The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for November 12, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           11/10/1999 - 11/12/1999

                              ** EVENT NUMBERS **

36331  36336  36338  36418  36419  36420  36421  36422  36423  36424  36425  36426 
36427  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36331       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FT CALHOUN               REGION:  4  |NOTIFICATION DATE: 10/22/1999|
|    UNIT:  [1] [] []                 STATE:  NE |NOTIFICATION TIME: 13:04[EDT]|
|   RXTYPE: [1] CE                               |EVENT DATE:        10/22/1999|
+------------------------------------------------+EVENT TIME:        09:22[CDT]|
| NRC NOTIFIED BY:  ERICK MATZKE                 |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA SMITH          R4      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - Steam Generator #RC-2A in Tech Spec Category C-3; Steam Generator          |
| inspections continuing -                                                     |
|                                                                              |
| At 0922 CDT on 10/22/99, during eddy current testing of the steam generators |
| (SG), it has been determined that 50 tubes in SG #RC-2A require plugging.    |
| This places SG #RC-2A in Technical Specification category C-3 per 3.17(2).   |
| Forty-four tubes have been determined to require plugging in SG #RC-2B at    |
| this time.  Eddy current testing is continuing on the SGs.  A 100% full      |
| length bobbin coil inspection program has been completed in both SGs.  A     |
| rotating pancake coil probe (Plus Point) is being used to inspect 100% of    |
| the top of the hot leg tube sheets for both SGs.  One hundred percent of     |
| these inspections for the 'A' SG are complete with about 99% evaluated.      |
| About 85% are complete on the 'B' SG with the rest expected to be completed  |
| on 10/22/99.  In addition, a large number of rotating pancake coil probe     |
| inspections are being conducted at other locations in the SGs.  In-situ      |
| pressure testing is being completed where needed.  To date, 4 tubes in the   |
| 'A' SG and 2 tubes in the 'B' SG have been pressure tested.  All 6 of these  |
| tubes have passed at 3 times normal operating differential pressure with     |
| zero leakage.                                                                |
|                                                                              |
| This report is conservatively being made prior to completing the SG testing  |
| and before completely evaluating the effect on the plant.  Further           |
| evaluation of reportability will be completed following the completion of    |
| the eddy current and in-situ pressure testing of the SGs.                    |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| NOTE:  Refer to related Event #36338.                                        |
|                                                                              |
| * * * RETRACTION 0923 EST 11/9/1999 FROM MATZKE TAKEN BY STRANSKY * * *      |
|                                                                              |
| "Both steam generators were declared in category C-3 per Technical           |
| Specification 3.17 due to having greater than 1% of the inspected tubes      |
| being found defective. In steam generator RC-2A, 63 tubes were found         |
| defective out of 4901 inspected tubes. In steam generator RC-2B, 57 tubes    |
| were found defective out of 4905 inspected tubes.                            |
|                                                                              |
| "The technical specifications contain provisions for plugging tubes when     |
| they are found to contain defects that penetrate greater than 40%            |
| through-wall. Under this technical specification, it is expected that the    |
| plant may operate for a period of time with defects greater than 40%         |
| through-wall prior to being found and plugged. The tubes that were found to  |
| contain defects were plugged in accordance with technical specifications.    |
| The plugging criteria currently in use at Fort Calhoun Station requires that |
| all indications of corrosion detected by eddy current are plugged on         |
| detection due to the absence of a qualified technique for sizing             |
| indications.                                                                 |
|                                                                              |
| "Following eddy current testing of the steam generator tubes, in-situ        |
| pressure testing was performed on certain defects which exceeded the         |
| screening criteria. The criteria is based on the potential to exceed the     |
| performance criteria for leakage or structural integrity. The leakage        |
| performance criterion requires that leakage from all defects within a steam  |
| generator shall not exceed 1 gallon per minute under worst case accident     |
| differential pressure and the structural integrity performance criterion     |
| states that the tubes shall withstand pressure of up to three times normal   |
| operating differential pressure without burst. Selected indications which    |
| are representative of the worst of the population of indications found in    |
| the steam generators successfully passed in-situ pressure tests with no      |
| leakage at worst case accident differential pressure and no leakage at three |
| times normal operating differential pressure. There was no detectable        |
| primary-to-secondary leakage during operation prior to shutdown for the      |
| current refueling outage. Therefore, the steam generators were both          |
| available to perform their required safety functions as verified through     |
| in-situ pressure testing. Based on the testing performed, the tubes are not  |
| considered to have been seriously degraded, the plant was not in an          |
| unanalyzed condition, the steam generators would have performed their design |
| basis functions during accident conditions, and this did not constitute a    |
| condition outside the plant's operating and emergency procedures.            |
|                                                                              |
| "The original reports were made conservatively awaiting the completion of    |
| the inspection and testing program. The reports are now being retracted      |
| based on the complete testing results. The Fort Calhoun Station Technical    |
| Specification 30-day plugging report and 6-month inspection report will be   |
| submitted as required."                                                      |
|                                                                              |
| The NRC resident inspector has been informed of this retraction by the       |
| licensee. Notified R4DO (Smith).                                             |
|                                                                              |
| * * * UPDATE AT 1605 ON 11/11/99 MATZKE TO GOULD * * *  UNRETRACT A          |
| RETRACTION                                                                   |
|                                                                              |
| As a result of discussions with NRC personnel on 11/10/99, regarding         |
| reporting requirements, OPPD is withdrawing the retraction notification of   |
| 11/09/99, and changing the basis of the original notification to             |
| "voluntary".  This is because the reporting requirements of 10CFR50.72 were  |
| determined to be not applicable, and thus it is not clear that reporting     |
| pursuant to the technical specifications is required.  However, due to NRC   |
| desire for formal, prompt notification of this type of event and the absence |
| of explicit regulatory guidance, reporting on a voluntary basis appears      |
| appropriate.                                                                 |
|                                                                              |
| The 30 day steam generator tube plugging report to the NRC pursuant to       |
| Technical Specification 3.17(5)(i) has been sent.  The six month steam       |
| generator inspection report pursuant to Technical Specification 3.17(5)(ii)  |
| will be sent as required and will include the information requested in the   |
| second sentence of Technical Specification 3.17(5)(iii).                     |
|                                                                              |
| The licensess notified the NRC Resident Inspector.  The NRC Operations       |
| Officer notified R4DO (Linda Smith).                                         |
+------------------------------------------------------------------------------+

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36336       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: NINE MILE POINT          REGION:  1  |NOTIFICATION DATE: 10/22/1999|
|    UNIT:  [1] [] []                 STATE:  NY |NOTIFICATION TIME: 20:55[EDT]|
|   RXTYPE: [1] GE-2,[2] GE-5                    |EVENT DATE:        10/22/1999|
+------------------------------------------------+EVENT TIME:        19:55[EDT]|
| NRC NOTIFIED BY:  DON SHEEHAN                  |LAST UPDATE DATE:  11/10/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |WILLIAM COOK         R1      |
|10 CFR SECTION:                                 |                             |
|AOUT 50.72(b)(1)(ii)(B)  OUTSIDE DESIGN BASIS   |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       98       Power Operation  |98       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - UNIT 1 IS OPERATING OUTSIDE ITS DESIGN BASIS IN ITS CURRENT OPERATING      |
| CONDITION -                                                                  |
|                                                                              |
| Unit 1 received information from its Engineering Department that Unit 1 is   |
| operating outside of design basis in its current operating condition.        |
| Specifically, with #11 Reactor Recirc Pump fully isolated, an analysis for   |
| thermal shock caused by initiation of #12 Emergency Cooling Loop injecting   |
| through #11 Reactor Recirc Loop suction nozzle has not been performed.       |
| Mitigating actions include isolating #12 Emergency Cooling Loop, in order to |
| return the plant to an analyzed condition, which requires that the plant     |
| enter a 7-Day Technical Specification Shutdown LCO until such time that an   |
| analysis for thermal shock has been performed.  Engineering Department has   |
| reasonable assurance that this analysis will be completed within the 7 days  |
| required by Unit 1 Tech Specs.                                               |
|                                                                              |
| All other Emergency Core Cooling System equipment is operable.               |
|                                                                              |
| This event has no effect on Unit 2.                                          |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| * * * UPDATE AT 1349 ON 11/10/99 BY KIRCHNER TAKEN BY WEAVER * * *           |
|                                                                              |
| A licensee engineering supporting analysis has been performed which          |
| demonstrated that the plant has been operating within the design basis.      |
| Therefore, this event has been retracted.  The licensee notified the NRC     |
| resident inspector.  The NRC Operations Officer notified R1DO (Dan Holody).  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36338       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FT CALHOUN               REGION:  4  |NOTIFICATION DATE: 10/23/1999|
|    UNIT:  [1] [] []                 STATE:  NE |NOTIFICATION TIME: 20:59[EDT]|
|   RXTYPE: [1] CE                               |EVENT DATE:        10/23/1999|
+------------------------------------------------+EVENT TIME:        16:45[CDT]|
| NRC NOTIFIED BY:  KEVIN BOSTON                 |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA SMITH          R4      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - Steam Generator #RC-2B is in Tech Spec Category C-3 -                      |
|                                                                              |
| In accordance with Tech Spec Section 3.17(5), Reporting Requirements, the    |
| following 4-hour non-emergency report is being made:                         |
|                                                                              |
| During eddy current testing of tubes of Steam Generator (SG) #RC-2B, greater |
| than 1% of the tubes tested were found to be defective.  The number of       |
| tested tubes during the 1999 refueling outage is 4905 in SG #RC-2B.  The     |
| number of tubes considered defective and require plugging exceeded 49        |
| tubes.                                                                       |
|                                                                              |
| SG #RC-2B was declared in Tech Spec 3.17, Table 3-13, Category C-3, at 1645  |
| CDT on 10/23/99.  Tube testing is being conducted under procedure            |
| SE-ST-RC-0003, Inservice Testing of Steam Generator Tubes.                   |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
|                                                                              |
| Note:  Refer to related Event #36331.                                        |
|                                                                              |
| *  *  * RETRACTION AT 0923 ON 11/09/99 FROM MATZKE TAKEN BY STRANSKY *  *    |
| *                                                                            |
|                                                                              |
| "Both steam generators were declared in Category C-3 per Technical           |
| Specification 3.17 due to having greater than 1% of the inspected tubes      |
| being found defective. In steam generator RC-2A, 63 tubes were found         |
| defective out of 4901 inspected tubes. In steam generator RC-2B, 57 tubes    |
| were found defective out of 4905 inspected tubes.                            |
|                                                                              |
| "The technical specifications contain provisions for plugging tubes when     |
| they are found to contain defects that penetrate greater than 40%            |
| through-wall. Under this technical specification, it is expected that the    |
| plant may operate for a period of time with defects greater than 40%         |
| through-wall prior to being found and plugged. The tubes that were found to  |
| contain defects were plugged in accordance with technical specifications.    |
| The plugging criteria currently in use at Fort Calhoun Station requires that |
| all indications of corrosion detected by eddy current are plugged on         |
| detection due to the absence of a qualified technique for sizing             |
| indications.                                                                 |
|                                                                              |
| "Following eddy current testing of the steam generator tubes, in-situ        |
| pressure testing was performed on certain defects which exceeded the         |
| screening criteria. The criteria is based on the potential to exceed the     |
| performance criteria for leakage or structural integrity. The leakage        |
| performance criterion requires that leakage from all defects within a steam  |
| generator shall not exceed 1 gallon per minute under worst case accident     |
| differential pressure and the structural integrity performance criterion     |
| states that the tubes shall withstand pressure of up to three times normal   |
| operating differential pressure without burst. Selected indications which    |
| are representative of the worst of the population of indications found in    |
| the steam generators successfully passed in-situ pressure tests with no      |
| leakage at worst case accident differential pressure and no leakage at three |
| times normal operating differential pressure. There was no detectable        |
| primary-to-secondary leakage during operation prior to shutdown for the      |
| current refueling outage. Therefore, the steam generators were both          |
| available to perform their required safety functions as verified through     |
| in-situ pressure testing. Based on the testing performed, the tubes are not  |
| considered to have been seriously degraded, the plant was not in an          |
| unanalyzed condition, the steam generators would have performed their design |
| basis functions during accident conditions, and this did not constitute a    |
| condition outside the plant's operating and emergency procedures.            |
|                                                                              |
| "The original reports were made conservatively awaiting the completion of    |
| the inspection and testing program. The reports are now being retracted      |
| based on the complete testing results. The Fort Calhoun Station Technical    |
| Specification 30-day plugging report and 6-month inspection report will be   |
| submitted as required."                                                      |
|                                                                              |
| The licensee notified the NRC Resident Inspector. The NRC Operations Officer |
| notified R4DO (Linda Smith).                                                 |
|                                                                              |
| *  *  * UPDATE AT 1605 ON 11/11/99 BY MATZKE TO GOULD * * *  UNRETRACT A     |
| RETRACTION                                                                   |
|                                                                              |
| As a result of discussions with NRC personnel on 11/10/99 regarding          |
| reporting requirements, OPPD is withdrawing the retraction notification of   |
| 11/09/99, and changing the basis of the original notification to             |
| "voluntary".  This is because the reporting requirements of 10CFR50.72 were  |
| determined to be not applicable, and thus it is not clear that reporting     |
| pursuant to the technical specifications is required.  However, due to NRC   |
| desire for formal, prompt notification of this type of event and the absence |
| of explicit regulatory guidance, reporting on a voluntary basis appears      |
| appropriate.                                                                 |
|                                                                              |
| The 30 day steam generator tube plugging report to the NRC pursuant to       |
| Technical Specification 3.17(5)(i) has been sent.  The six month steam       |
| generator inspection report pursuant to Technical Specification 3.17(5)(ii)  |
| will be sent as required and will include the information requested in the   |
| second sentence of Technical Specification 3.1 7(5)(iii).                    |
|                                                                              |
| The licensee notified the NRC Resident Inspector.  The NRC Operations        |
| Officer notified R4DO (Linda Smith).                                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36418       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 11/10/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 14:33[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        11/10/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:             [EST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/10/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |MICHAEL PARKER       R3      |
|  DOCKET:  0707002                              |JOHN HICKEY          NMSS    |
+------------------------------------------------+JOSEPH GIITTER       IRO     |
| NRC NOTIFIED BY:  ERIC SPAETH                  |                             |
|  HQ OPS OFFICER:  DOUG WEAVER                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 4 HOUR BULLETIN 91-01 REPORT                                                 |
|                                                                              |
| On November 11, 1999 at 1020, the Nuclear Criticality Safety (NCS) staff     |
| determined that a Nuclear Criticality Safely Approval (NCSA) for X-705 was   |
| deficient.  The compressor turnover pit located in the equipment disassembly |
| north tear down area, has a sump pump which activates if solution should     |
| accumulate above 2.3 inches.  NCSA-0705_031.AOO analyzed the turnover pit,   |
| assuming a maximum enrichment of 3%.  The Nuclear Criticality Safety         |
| Evaluation (NCSE) for this operation failed to consider the contingency that |
| the Geometrically Safe Storage (GSS) located overhead, which was analyzed at |
| 100% enrichment, could leak into the compressor turnover pit.                |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   36419       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  STATE OF LOUISIANA                   |NOTIFICATION DATE: 11/10/1999|
|LICENSEE:  MOORE & ASSOCIATES, INC.             |NOTIFICATION TIME: 16:00[EST]|
|    CITY:                           REGION:  4  |EVENT DATE:        11/10/1999|
|  COUNTY:  E. BATON ROUGE PAR.       STATE:  LA |EVENT TIME:        07:00[CST]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  11/10/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |LINDA SMITH          R4      |
|                                                |                             |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  TORY MEAUX                   |                             |
|  HQ OPS OFFICER:  DOUG WEAVER                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT - STOLEN MOISTURE/DENSITY GAUGE                       |
|                                                                              |
| The state of Louisiana reported that a Campbell moisture/density gauge,      |
| model MC3, serial number 6368, was stolen on 11/10/99.  The gauge was        |
| reported missing at 0700 CST on 11/10/99.  The gauge contains 10 �Ci of      |
| Cs-137 and a 50 �Ci AmBe source.  The gauge was stolen from the back of a    |
| truck at the offices of Moore & Associates.  The lock on the gauge had been  |
| cut.  The theft was reported to the local and state police departments.      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36420       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HATCH                    REGION:  2  |NOTIFICATION DATE: 11/10/1999|
|    UNIT:  [1] [2] []                STATE:  GA |NOTIFICATION TIME: 17:39[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        15:49[EST]|
| NRC NOTIFIED BY:  BARRY COLEMAN                |LAST UPDATE DATE:  11/10/1999|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES OGLE         R2      |
|10 CFR SECTION:                                 |                             |
|HFIT 26.73               FITNESS FOR DUTY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| FITNESS FOR DUTY REPORT                                                      |
|                                                                              |
| A supervisory contract employee was found to have used two illegal drugs     |
| during a random drug screening.                                              |
| The NRC resident inspector has been notified.                                |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36421       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRUNSWICK                REGION:  2  |NOTIFICATION DATE: 11/10/1999|
|    UNIT:  [1] [2] []                STATE:  NC |NOTIFICATION TIME: 19:09[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        18:15[EST]|
| NRC NOTIFIED BY:  DAN HARDIN                   |LAST UPDATE DATE:  11/10/1999|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES OGLE         R2      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| SECURITY REPORT                                                              |
|                                                                              |
| UNESCORTED ACCESS GRANTED INAPPROPRIATELY.   IMMEDIATE CORRECTIVE ACTIONS    |
| TAKEN UPON DISCOVERY.  THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR.     |
| SEE THE HOO LOG FOR ADDITIONAL DETAILS.                                      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36422       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DUANE ARNOLD             REGION:  3  |NOTIFICATION DATE: 11/10/1999|
|    UNIT:  [1] [] []                 STATE:  IA |NOTIFICATION TIME: 21:27[EST]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        19:10[CST]|
| NRC NOTIFIED BY:  DICK FOWLER                  |LAST UPDATE DATE:  11/10/1999|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MICHAEL PARKER       R3      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| INTERGRANULAR STRESS CORROSION CRACKING IDENTIFIED ON RECIRCULATION RISER    |
| WELD                                                                         |
|                                                                              |
| While performing ultrasonic examination of recirculation riser weld          |
| #RRF-F002, nozzle to safe end weld, indications of Intergranular Stress      |
| Corrosion Cracking (IGSCC) were identified.  Specifically, a 0.3 inch X 13   |
| inch long crack on the nozzle to safe end weld.   This nozzle was being      |
| inspected as part of an expanded inspection scope as a result of similar     |
| indications found on the 'B' recirc riser to safe end weld.  To date,        |
| indications have been found on the 'B', 'D', and 'F' nozzles with no         |
| indications on the 'A' and 'C' nozzles.  The 'E', 'G' and 'H' inspections    |
| have not been completed.                                                     |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
|                                                                              |
| See events #36402 and #36416.                                                |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36423       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 11/10/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 22:02[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        11/09/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        23:15[EST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/10/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |MICHAEL PARKER       R3      |
|  DOCKET:  0707002                              |ROBERT PIERSON       NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  JEFF CASTLE                  |                             |
|  HQ OPS OFFICER:  DOUG WEAVER                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24 HOUR BULLETIN 91-01 REPORT                                                |
|                                                                              |
| At 2315 on 11/09/99, a maintenance mechanic in the X-330 building identified |
| four pieces of equipment which violated NCSA-PLANT062.A02 requirement #4     |
| which states "Openings / penetrations made during maintenance activities     |
| shall be covered to minimize the potential for moderator collection and      |
| moist air exposure when unattended".  The violations were corrected by       |
| repairing or replacing the damaged covers by 0218 on 11/10/99.   One         |
| additional violation of the NCSA requirement was identified during followup  |
| facility walkdowns.   The additional piece of equipment was discovered in    |
| the X-330 building at 1030 on 11/10/99.  This deficiency was corrected at    |
| 1259 on 11/10/99.  This constitutes a loss of control such that only one     |
| double contingency control remains in place.                                 |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36424       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BYRON                    REGION:  3  |NOTIFICATION DATE: 11/11/1999|
|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 03:06[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        22:20[CST]|
| NRC NOTIFIED BY:  MARRI MARCHIONDA             |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MICHAEL PARKER       R3      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - S/G  LEVEL DROPPED TO REACTOR TRIP/AFW AUTO START SETPOINT DURING          |
| MAINTENANCE -                                                                |
|                                                                              |
| At 2220 CST on 11/10/99 with Unit 2 in Mode 5 (Cold Shutdown), priming of    |
| the feedwater isolation valves to support maintenance activities was in      |
| progress.  While priming the 'B' steam generator (S/G) feedwater isolation   |
| valve #2FW009B, the valve was opened and water back-flowed from the 'B' S/G  |
| into the feedwater piping and the S/G level decreased to the low level 2     |
| reactor trip setpoint of 36.3% which is also the setpoint for the autostart  |
| of the auxiliary feedwater (AFW) system.  The initial level in the 'B' S/G   |
| was 50%.  A reactor protection system actuation and engineered safety        |
| features actuation occurred and all plant systems responded normally for     |
| Mode 5.  The reactor trip breakers opened but the control rod drive system   |
| was out of service and not capable of control rod withdrawal.  The AFW       |
| auxiliary lube oil pumps auto started but the AFW pumps were in pull-to-lock |
| due to current plant conditions so the AFW pumps did not start.  The cause   |
| of the level decrease is due to unfilled feedwater piping following outage   |
| restoration.  Corrective action is being determined.  This event is          |
| reportable under the requirements of 10CFR50.72(b)(2)(ii).                   |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36425       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FERMI                    REGION:  3  |NOTIFICATION DATE: 11/11/1999|
|    UNIT:  [2] [] []                 STATE:  MI |NOTIFICATION TIME: 09:59[EST]|
|   RXTYPE: [2] GE-4                             |EVENT DATE:        11/11/1999|
+------------------------------------------------+EVENT TIME:        07:15[EST]|
| NRC NOTIFIED BY:  MIKE PHILIPPON               |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MICHAEL PARKER       R3      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2     N          Y       97       Power Operation  |97       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - REACTOR WATER CLEANUP SYSTEM ISOLATION DUE TO HIGH DIFFERENTIAL            |
| TEMPERATURE -                                                                |
|                                                                              |
| A Reactor Water Cleanup (RWCU) System steam leak detection high differential |
| temperature alarm was received and the subsequent isolation of the outboard  |
| isolation valves #G33F004 and #G33F220 occurred.  The reactor building was   |
| immediately evacuated and access was restricted as a precaution until the    |
| cause of the high temperature alarm and RWCU System isolation could be       |
| determined.  Although it was confirmed that there was no steam leak, the     |
| RWCU System isolation signal was considered valid because an actual high     |
| differential temperature condition existed.  The valid isolation signal was  |
| a result of a trip of the Reactor Building HVAC System and the failure of    |
| the RWCU pump 'B' room cooler to automatically start on high room            |
| temperature.  Investigation revealed that the thermal overloads on the RWCU  |
| room cooler were tripped.  The Reactor Building HVAC System had tripped on   |
| low freezstat (temperature switch) temperature.  All other systems operated  |
| as expected, and the RWCU System remains shut down pending investigation of  |
| the failure of the 'B' room cooler to start.                                 |
|                                                                              |
| The NRC Resident Inspector was notified by the licensee.                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36426       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PALISADES                REGION:  3  |NOTIFICATION DATE: 11/11/1999|
|    UNIT:  [1] [] []                 STATE:  MI |NOTIFICATION TIME: 11:18[EST]|
|   RXTYPE: [1] CE                               |EVENT DATE:        11/10/1999|
+------------------------------------------------+EVENT TIME:        14:00[EST]|
| NRC NOTIFIED BY:  STEVE ELLIS                  |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MICHAEL PARKER       R3      |
|10 CFR SECTION:                                 |                             |
|HFIT 26.73               FITNESS FOR DUTY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - TWO EMPTY BEER CANS FOUND IN A TRAILER INSIDE THE PLANT PROTECTED AREA -   |
|                                                                              |
| Plant janitors found two empty beer cans in a shower trailer in a            |
| maintenance workers area inside the plant protected area.  The licensee is   |
| interviewing the janitors and searched the trailer for additional cans; none |
| were found.  The licensee sent the cans to the local police for possible     |
| identification of fingerprints; results are pending.  The licensee searched  |
| the hand held items of people exiting the plant protected area; nothing      |
| unusual was found.  The licensee notified the NRC Resident Inspector and is  |
| continuing to investigate this incident.                                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36427       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: ARKANSAS NUCLEAR         REGION:  4  |NOTIFICATION DATE: 11/11/1999|
|    UNIT:  [] [2] []                 STATE:  AR |NOTIFICATION TIME: 17:53[EST]|
|   RXTYPE: [1] B&W-L-LP,[2] CE                  |EVENT DATE:        11/11/1999|
+------------------------------------------------+EVENT TIME:        16:45[CST]|
| NRC NOTIFIED BY:  SCOTT                        |LAST UPDATE DATE:  11/11/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA SMITH          R4      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| FAILURE OF INSIDE AND OUTSIDE CCW CONTAINMENT ISOLATION VALVES.              |
|                                                                              |
| ON 11/09/99, WHILE IN MODE 5, COLD SHUTDOWN, FOR MID-CYCLE OUTAGE, THE       |
| OUTSIDE CONTAINMENT ISOLATION VALVE FOR COMPONENT COOLING WATER (CCW) RETURN |
| (2CV-5255-1) FAILED TO FULLY CLOSE BASED ON FLOW NOISE DURING THE INITIAL    |
| STROKE. THE VALVE WAS STROKED 10 TIMES AND APPEARED TO CLOSE ON ALL STROKES  |
| FOLLOWING THE INITIAL ATTEMPT.  ON 11/10/99, THE INSIDE CONTAINMENT          |
| ISOLATION VALVE FOR CCW RETURN (2CV-5254-2) FAILED TO REACH THE TRAVEL LIMIT |
| ON ITS FIRST STROKE.  AN IMPROMPTU LEAK TEST USING WATER WITH 2CV-5254-2 IN  |
| ITS INITIAL POSITION INDICATED 300-500 ML/MIN LEAKAGE VIA THE VALVE SEAT.    |
| BOTH VALVES WERE OVERHAULED DURING THE REFUELING OUTAGE IN EARLY 1999 AND    |
| SUCCESSFULLY PASSED POST-MAINTENANCE TESTING. DETERMINATION OF THE CAUSE(S)  |
| AND RESTORATION OF BOTH VALVES TO AN OPERABLE STATUS WILL BE COMPLETED       |
| BEFORE PLANT STARTUP.  THERE DOES NOT APPEAR TO BE FIRM EVIDENCE CONCERNING  |
| A TIME OF FAILURE BEFORE THE CONDITIONS WERE DISCOVERED.  ON NOVEMBER 11,    |
| 1999, DURING A REVIEW OF THESE CONDITIONS AFFECTING THE SAME CONTAINMENT     |
| PENETRATION, IT WAS DETERMINED THAT THEY MET THE REPORTING CRITERION OF      |
| 10CFR5O.72(b)(2)(I) AS A SERIOUS DEGRADATION OF A PRINCIPAL SAFETY BARRIER   |
| (REACTOR CONTAINMENT) FOUND WHILE SHUTDOWN.                                  |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED.                                         |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021