Event Notification Report for January 20, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/19/2000 - 01/20/2000 ** EVENT NUMBERS ** 36596 36601 36604 36605 36606 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36596 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 01/17/2000| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 06:32[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 01/17/2000| +------------------------------------------------+EVENT TIME: 05:38[EST]| | NRC NOTIFIED BY: MIKE DAVID |LAST UPDATE DATE: 01/19/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GLENN MEYER R1 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY REPORT. FITNESS-FOR-DUTY QUESTIONED DUE TO INATTENTIVENESS. | | IMMEDIATE COMPENSATORY MEASURES TAKEN UPON DISCOVERY. CONTACT THE NRC | | OPERATIONS CENTER FOR ADDITIONAL DETAILS. | | | | * * * UPDATE 1140EST ON 1/19/00 FROM MATTHEW ARSENAULT TO S.SANDIN * * * | | | | THIS REPORT IS BEING RETRACTED BASED ON THE FOLLOWING: | | | | "On January 17, 2000, at 6:32 EST, North Atlantic Energy Service Corporation | | (North Atlantic) submitted a 1-hour report to the Nuclear Regulatory | | Commission pursuant to 10 CFR 73.71 regarding a Security Officer that was | | discovered to be inattentive to duty (NRC Event Report 36596). | | | | "Subsequent to the report and after a thorough review, it was determined | | that this incident was loggable and did not meet the criteria for a 1-hour | | report. Specifically, this condition did not constitute an uncompensated | | loss as defined in Regulatory Guide 5.62 because the original capability was | | restored within 10 minutes of discovery of the event. Additionally, | | consistent with the guidance provided in Generic Letter 91-03, events | | involving inattentive security personnel can be logged if they are properly | | compensated for in accordance with Regulatory Guide 5.62 and NUREG-1304. | | Therefore, North Atlantic retracts the 1-hour report. This event has been | | captured in the event log." | | | | The licensee will inform the NRC resident inspector. Notified R1DO | | (Hinson). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36601 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 01/18/2000| | UNIT: [1] [2] [3] STATE: AZ |NOTIFICATION TIME: 11:41[EST]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 01/18/2000| +------------------------------------------------+EVENT TIME: 09:25[MST]| | NRC NOTIFIED BY: DAN MARKS |LAST UPDATE DATE: 01/19/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA SMITH R4 | |10 CFR SECTION: | | |AENS 50.72(b)(1)(v) ENS INOPERABLE | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF COMMERCIAL TELEPHONE SERVICE | | | | The licensee reported that all U.S. West commercial telephone service to the | | site (including the ENS) has been lost due to a problem offsite. The | | licensee is attempting to contact U.S. West to determine the cause of the | | problem and estimate time to restore. | | | | The NRC resident inspector will be informed of this event by the licensee. | | | | ******************** UPDATE AT 1916 ON 01/18/00 FROM DAN MARKS TO LEIGH | | TROCINE ******************** | | | | The following text is a portion of a facsimile received from the licensee: | | | | "The following event description is based on information currently | | available. If through subsequent reviews of this event, additional | | information is identified that is pertinent to this event or alters the | | information being provided at this time, a followup notification will be | | made via the ENS or under the reporting requirements of 10 CFR 50.73." | | | | "NOTE: THIS ENS WORKSHEET IS A FOLLOW-UP TO ENS ID 36601, PERFORMED AT 09:41 | | MST. SINCE U.S. WEST LINES WERE AFFECTED, THE INITIAL CALL WAS MADE VIA A | | CELLULAR TELEPHONE." | | | | "On January 18, 2000, at approximately 0925 MST, Palo Verde Units 1, 2, and | | 3 determined that the ENS telephones were inoperable. This was related to | | the offsite damage to a 200-pair telecommunications cable affecting Palo | | Verde. The initial call was placed from the Nuclear Regulatory Affairs | | Director's cellular telephone, and that phone number was also provided to | | the [headquarters operations officer] if followup was necessary prior to | | restoration of the ENS." | | | | "The current prognosis for full restoration of the ENS is approximately 2400 | | MST. If the Palo Verde Units 1, 2, or 3 cannot be reached via the ENS, | | [commercial] ... phone numbers are available. [Call the NRC operations | | officer for site contact numbers.] ..." | | | | "Emergency Plan notification system backups for communication with State and | | County agencies were confirmed to remain operable; therefore, this | | notification was only for the loss of ENS and did not reflect a loss of | | emergency assessment or notification capability." | | | | "There is no corresponding 10 CFR 50.73 reporting requirement. Palo Verde | | does not expect to followup this report with a Licensee Event Report | | (LER)." | | | | "Palo Verde [plans to] complete a followup notification when full capability | | is restored." | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R4DO (Smith). | | | | * * * UPDATE 0006EST ON 1/19/2000 FROM BRAD ROBINSON TO S.SANDIN * * * | | | | The ENS phones have been restored to complete functionality at 2206MST. The | | licensee notified the NRC resident inspector. Notified R4DO(Smith). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36604 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 01/19/2000| | UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 15:46[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 01/19/2000| +------------------------------------------------+EVENT TIME: 14:24[CST]| | NRC NOTIFIED BY: DON CERNY |LAST UPDATE DATE: 01/19/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA SMITH R4 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT UNIT SPECIFIC LOADS WERE ON COMMON BUSES | | | | The following text is a portion of a facsimile received from the licensee: | | | | "FSAR section 1A(B) for compliance to Reg Guide 1.81 states that [the | | Comanche Peak] design complies with the provisions of Revision 1 of this Reg | | Guide. Contrary to the above, unit specific [118-volt AC] loads fed from | | common buses XEC1-1 and XEC2-1 were shared between two units." | | | | The licensee stated that affected loads involve a lot of different equipment | | and systems but did not specify which equipment or systems. The licensee | | also stated that the units are not currently in any technical specification | | limiting conditions for operation as a result of this issue because the | | loads are now aligned to an alternate power supply. Corrective actions have | | not yet been determined. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36605 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 01/19/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 17:59[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 01/19/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 09:00[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 01/19/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |DAVID HILLS R3 | | DOCKET: 0707002 |WAYNE HODGES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DALE NOEL | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF HIGH PRESSURE FIRE WATER SPRINKLER SYSTEMS TO MEET SYSTEM | | OPERABILITY REQUIREMENTS (24-Hour Report) - (Refer the event #36018 for a | | similar event at Portsmouth and refer to event #35790 and event #36552 for | | related events at Paducah.) | | | | The following text is a portion of a facsimile received from Portsmouth: | | | | "On 01/19/00 at approximately 0900 hours during the scheduled semi-annual | | walkdown of the X-330 Process Building high pressure fire water (HPFW) | | systems, the Plant Shift Superintendent (PSS) was notified that sprinkler | | systems #284 and #365 were not capable of meeting system operability | | requirements due to corrosion problems identified on adjacent sprinkler | | heads." | | | | "Two adjacent heads on system #284 and three adjacent heads on system #365 | | were identified with corrosion around the valve seat. This condition | | prevents the heads from being able to actuate at normal water pressure. | | When two adjacent heads are inoperable, the system is considered unable to | | perform its design function. The PSS declared the affected sprinkler | | systems inoperable, and [technical safety requirement (TSR)] required | | actions were initiated and completed." | | | | "Further inspections of the Process Building sprinkler systems are planned. | | This report will be updated if additional sprinkler systems are determined | | to be inoperable." | | | | "There was no loss of hazardous/radioactive material or | | radioactive/radiological contamination exposure as a result of this event." | | | | At the time of this event notification, Portsmouth personnel had completed | | repairs and were in the process of closing out the paperwork to be able to | | declare the systems operable again. | | | | Portsmouth personnel notified the NRC resident inspector and a Department of | | Energy site representative. | | | | (Call the NRC operations officer for a site contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36606 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 01/19/2000| | UNIT: [1] [2] [] STATE: IL |NOTIFICATION TIME: 21:59[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 01/19/2000| +------------------------------------------------+EVENT TIME: 14:55[CST]| | NRC NOTIFIED BY: CAROL KRONICK |LAST UPDATE DATE: 01/19/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 85 Power Operation |85 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A LOOSE STEM NUT AND THE INABILITY TO MANUALLY OPERATE A SAFE | | SHUTDOWN MAKEUP PUMP (SSMP) INJECTION VALVE FOLLOWED BY DISCOVERY THAT THE | | VALVE WAS NOT FULLY CLOSED | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On January 19, 2000, at 1357 [CST], the MO 2-2901-8 [valve] (SSMP injection | | to Unit 2) was taken [out of service] for planned maintenance on the valve | | position limit switches. At 1455 [CST], the Maintenance Supervisor notified | | the control room that the stem nut was found loose and [that] the valve | | could not be manually operated. For Unit 2, a 14-day technical | | specification [(TS) limiting condition for operation (LCO)] was entered per | | TS 3.8.J, and a 14-day LCO for administrative technical requirements (ATR) | | was entered. At 1605 [CST,] it was determined that the valve was not fully | | closed, and the SSMP system [was] declared inoperable to Unit 1. [As a | | result, a] 14-day LCO for [TSs] and a 14-day ATR [were] entered for Unit 1. | | A plan is being developed to repair/correct the MO 2-2901-8 [valve]." | | | | "It was determined at 2040 [CST] that this event is reportable ... ." | | | | The licensee stated that both the pump and the valve have quarterly | | surveillances and that the surveillances were up to date. | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021