36639 36640 36641 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36552 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 12/30/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 21:45[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 12/30/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 11:30[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 01/28/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |BRUCE BURGESS R3 | | DOCKET: 0707001 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC WALKER | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NOTE: THIS EVENT IS A CONTINUATION OF EVENT #35790. (Refer the event | | #36018 and event #36605 for similar events at Portsmouth.) | | | | At 1130 CST on 12/30/99, the Plant Shift Superintendent (PSS) was notified | | that during walkdowns of the high pressure fire water (HPFW) system in | | C-337, a total of thirteen corroded sprinkler heads were discovered in | | System B-2. The system was declared inoperable, and actions were taken as | | required by the technical safety requirement (TSR). The PSS determined that | | an update to this event report is required. | | | | The NRC resident inspector has been notified of this event by Paducah | | personnel. | | | | * * * UPDATE AT 2233 EST ON 1/12/00 FROM ERIC WALKER TO S. SANDIN * * * | | | | At 0910 CST on 1/12/00 the PSS was notified that during walk downs of the | | HPFW systems in C-337, two adjacent corroded heads were discovered on system | | B-10. Per Engineering Notice C-822-99-047, Rev. 2, the criteria necessary | | for system operability was not being met. The system was declared | | inoperable, and actions were taken as required by the TSR. The PSS | | determined that an update to this event report is required. | | | | It has been determined that this event is reportable under 10CFR76.120(c)(2) | | as an event in which equipment is disabled or fails to function as | | designed. | | | | The NRC resident inspector has been notified of this event by Paducah | | personnel. The NRC operations officer notified the R3DO (Clayton) and NMSS | | EO (Haughney). | | | | *** UPDATE ON 1/21/00 @ 2306 FROM UNDERWOOD TO GOULD *** | | | | At 1100 CST on 1/21/00, the PSS was notified that during walk downs of the | | HPFW systems in C-337, thirteen corroded heads were discovered on system | | D-3. This system was previously inspected on 6/24/99. In addition, at | | 1640 CST on 1/21/00, the PSS was notified that during walk downs of the HPFW | | systems in C-331, three adjacent corroded heads were discovered on system | | 12. This system was previously inspected by Fire Services personnel on | | 4/10/99. Per Engineering Notice C-822-99-047, Rev. 2, the criteria | | necessary for system operability was not being met. The systems were | | declared inoperable and actions were taken as required by the TSR. The PSS | | determined that an update to this event report is required. | | | | The NRC resident inspector has been notified of this event by Paducah | | personnel. The R3DO (Hills) was notified by the NRC operations officer. | | | | * * * UPDATE AT 1549 ON 1/27/00 FROM WHITE TAKEN BY STRANSKY * * * | | | | At 1500 [CST] on 1/26/00, the PSS was notified that during walk downs of the | | HPFW systems in C-337, eight corroded heads were discovered on system D-12. | | This system was previously inspected on 8/28/99. Per Engineering Notice | | C-822-99-047, Rev. 2, the criteria necessary for system operability was not | | being met. The systems were declared inoperable, and actions were taken as | | required by the TSR. The PSS determined that an update to this event report | | is required. | | | | The NRC resident inspector has been notified of this event by Paducah | | personnel. The NRC operations officer notified the R3DO (Phillips). | | | | * * * UPDATE AT 1457 ON 1/28/00 FROM UNDERWOOD TAKEN BY STRANSKY * * * | | | | At 1820 [CST] on 1/27/00, the PSS was notified that during walk downs of the | | HPFW systems in C-333, twenty-nine corroded heads were discovered on system | | B-1. This system was previously inspected on 8/22/99. Per Engineering Notice | | C-822-99-047, Rev. 2, the criteria necessary for system operability was not | | being met. The system was declared inoperable, and actions were taken as | | required by the TSR. The PSS determined that an update to this event report | | is required. | | | | The NRC resident inspector has been notified of this event by Paducah | | personnel. The NRC operations officer notified the R3DO (Phillips). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36625 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 01/26/2000| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 07:42[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 01/26/2000| +------------------------------------------------+EVENT TIME: 06:48[EST]| | NRC NOTIFIED BY: FRANK GORLEY |LAST UPDATE DATE: 01/30/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: |WILLIAM BATEMAN NRR | |ACCS 50.72(b)(1)(iv) ECCS INJECTION |FRANK CONGEL IRO | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 EXPERIENCED AN AUTOMATIC REACTOR SCRAM ON LOW REACTOR VESSEL WATER | | LEVEL DUE TO A FEEDWATER (FW) CONTROL FAILURE. | | | | AT APPROXIMATELY 0648 EST ON 1/26/2000, CONTROL ROOM OPERATORS RESPONDED TO | | A FEEDWATER CONTROL FAILURE ALARM. WHILE INVESTIGATING, FEEDWATER PUMP | | SPEED DECREASED CAUSING REACTOR VESSEL WATER LEVEL (RVWL) TO DROP FROM ITS | | NORMAL OPERATING LEVEL OF 37.5" TO APPROXIMATELY -45". AT 0", AN AUTOMATIC | | REACTOR SCRAM AND GROUP 2 ENGINEERED SAFEGUARDS FEATURES (ESF) ACTUATION | | OCCURRED, AS EXPECTED. ALL CONTROL RODS FULLY INSERTED. AT -38", BOTH THE | | HIGH PRESSURE COOLANT INJECTION (HPCI) AND REACTOR CORE ISOLATION COOLING | | (RCIC) SYSTEM RECEIVED A START SIGNAL. HPCI INJECTED UNTIL THE HPCI PUMP | | TRIPPED AT ITS RVWL SETPOINT OF 51.5". THE FW PUMPS TRIPPED AT 58" WITH | | RVWL SWELL CAUSING LEVEL TO REACH 100". FOLLOWING THE LEVEL TRANSIENT, | | OPERATORS HAD DIFFICULTY IN ESTABLISHING THE LOW-LOW SET RANGE FOR PRESSURE | | CONTROL. NORMALLY, ONE OF THE FOUR SAFETY RELIEF VALVES (SRV) USED FOR | | PRESSURE CONTROL (i.e., THE "H," "A," "G," OR "C" SRV) IS OPENED | | ELECTRICALLY FROM THE CONTROL ROOM WHICH THEN ESTABLISHES THE LOWER PRESSURE | | CONTROL. TEN OF THE ELEVEN SRVs FAILED TO OPEN IN RESPONSE TO CONTROL ROOM | | SWITCH POSITIONING. THE LAST SRV ATTEMPTED (THE "B" SRV) OPENED. UNIT 1 IS | | CURRENTLY STABLE IN HOT SHUTDOWN REJECTING DECAY HEAT TO THE TORUS WITH BOTH | | TRAINS OF SUPPRESSION POOL COOLING IN SERVICE. EFFORTS ARE UNDERWAY TO | | RESTORE THE MAIN CONDENSER AS A HEAT SINK. THE LICENSEE INTENDS TO COOL | | DOWN UNIT 1 TO INVESTIGATE AND RESOLVE THE PROBLEM WITH THE SRVs. THERE IS | | NO INDICATION THAT THE SRV MECHANICAL SAFETY OR AUTOMATIC DEPRESSURIZATION | | SYSTEM FUNCTION IS IMPAIRED AT THIS TIME. DURING THE TRANSIENT, REACTOR | | COOLANT SYSTEM (RCS) TEMPERATURE AND PRESSURE DECREASED FROM THEIR NORMAL AT | | POWER VALUES OF 532�F AND 1035 PSIG TO AN OBSERVED MINIMUM OF 480�F AND 871 | | PSIG. BOTH ARE CURRENTLY AT 510�F AND 977 PSIG. THERE IS NO INDICATION | | THAT THE 100�F/HOUR COOLDOWN RATE WAS EXCEEDED. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | ******************* UPDATE AT 0138 ON 01/30/00 FROM BRUCE BUTLER TO LEIGH | | TROCINE ******************* | | | | The following text is a portion of a facsimile received from the licensee: | | | | "Upon subsequent investigation, the event review team determined that the | | cause of the low level condition that resulted in the Unit 1 reactor scram | | was the inadvertent closure of feedwater valve 1N21-F005B. This valve is | | the inlet valve to the 5th-stage feedwater heater. Closure of the valve | | caused a feedwater flow reduction such that the low level scram setpoint was | | reached. The valve closure was apparently caused by the spurious contact | | closure within the control switch for the valve." | | | | "The plant systems initially appeared to respond automatically as expected | | to this transient condition. Even though the [HPCI] system appeared | | initially to trip at its high level setpoint, subsequent review of its | | operation revealed that it operated longer than expected, and reactor water | | reached a higher level than desired. Operators isolated the main steam | | isolation valves [(MSIV)] in accordance with plant procedures. The HPCI | | system eventually tripped, and reactor water level appeared to stop | | increasing before reaching the main steam lines. A more detailed review of | | the event using the plant's safety parameter display system (SPDS) revealed | | that reactor water level increased to the point that water apparently | | reached the bottom of the main steam lines with some water entering the | | lines." | | | | "Operators proceeded to control reactor pressure using the main [SRV] system | | manually and in the low-low set mode of operation. Normally one (1) of the | | four (4) SRVs used for pressure control is opened manually from the main | | control room, which then initiates automatic pressure control using the SRVs | | in the low-low set mode. An operator attempted to manually open nine (9) of | | the eleven (11) SRVs but did not receive direct indication that any of these | | SRVs opened. When a tenth SRV was opened, the operator received direct | | indication that the SRV opened." | | | | "During subsequent investigation, the event review team has preliminarily | | determined that apparently enough water entered the main steam lines to | | flood the SRVs. With the MSIVs closed, engineers calculated that a total of | | approximately 4,100 gallons of water would be necessary to flood the SRVs. | | The amount of water necessary to flood the SRVs differs with each steam | | line, but it would only require an entry of approximately 860 to 1,060 | | gallons to flood the affected SRVs. A review of the data indicated that the | | flooded SRVs, although flooded, apparently opened upon demand by the | | operator. This is based upon a significant and rapid increase in the | | tailpipe temperature for the SRVs that were given an 'open' signal. Since | | the medium passing through the SRV was two-phase, the tailpipe pressure | | switches that provide positive direct indication that the SRV opened, and | | initiate the low-low set logic, did not actuate on nine of the SRVs. This | | led the operator to believe that those SRVs had not opened. When the | | operator gave the 'B' SRV an 'open' signal, enough of the water had been | | displaced to allow the tailpipe pressure switch to react normally. This | | resulted in the operator seeing direct indication that the 'B' SRV opened | | and actuation of low-low set logic. The operation of the SRVs with a | | two-phase medium was confirmed by an engineer from General Electric with | | extensive experience in SRV design and operation." | | | | "The plant is currently in Cold Shutdown. As a conservative measure all | | eleven SRV topworks and solenoids were removed and replaced. Initially, | | five (5) topworks and four (4) solenoids were sent to Wyle labs. | | Preliminary results of testing performed at Wyle labs indicated [that] these | | five topworks and four solenoids functioned normally. The remainder of the | | solenoids is being checked by Target Rock technicians at the plant. | | Appropriate walkdowns of plant systems are being conducted, and followup is | | occurring for equipment items that require resolution prior to startup." | | | | "Plant management [plans to] review and evaluate the event in its entirety | | and the response of plant systems before granting permission for restart of | | the unit." | | | | The licensee notified the NRC resident inspector. The NRC operation officer | | notified the R2DO (Julian), NRR EO (Matthews), and IRO (Congel.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36638 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 01/28/2000| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 05:14[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 01/28/2000| +------------------------------------------------+EVENT TIME: 02:40[CST]| | NRC NOTIFIED BY: DARYL CLARK |LAST UPDATE DATE: 01/28/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BOTH EMERGENCY DIESEL GENERATORS INOPERABLE DURING CORE ALTERATIONS. | | | | "On 1/28/00 at 0005 hrs, the U-2 Emergency Diesel Generator was found to be | | inoperable due to the diesel generator room vent fan selector switch being | | selected to the alternate feed. The 1/2 Emergency Diesel Generator was | | inoperable due to Division I electrical system refuel outage work. Core | | alterations were in progress. | | | | "Per Tech Spec 3.9.B, one diesel generator must be operable in Mode 5 and | | when handling irradiated fuel in the secondary containment. | | | | "The switch was aligned to the normal position, and vent fan operation was | | verified within approximately 15 minutes to restore the U-2 diesel generator | | to an operable status. An internal investigation is commencing. Although | | both the 1/2 and U-2 EDGs were inoperable, both diesels remained available | | for operation. | | | | "This event is being reported as required by 10CFR50.72(b)(2)(iii)(D), an | | event which alone could have prevented the fulfillment of a safety function | | needed to mitigate the consequences of an accident." | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36639 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 01/28/2000| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 16:25[EST]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 01/28/2000| +------------------------------------------------+EVENT TIME: 13:31[EST]| | NRC NOTIFIED BY: QUENTIN HICKS |LAST UPDATE DATE: 01/28/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN ROGGE R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION DUE TO WILDLIFE KILL | | | | The licensee notified the New York Department of Environmental Conservation | | and the U.S. Fish and Wildlife Service regarding the death of 101 blue | | billed ducks. The ducks were discovered after the circulating water system | | was realigned from reverse flow to normal flow. The NRC resident inspector | | will be informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36640 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 01/29/2000| | UNIT: [1] [] [] STATE: MD |NOTIFICATION TIME: 00:45[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 01/28/2000| +------------------------------------------------+EVENT TIME: 22:00[EST]| | NRC NOTIFIED BY: GETZ |LAST UPDATE DATE: 01/31/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN ROGGE R1 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ECCS VENT SYSTEM FAILED SURVEILLANCE DUE TO PROBLEMS WITH THE CHARCOAL | | FILTERS. | | | | UPON THE COMPLETION OF MAINTENANCE PERFORMED ON THE "11" AND "12" ECCS PUMP | | ROOM VENT FANS, IT WAS DETERMINED THAT THE CHARCOAL FILTERS DID NOT SEAT | | PROPERLY DURING A CHARCOAL TEST (STPM-547-1) RESULTING IN THE TEST CRITERIA | | NOT BEING MET. SEVERAL LOOSE NUTS WERE DISCOVERED ON THE CHARCOAL TRAY | | HOLD-DOWN FASTENERS. THE NUTS WERE TIGHTENED, AND THE SURVEILLANCE WAS | | PERFORMED SATISFACTORILY. THE LICENSEE IS INVESTIGATING WHY THE NUTS WERE | | LOOSE SINCE THE FILTERS WERE NOT INVOLVED IN MAINTENANCE PERFORMED. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED BY THE LICENSEE. | | | | *************** UPDATE AT 0335 ON 01/31/00 FROM LEO GREGORY GETZ TO LEIGH | | TROCINE *************** | | | | The licensee called to change its internal event report number and to | | provide the following updated information. In an effort to check for a | | common mode problem, the licensee checked the Unit 2 charcoal filters on | | 01/29/00. They all tested satisfactorily. | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R1DO (Rogge). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36641 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 01/29/2000| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 17:20[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 01/29/2000| +------------------------------------------------+EVENT TIME: 15:40[EST]| | NRC NOTIFIED BY: ANDY DISMUKE |LAST UPDATE DATE: 01/29/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BLOWN FUSE CAUSES VALVES TO REPOSITION. | | | | A short circuit in a relay coil caused a blown fuse and resulted in the | | following actuations: the main condenser mechanical vacuum pump tripped, | | turbine steam packing exhausters received a trip signal (they were not | | running at the time), partial primary containment isolation system (PCIS) | | Group 2 isolation (outboard valves), and a partial PCIS Group 1 isolation | | (outboard main steam line drain and reactor water sample valves). The | | licensee reported that all actuations were expected for this condition. | | | | The faulty relay has been electrically isolated for repair, and the blown | | fuse was replaced. | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021