Event Notification Report for December 15, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/14/1999 - 12/15/1999 ** EVENT NUMBERS ** 36506 36507 36508 36509 36510 36511 36512 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36506 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 12/14/1999| | UNIT: [1] [2] [] STATE: IL |NOTIFICATION TIME: 00:27[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 12/13/1999| +------------------------------------------------+EVENT TIME: 20:45[CST]| | NRC NOTIFIED BY: DAVE BOWMAN |LAST UPDATE DATE: 12/14/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SHEAR R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY SYSTEM FAILURE: THE BREAKER FOR THE "B" TRAIN REFRIGERATION CONTROL | | UNIT (RCU) TRIPPED. | | | | The licensee started the "B" control room HVAC to support routine | | maintenance on "A" train. The "B" train would not operate properly on | | non-safety-related cooling (station service water). Safety-related cooling | | (RHR service water ) was started to provide cooling to the "B" train, which | | operated properly on safety-related cooling. After the control room had | | cooled down, the "B" train was shut down and then restarted with | | non-safety-related cooling, after which it operated properly. During | | subsequent swap to the "A" train, the breaker for the "B" train RCU tripped. | | This is a safety system functional failure. The licensee entered Technical | | Specification 3.8.D.1.b for RCU inoperable, which is a 30-day limiting | | condition of operation. Troubleshooting of the problem is in progress. | | This is part of the control room emergency ventilation system. | | | | The NRC resident inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36507 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 12/14/1999| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 07:21[EST]| | RXTYPE: [1] W-3-LP |EVENT DATE: 12/14/1999| +------------------------------------------------+EVENT TIME: 03:55[EST]| | NRC NOTIFIED BY: M GRIFFIN |LAST UPDATE DATE: 12/14/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO LOSS OF CONDENSATE PUMP | | | | The plant was initially at 100% power. At 0354 EST, a ground fault occurred | | on the "A" condensate pump resulting in a loss of the "A" condensate pump. | | This caused a subsequent trip of the "A" condensate booster pump and "A" | | main feedwater (MFW) pump. The plant automatically ran back to | | approximately 60% power. Steam generator (SG) levels lowered and approached | | the automatic trip setpoint so the reactor was manually tripped from | | approximately 60% at 0355 EST. All rods fully inserted into the core. The | | auxiliary feedwater (AFW) pumps were manually started to aid SG level | | control; however, an automatic AFW initiation signal was properly received. | | All ESF components actuated as required. There were no safety problems | | encountered after the trip. The plant is stable in Hot Shutdown with main | | feedwater in service. No power-operated relief valves opened. | | | | The NRC resident inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36508 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 12/14/1999| | UNIT: [] [2] [3] STATE: AL |NOTIFICATION TIME: 10:05[EST]| | RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 12/13/1999| +------------------------------------------------+EVENT TIME: 14:25[CST]| | NRC NOTIFIED BY: R. SANFIELD |LAST UPDATE DATE: 12/14/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A RANDOM DRUG TEST WAS PERFORMED ON A CONTRACT FOREMAN, AND NITRATES WERE | | FOUND IN HIS SAMPLE WHICH INDICATED THAT THE SAMPLE HAD BEEN ADULTERATED. | | THE CONTRACT FOREMAN'S ACCESS AND BADGE WERE PULLED ON CONFIRMATION. HE WAS | | ESCORTED OFFSITE, AND HIS WORK IS BEING REVIEWED. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED OF THIS EVENT BY THE LICENSEE. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36509 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TN DIVISION OF RADIOLOGICAL HEALTH |NOTIFICATION DATE: 12/14/1999| |LICENSEE: AMERICAN ECOLOGY RECYCLE CENTER |NOTIFICATION TIME: 12:18[EST]| | CITY: OAK RIDGE REGION: 2 |EVENT DATE: 12/09/1999| | COUNTY: STATE: TN |EVENT TIME: 13:15[EST]| |LICENSE#: R-01037 AGREEMENT: Y |LAST UPDATE DATE: 12/14/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANN BOLAND R2 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DEBRA SHULTS | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FIRE IN SLUDGE DRYER | | | | "The licensee reported a fire (no flames) in their sludge dryer. | | Technicians noticed a glow in the dryer. The building was evacuated | | immediately. The gas line, which provide heat to the dryer, was cut off, | | and the smoke began to subside. Water was piped into the sludge dryer to | | squelch the remaining embers. A stop-work order was placed on the dryer | | after it was secured. The air filtration system was shut down in order to | | change the pre-filters. The contamination was localized to the sooty | | deposits that appeared to be within a few feet of the sludge dryer. There | | was no spread of contamination beyond that area. Work place air samplers | | operated continuously during the event. Results have not been released at | | this time. Employees who were in the area during the event received whole | | body counts. Results were negative. The fire department was not called." | | | | (Call the NRC operations officer for a contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 36510 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MERITER HOSPITAL |NOTIFICATION DATE: 12/14/1999| |LICENSEE: MERITER HOSPITAL |NOTIFICATION TIME: 12:50[EST]| | CITY: MADISON REGION: 3 |EVENT DATE: 12/14/1999| | COUNTY: STATE: WI |EVENT TIME: 10:25[CST]| |LICENSE#: 480039502 AGREEMENT: N |LAST UPDATE DATE: 12/14/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GARY SHEAR R3 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES YANG | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE MEDICAL MISADMINISTRATION | | | | During insertion of iodine-125 (I-125) seeds in a prostate treatment, one of | | the needles broke during seed planting and remains in the patient about 3 | | centimeters outside the prostate gland. The needle retained four of the | | seeds, each containing 0.326 mCi of I-125. The needle has been left in | | place, as that has been determined to be in the best interest of the patient | | at this time. The attending physician was present and the patient informed. | | There will be little impact on the treatment of the prostrate. The licensee | | is evaluating whether any adverse effect to the patient is expected of this | | possible misadministration, the seeds located outside the treatment site. | | The hospital contacted NRC Region 3 inspector (James Cameron). | | | | (Call the NRC operations officer for a contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 36511 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: H. C. NUTTING CO. |NOTIFICATION DATE: 12/14/1999| |LICENSEE: H. C. NUTTING CO. |NOTIFICATION TIME: 13:08[EST]| | CITY: CINCINATTI REGION: 3 |EVENT DATE: 12/14/1999| | COUNTY: STATE: OH |EVENT TIME: 09:50[EST]| |LICENSE#: 34-18882-01 AGREEMENT: Y |LAST UPDATE DATE: 12/14/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GARY SHEAR R3 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HAROLD WIDNER | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STOLEN TROXLER MOISTURE DENSITY GAUGE | | | | The licensee reported a Troxler moisture density gauge (model 3430, serial | | number 28862) stolen some time last night after 2110 CST from the cargo area | | of a locked Nissan Pathfinder. The gauge was in a locked box in the vehicle | | at the technician's home in Cincinnati. The gauge sources contain 8 mCi of | | Cs-137 and 40 mCi of Am/Be-241. The City of Cincinnati Police responded and | | are investigating the theft (no report number at this time). The licensee | | notified the Ohio Bureau of Radiation Safety, part of the Department of | | Health as part of their license requirement. | | | | (Call the NRC operations officer for a contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36512 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ITT INDUSTRIES |NOTIFICATION DATE: 12/14/1999| |LICENSEE: ITT INDUSTRIES |NOTIFICATION TIME: 17:10[EST]| | CITY: LANCASTOR REGION: 1 |EVENT DATE: 12/14/1999| | COUNTY: STATE: PA |EVENT TIME: [EST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 12/14/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |HAROLD GRAY R1 | | |ANN BOLAND R2 | +------------------------------------------------+GARY SHEAR R3 | | NRC NOTIFIED BY: RICHARD RANSALL |PHIL HARRELL R4 | | HQ OPS OFFICER: FANGIE JONES |VERN HODGE (Fax) NRR | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 10-CFR-PART-21 REPORT ON 3-INCH DIAPHRAGM VALVES WITH 3250L ACTUATORS | | | | "Recently, Engineered Valves was asked by a customer to perform tests and | | analysis documenting the maximum shutoff pressure for a diaphragm valve | | configuration. Based on testing and engineering calculations performed in | | November and December of 1999, Engineered Valves has discovered that 3" | | diaphragm valves with 3250L actuators, supplied to the nuclear power | | industry, may not be capable of bubble tight shutoff at customer specified | | operating conditions. | | | | "These valves were supplied to the nuclear power industry for design | | pressures up to 200 psig and were factory tested at or above specified | | shutoff pressure depending on design specification or ASME Section III | | requirements. The testing and analysis described above indicate that there | | is a statistical possibility, depending on the tolerances of each valve and | | actuator component, that a valve can be built which will shut off bubble | | tight at no more than 147 psig. Therefore, it is possible that a valve, | | which has been maintained or repaired with new components or subassemblies | | might not have sufficient actuator thrust to shut off against the specified | | pressure." | | | | Purchasers and sites include the following: | | Westinghouse Electric Corporation at multiple locations | | TVA at Bellefonte | | Louisiana Power and Light at Waterford | | Toledo Edison at Davis Besse | | Iowa Electric at Duane Arnold | | Pacific Gas and Electric at Diablo Canyon | | Consolidated Edison at Indian Point | | Virginia Electric and Power Company at Surry | | Florida Power and Light at Turkey Point and St. Lucie | | Duke Energy Corp. at Oconee | | | | Due to organizational and name changes, include the following names as | | possible organizations over the past 31 years: ITT Corporation, ITT | | Grinnell Corporation, ITT Grinnell Valve Division, ITT Dia Flo, ITT | | Specialty Valve Group, ITT Fluid Products Corporation, ITT Fluid Technology | | Corporation, ITT Engineered Valves, and ITT Industries. | | | | Engineered Valves is now finalizing the list of affected purchasers and will | | notify them by Monday, 12/20/99. | | | | (Call the NRC operations officer for ITT Engineered Valves contact | | information.) | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021