Event Notification Report for December 3, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/02/1999 - 12/03/1999 ** EVENT NUMBERS ** 36421 36478 36479 36480 36481 36482 36483 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36421 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 11/10/1999| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 19:09[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 11/10/1999| +------------------------------------------------+EVENT TIME: 18:15[EST]| | NRC NOTIFIED BY: DAN HARDIN |LAST UPDATE DATE: 12/02/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES OGLE R2 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY REPORT | | | | UNESCORTED ACCESS GRANTED INAPPROPRIATELY. IMMEDIATE CORRECTIVE ACTIONS | | TAKEN UPON DISCOVERY. THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. | | SEE THE HOO LOG FOR ADDITIONAL DETAILS. | | | | * * * RETRACTED AT 1655 EST ON 12/2/1999 BY CHARLES ELBERFELT TO FANGIE | | JONES * * * | | | | Upon further investigation a determination was made that access was not | | granted inappropriately, thus the licensee is retracting this event. The | | licensee informed the NRC Resident Inspector and the NRC Headquarters | | Operations Officer informed the R2DO (Kenneth Barr). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36478 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA DEPARTMENT OF HEALTH |NOTIFICATION DATE: 12/01/1999| |LICENSEE: PROFESSIONAL ENGINEERING & INSPECTION|NOTIFICATION TIME: 12:50[EST]| | CITY: JUPITER REGION: 2 |EVENT DATE: 12/01/1999| | COUNTY: MARTIN STATE: FL |EVENT TIME: [EST]| |LICENSE#: 2940-1 AGREEMENT: Y |LAST UPDATE DATE: 12/02/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |KENNETH BARR R2 | | |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHARLES ADAMS (fax) | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - LOST TROXLER GAUGE | | | | A Troxler Model # 3411B moisture/density gauge (serial no. 13472) was lost | | from the back of a pickup truck. The gauge contains one 8 mCi Cs-137 source | | and one 40 mCi Am-241/Be source. The following narrative was submitted via | | facsimile: | | | | "The gauge was in the back of a pickup proceeding down Highway A1A. The | | tailgate came open and the bed liner and gauge fell out of the vehicle. A | | county employee working nearby witnessed the incident. He saw a vehicle stop | | and pick up the bed liner and another vehicle stop and pick up the gauge. | | The Martin County Sheriff's office is working the case. Martin County | | Emergency Management and the owner are issuing a joint press release. | | Florida Bureau of Radiation Control is also investigating the incident." | | | | * * * UPDATE ON 12/02/99 AT 0808ET BY JERRY EAKINS TAKEN BY MACKINNON * * * | | | | Jerry Eakins of the Florida Bureau of Radiation Control reported that the | | Troxler gauge was recovered by the Licensee this morning at 0700ET. The | | Troxler gauge is not damaged and the licensee will perform a leak test of | | the gauge. The State of Florida case number for this event is Fl 99-0162. | | | | | | NRC R2DO (Ken Barr) and NMSS EO (Scott Moore) notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36479 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ABB POWER T&D COMPANY |NOTIFICATION DATE: 12/02/1999| |LICENSEE: ABB POWER T&D COMPANY |NOTIFICATION TIME: 10:33[EST]| | CITY: Florence REGION: 2 |EVENT DATE: 12/02/1999| | COUNTY: STATE: SC |EVENT TIME: 10:33[EST]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 12/02/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |KENNETH BARR R2 | | |STEVEN DENNIS R1 | +------------------------------------------------+GEOFFREY WRIGHT R3 | | NRC NOTIFIED BY: H. SCOTT BRIDGES |PHIL HARRELL R4 | | HQ OPS OFFICER: JOHN MacKINNON |VERN HODGE NRR | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TRIP ROLLER - HK CIRCUIT BREAKER, ABB PART # 180097A00 | | | | During the 4kV ABB Type HK breaker refurbishment at the DC Cook Plant on | | October 21, 1999, newly installed trip rollers, ABB Part Number 180097A00, | | were determined to be below the minimum hardness specification, Rockwell C | | 50-55. One roller was observed to be "scoring" after 200 cycles. This | | roller was one of 130 rollers sent to DC Cook through a purchase order from | | ABB Service Company in Cleveland, Ohio. A sample of rollers indicated that | | all were below the hardness specification. After communicating this to ABB | | Service and the ABB Florence facility, the roller with the lowest measured | | hardness, Rockwell C13, was returned for evaluation at the ABB-Florence | | factory. | | | | ABB Power T&D Company received notification from ABB Service Company, The | | Woodlands, TX, of a trip roller, 180097A00, problem occurring in November | | 11, 1998, purchased under ABB Service Company Purchase Order Number | | 27-04459-P4031, ABB Power T&D Company Order Number CCN0449. The initial | | investigation points to a roller that has not been heat-treated to its | | hardness specification as well. This information will serve to address the | | trip roller issue here as well. | | | | An HK Circuit Breaker that contains trip rollers that are not properly | | hardened may fail to trip at some point during the life of the breaker. ABB | | Power T&D Company testing indicates that a very soft trip roller measuring | | Rockwell C13 was able to operate 4000 operations before minimum trip voltage | | failed to operate the circuit breaker. | | | | The information of the defect of the trip roller was obtained on October 21, | | 1999 | | | | This information affects trip rollers that were shipped as Component Orders | | or as part of Complete Circuit Breakers from October 30, 1995 through June | | 1999. | | | | The hardness critical characteristic was added to the QC Record Card in June | | 1999 for the trip roller, 180097A00. | | | | ABB will notify all customers who purchased this product. | | | | Replacement trip rollers may be obtained from ABB Power T&D Company, | | Sanford, FL, by contacting the Components Group. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Research Reactor |Event Number: 36480 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: UNIV OF TEXAS |NOTIFICATION DATE: 12/02/1999| | RXTYPE: 1100 KW TRIGA MARK II |NOTIFICATION TIME: 17:26[EST]| | COMMENTS: |EVENT DATE: 12/01/1999| | |EVENT TIME: 10:00[CST]| | |LAST UPDATE DATE: 12/02/1999| | CITY: AUSTIN REGION: 4 +-----------------------------+ | COUNTY: TRAVIS STATE: TX |PERSON ORGANIZATION | |LICENSE#: R-129 AGREEMENT: Y |PHIL HARRELL R4 | | DOCKET: 05000602 |WILLIAM BECKNER NRR | +------------------------------------------------+CHARLES MILLER IRO | | NRC NOTIFIED BY: SEAN O'KELLY |ALEXANDER ADAMS NRR | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECHNICAL SPECIFICATION VIOLATION DISCOVERED | | | | The licensee has determined that Tech Spec 3.4.2, which limits the amount of | | explosive material in the reactor to less than 25 milligrams has been | | exceeded. Following an investigation of bulging of the reactor reflector in | | October this year it has been determined that an accumulation of hydrogen | | and oxygen gas of approximately 5000 times the Tech Spec limit has | | accumulated in the reflector. The reflector is graphite, contained an | | aluminum can, doughnut shaped, that fits around the reactor. Apparently, a | | pinhole sized leak allowed water from the reactor pool to seep into the | | reflector can, which then underwent radiolytic decomposition filling the can | | with hydrogen and oxygen gas. The reflector has been ultrasonically | | examined to determine if it was full of water and it is not. | | | | The licensee has and is consulting experts concerning their plan to vent the | | gasses out of the reflector under water in a slow and controlled manner. | | The reactor is defueled and will remain so until this problem is corrected. | | | | The licensee notified the NRC Project Manager concerning this issue. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36481 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 12/02/1999| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 17:47[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 12/02/1999| +------------------------------------------------+EVENT TIME: 16:05[CST]| | NRC NOTIFIED BY: RICK HUBBARD |LAST UPDATE DATE: 12/02/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PHIL HARRELL R4 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTAINMENT SUMP LEVEL DETECTION DOES NOT MEET REQUIREMENT FOR RCS LEAK | | DETECTION | | | | "While investigating concerns with the containment instrument tunnel sump | | leak detection capabilities and satisfying the requirements for RCS leak | | detection in the Improved Tech Specs (TS 3.4.15) an issue was identified | | with the Normal Containment Sump Level Monitoring capability. From review | | and investigation of this issue, it was identified that the current | | calculation for the instrument tunnel sump leak rate would not always be | | able to detect a 1 gpm leak in one hour to satisfy the Reg Guide 1.45 basis | | for this Tech Spec. After even further review, it has been concluded that | | the current calculation for the containment normal sumps is performed in a | | similar manner. Thus, the containment normal sumps will not always provide | | adequate leak detection to ensure that a 1 gpm RCS leak is detected in one | | hour. | | | | "The Wolf Creek Updated FSAR states that one of the design bases of the | | reactor coolant system leakage detection systems is to be capable of | | detecting a 1 gallon per minute leak consistent with Regulatory Guide 1.45 | | and 10 CFR 50, Appendix A, General Design Criteria 30. Regulatory Guide 1.45 | | states that the systems must be capable of detecting a 1 gpm leak within 1 | | hour. Since the Wolf Creek Containment Normal sump does not meet this design | | basis, it is believed that the plant may be outside its design basis, in | | accordance with the reporting criteria of 10 CFR 50.72(b)(1)(ii)." | | | | The fix is a software change to the Plant Computer and the licensee has it | | and intends to have it in operation well within the 30 day shutdown | | requirement of Tech Specs. | | | | The licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36482 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 12/02/1999| | UNIT: [] [2] [] STATE: VA |NOTIFICATION TIME: 18:11[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 12/02/1999| +------------------------------------------------+EVENT TIME: 16:47[EST]| | NRC NOTIFIED BY: JEFF MOSHER |LAST UPDATE DATE: 12/02/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KENNETH BARR R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 95 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP AFTER MAIN FEEDWATER PUMP TRIP ON LOW SUCTION PRESSURE | | | | The reactor was manually tripped (all rods fully inserted) after two of | | three main feedwater pumps tripped due to low suction pressure. The low | | suction pressure was due to a secondary system transient which caused the | | loss of one of the high pressure heater drain pumps. The transient was from | | feedwater heater level system. The exact cause is under investigation. | | | | All auxiliary feedwater pumps started, as designed, on low steam generator | | level and the steam dumps opened to the condenser to remove excess heat. | | The unit is stabilized in Mode 3. | | | | The licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36483 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 12/03/1999| | UNIT: [2] [3] [] STATE: PA |NOTIFICATION TIME: 00:09[EST]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 12/02/1999| +------------------------------------------------+EVENT TIME: 22:25[EST]| | NRC NOTIFIED BY: BREIDENBAUGH |LAST UPDATE DATE: 12/03/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |STEVEN DENNIS R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PERFORMANCE OF RHR LOGIC FUNCTIONAL TEST DEFEATS THE AUTOMATIC START OF ALL | | FOUR RHR PUMPS | | | | A review of the Residual Heat Removal (RHR) logic system functional test | | identified that during part of the performance of the test the automatic | | start of all four RHR pumps was defeated. Manual initiation remained | | available. This test was last performed on both Unit 2 and Unit 3 in 1997. | | This report is being made due to the loss of the automatic initiation of the | | Low Pressure Coolant Injection (LPCI) mode of RHR. This alone could have | | prevented the fulfillment of a safety function. | | | | The NRC Resident Inspector will be notified of this event by the Licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021