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Event Notification Report for January 25, 2000

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           01/24/2000 - 01/25/2000

                              ** EVENT NUMBERS **

36610  36612  36618  36619  36620  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36610       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: POINT BEACH              REGION:  3  |NOTIFICATION DATE: 01/21/2000|
|    UNIT:  [1] [] []                 STATE:  WI |NOTIFICATION TIME: 04:21[EST]|
|   RXTYPE: [1] W-2-LP,[2] W-2-LP                |EVENT DATE:        01/21/2000|
+------------------------------------------------+EVENT TIME:        02:39[CST]|
| NRC NOTIFIED BY:  JOHN SELL                    |LAST UPDATE DATE:  01/24/2000|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |DAVID HILLS          R3      |
|10 CFR SECTION:                                 |                             |
|ASHU 50.72(b)(1)(i)(A)   PLANT S/D REQD BY TS   |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     M/R        Y       40       Power Operation  |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNIT 1 MANUALLY TRIPPED FROM 40% POWER DUE TO A DECREASING FOREBAY LEVEL     |
|                                                                              |
| "UNIT 1 WAS MANUALLY TRIPPED FROM 40% POWER AFTER AN ANTICIPATORY POWER      |
| REDUCTION AT 0239 CST DUE TO DECREASING LEVEL IN THE CIRC. WATER INLET       |
| FOREBAY.  DECREASING LEVEL WAS APPARENTLY DUE TO ICING OF THE INTAKE         |
| STRUCTURE.  UNIT 1 CIRC. WATER SYSTEM HAS BEEN SECURED AND FOREBAY LEVEL HAS |
| INCREASED.  THE UNIT 1 CIRC. WATER SYSTEM WAS SECURED TO MAINTAIN            |
| OPERABILITY OF THE SERVICE WATER SYSTEM.  UNIT 2 REMAINS AT 100% POWER AND   |
| IS STABLE."                                                                  |
|                                                                              |
| FOREBAY LEVEL HAD DECREASED TO -11 FT FROM THE NORMAL OPERATING -8 FT.  THE  |
| -11 FT CORRESPONDS TO THE MINIMUM DESIGN LIMIT FOR THE SERVICE WATER SYSTEM. |
| CURRENTLY, LEVEL IS -6 FT 4 INCHES.  STEAM GENERATORS USING THE ATMOSPHERIC  |
| DUMPS ARE PROVIDING THE HEAT SINK FOR DECAY HEAT REMOVAL SINCE THE CONDENSER |
| IS NOT IN SERVICE.  ALL CONTROL RODS FULLY INSERTED FOLLOWING THE MANUAL     |
| TRIP.                                                                        |
|                                                                              |
| THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR.                         |
|                                                                              |
| * * * UPDATE ON 01/21/00 @ 1339 EST BY KRAUSE TO GOULD * * *                 |
|                                                                              |
| THE LICENSEE UPDATED THIS EVENT BY ALSO CLASSIFYING IT AS A RPS ACTUATION    |
| DUE  TO THE MANUAL REACTOR TRIP.                                             |
|                                                                              |
| THE NRC RESIDENT INSPECTOR WILL BE NOTIFIED.                                 |
|                                                                              |
| THE R3DO (HILLS) WAS NOTIFIED.                                               |
|                                                                              |
| * * * UPDATE ON 01/24/00 @ 1201 EST BY KRAUSE TO JONES * * *                 |
|                                                                              |
| The licensee performed an engineering evaluation that demonstrated that at   |
| no time was the design basis water level for service water exceeded.  The    |
| report of the Tech Spec required shutdown is retracted, but the report of    |
| the RPS activation stands as previously updated.                             |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| The R3DO (Monte Phillips) has been notified.                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36612       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: OYSTER CREEK             REGION:  1  |NOTIFICATION DATE: 01/21/2000|
|    UNIT:  [1] [] []                 STATE:  NJ |NOTIFICATION TIME: 11:17[EST]|
|   RXTYPE: [1] GE-2                             |EVENT DATE:        01/21/2000|
+------------------------------------------------+EVENT TIME:        10:48[EST]|
| NRC NOTIFIED BY:  GLENN HUTTON                 |LAST UPDATE DATE:  01/24/2000|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |FELICIA HINSON       R1      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     M/R        Y       65       Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MANUAL REACTOR SCRAM PER PROCEDURE FOLLOWING TRIP OF ALL RECIRCULATION       |
| PUMPS                                                                        |
|                                                                              |
| During the performance of a surveillance test, with a half scram signal      |
| inserted, a spurious trip signal from the other system initiated a trip of   |
| all the reactor coolant system recirculation pumps.  The operators manually  |
| scrammed the reactor per procedure, all rods fully inserted.  Heat removal   |
| is via the main condenser with main feedwater feeding the reactor.  All      |
| systems functioned as designed and the plant is proceeding to cold shutdown. |
| A trip review will be performed by the licensee.                             |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| * * * UPDATE AT 1943 EST ON 01/24/00 BY FRANK CIGANIK TO FANGIE JONES * * *  |
|                                                                              |
|                                                                              |
| On 01/21/00, the licensee inserted a manual scram in accordance with station |
| procedures in response to a trip of all the reactor recirculation pumps.     |
| The trip of all the pumps was due to an error in the performance of the      |
| ongoing surveillance test.                                                   |
|                                                                              |
| "During the performance of an instrument logic surveillance test on the      |
| isolation condenser actuation logic which also inserts trip signals into the |
| recirculation pump trip logic, the reactor recirculation pumps tripped.      |
| After testing the first instrument, the trip signal associated with the      |
| isolation condensers were reset; however, the recirc pump trip logic was not |
| properly reset before proceeding to the second instrument.  When a test      |
| signal was introduced on this instrument, the reactor recirculation pumps    |
| tripped as designed.  In response to the pump trip, the operators manually   |
| scrammed the reactor.  The plant is currently in cold shutdown.  A trip      |
| review has been performed.  Oyster Creek plans to take advantage of this     |
| shutdown to perform some other maintenance activities."                      |
|                                                                              |
| The original report should have read "half trip" rather than "half scram"    |
| referring to the trip logic of the reactor recirculation pumps; this was     |
| entered wrong the first time.                                                |
|                                                                              |
| The licensee notified the NRC Resident Inspector.  The R1DO (John Rogge) has |
| been notified.                                                               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36618       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: TURKEY POINT             REGION:  2  |NOTIFICATION DATE: 01/24/2000|
|    UNIT:  [] [4] []                 STATE:  FL |NOTIFICATION TIME: 12:50[EST]|
|   RXTYPE: [3] W-3-LP,[4] W-3-LP                |EVENT DATE:        01/24/2000|
+------------------------------------------------+EVENT TIME:        11:42[EST]|
| NRC NOTIFIED BY:  DAVE MORRIS                  |LAST UPDATE DATE:  01/24/2000|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |KERRY LANDIS         R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|4     M/R        Y       95       Power Operation  |0        Hot Standby      |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MANUAL REACTOR TRIP DUE TO FEEDWATER OSCILLATIONS                            |
|                                                                              |
| The licensee had reduced power to 95% to examine the '4A' steam generator    |
| feedwater regulating valve due to feedwater oscillations.  A preliminary     |
| determination of valve internal problems versus control problems was made.   |
| The licensee was ready to continue the down power to shutdown to repair the  |
| feedwater regulating valve, when a manual trip became necessary due to the   |
| feedwater oscillations on '4A' steam generator.                              |
|                                                                              |
| All systems functioned as designed, all rods fully inserted, no secondary    |
| safety valves lifted, and the plant is stable in Mode 3.  Heat removal is    |
| via the atmospheric steam dumps, normal procedure with no tube leaks, and    |
| feedwater is via the standby feedwater system.  The plant will remain shut   |
| down until repairs to the feedwater regulating valve are complete.           |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36619       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MONTICELLO               REGION:  3  |NOTIFICATION DATE: 01/24/2000|
|    UNIT:  [1] [] []                 STATE:  MN |NOTIFICATION TIME: 17:59[EST]|
|   RXTYPE: [1] GE-3                             |EVENT DATE:        01/24/2000|
+------------------------------------------------+EVENT TIME:        15:30[CST]|
| NRC NOTIFIED BY:  STEVE GORTON                 |LAST UPDATE DATE:  01/24/2000|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MONTE PHILLIPS       R3      |
|10 CFR SECTION:                                 |JAMES CREED          IAT     |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| COURTESY NOTIFICATION OF LOCAL AND STATE LAW ENFORCEMENT AGENCIES            |
|                                                                              |
| The licensee notified local and state law enforcement agencies as a courtesy |
| concerning an investigation.  This prompted notification of the NRC under    |
| 10CFR50.72(b)(2)(vi), "Offsite Notification."                                |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| Refer to the HOO log for additional details.                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36620       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUMMER                   REGION:  2  |NOTIFICATION DATE: 01/24/2000|
|    UNIT:  [1] [] []                 STATE:  SC |NOTIFICATION TIME: 22:37[EST]|
|   RXTYPE: [1] W-3-LP                           |EVENT DATE:        01/24/2000|
+------------------------------------------------+EVENT TIME:        22:15[EST]|
| NRC NOTIFIED BY:  HENRY MANOS                  |LAST UPDATE DATE:  01/24/2000|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |KERRY LANDIS         R2      |
|10 CFR SECTION:                                 |                             |
|AENS 50.72(b)(1)(v)      ENS INOPERABLE         |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MORE THAN 25% OF THE OFFSITE WARNING SIRENS LOST DUE TO ICE STORMS           |
|                                                                              |
| The licensee reported the loss of more than 25% of the offsite warning       |
| sirens due to ice storms passing through the local area.  The licensee will  |
| be contacting the power suppliers of the sirens to take action to recover    |
| them.                                                                        |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+


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