Event Notification Report for November 12, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/10/1999 - 11/12/1999 ** EVENT NUMBERS ** 36331 36336 36338 36418 36419 36420 36421 36422 36423 36424 36425 36426 36427 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36331 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FT CALHOUN REGION: 4 |NOTIFICATION DATE: 10/22/1999| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 13:04[EDT]| | RXTYPE: [1] CE |EVENT DATE: 10/22/1999| +------------------------------------------------+EVENT TIME: 09:22[CDT]| | NRC NOTIFIED BY: ERICK MATZKE |LAST UPDATE DATE: 11/11/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA SMITH R4 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Steam Generator #RC-2A in Tech Spec Category C-3; Steam Generator | | inspections continuing - | | | | At 0922 CDT on 10/22/99, during eddy current testing of the steam generators | | (SG), it has been determined that 50 tubes in SG #RC-2A require plugging. | | This places SG #RC-2A in Technical Specification category C-3 per 3.17(2). | | Forty-four tubes have been determined to require plugging in SG #RC-2B at | | this time. Eddy current testing is continuing on the SGs. A 100% full | | length bobbin coil inspection program has been completed in both SGs. A | | rotating pancake coil probe (Plus Point) is being used to inspect 100% of | | the top of the hot leg tube sheets for both SGs. One hundred percent of | | these inspections for the 'A' SG are complete with about 99% evaluated. | | About 85% are complete on the 'B' SG with the rest expected to be completed | | on 10/22/99. In addition, a large number of rotating pancake coil probe | | inspections are being conducted at other locations in the SGs. In-situ | | pressure testing is being completed where needed. To date, 4 tubes in the | | 'A' SG and 2 tubes in the 'B' SG have been pressure tested. All 6 of these | | tubes have passed at 3 times normal operating differential pressure with | | zero leakage. | | | | This report is conservatively being made prior to completing the SG testing | | and before completely evaluating the effect on the plant. Further | | evaluation of reportability will be completed following the completion of | | the eddy current and in-situ pressure testing of the SGs. | | | | The licensee notified the NRC Resident Inspector. | | | | NOTE: Refer to related Event #36338. | | | | * * * RETRACTION 0923 EST 11/9/1999 FROM MATZKE TAKEN BY STRANSKY * * * | | | | "Both steam generators were declared in category C-3 per Technical | | Specification 3.17 due to having greater than 1% of the inspected tubes | | being found defective. In steam generator RC-2A, 63 tubes were found | | defective out of 4901 inspected tubes. In steam generator RC-2B, 57 tubes | | were found defective out of 4905 inspected tubes. | | | | "The technical specifications contain provisions for plugging tubes when | | they are found to contain defects that penetrate greater than 40% | | through-wall. Under this technical specification, it is expected that the | | plant may operate for a period of time with defects greater than 40% | | through-wall prior to being found and plugged. The tubes that were found to | | contain defects were plugged in accordance with technical specifications. | | The plugging criteria currently in use at Fort Calhoun Station requires that | | all indications of corrosion detected by eddy current are plugged on | | detection due to the absence of a qualified technique for sizing | | indications. | | | | "Following eddy current testing of the steam generator tubes, in-situ | | pressure testing was performed on certain defects which exceeded the | | screening criteria. The criteria is based on the potential to exceed the | | performance criteria for leakage or structural integrity. The leakage | | performance criterion requires that leakage from all defects within a steam | | generator shall not exceed 1 gallon per minute under worst case accident | | differential pressure and the structural integrity performance criterion | | states that the tubes shall withstand pressure of up to three times normal | | operating differential pressure without burst. Selected indications which | | are representative of the worst of the population of indications found in | | the steam generators successfully passed in-situ pressure tests with no | | leakage at worst case accident differential pressure and no leakage at three | | times normal operating differential pressure. There was no detectable | | primary-to-secondary leakage during operation prior to shutdown for the | | current refueling outage. Therefore, the steam generators were both | | available to perform their required safety functions as verified through | | in-situ pressure testing. Based on the testing performed, the tubes are not | | considered to have been seriously degraded, the plant was not in an | | unanalyzed condition, the steam generators would have performed their design | | basis functions during accident conditions, and this did not constitute a | | condition outside the plant's operating and emergency procedures. | | | | "The original reports were made conservatively awaiting the completion of | | the inspection and testing program. The reports are now being retracted | | based on the complete testing results. The Fort Calhoun Station Technical | | Specification 30-day plugging report and 6-month inspection report will be | | submitted as required." | | | | The NRC resident inspector has been informed of this retraction by the | | licensee. Notified R4DO (Smith). | | | | * * * UPDATE AT 1605 ON 11/11/99 MATZKE TO GOULD * * * UNRETRACT A | | RETRACTION | | | | As a result of discussions with NRC personnel on 11/10/99, regarding | | reporting requirements, OPPD is withdrawing the retraction notification of | | 11/09/99, and changing the basis of the original notification to | | "voluntary". This is because the reporting requirements of 10CFR50.72 were | | determined to be not applicable, and thus it is not clear that reporting | | pursuant to the technical specifications is required. However, due to NRC | | desire for formal, prompt notification of this type of event and the absence | | of explicit regulatory guidance, reporting on a voluntary basis appears | | appropriate. | | | | The 30 day steam generator tube plugging report to the NRC pursuant to | | Technical Specification 3.17(5)(i) has been sent. The six month steam | | generator inspection report pursuant to Technical Specification 3.17(5)(ii) | | will be sent as required and will include the information requested in the | | second sentence of Technical Specification 3.17(5)(iii). | | | | The licensess notified the NRC Resident Inspector. The NRC Operations | | Officer notified R4DO (Linda Smith). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36336 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 10/22/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 20:55[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 10/22/1999| +------------------------------------------------+EVENT TIME: 19:55[EDT]| | NRC NOTIFIED BY: DON SHEEHAN |LAST UPDATE DATE: 11/10/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM COOK R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 98 Power Operation |98 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - UNIT 1 IS OPERATING OUTSIDE ITS DESIGN BASIS IN ITS CURRENT OPERATING | | CONDITION - | | | | Unit 1 received information from its Engineering Department that Unit 1 is | | operating outside of design basis in its current operating condition. | | Specifically, with #11 Reactor Recirc Pump fully isolated, an analysis for | | thermal shock caused by initiation of #12 Emergency Cooling Loop injecting | | through #11 Reactor Recirc Loop suction nozzle has not been performed. | | Mitigating actions include isolating #12 Emergency Cooling Loop, in order to | | return the plant to an analyzed condition, which requires that the plant | | enter a 7-Day Technical Specification Shutdown LCO until such time that an | | analysis for thermal shock has been performed. Engineering Department has | | reasonable assurance that this analysis will be completed within the 7 days | | required by Unit 1 Tech Specs. | | | | All other Emergency Core Cooling System equipment is operable. | | | | This event has no effect on Unit 2. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE AT 1349 ON 11/10/99 BY KIRCHNER TAKEN BY WEAVER * * * | | | | A licensee engineering supporting analysis has been performed which | | demonstrated that the plant has been operating within the design basis. | | Therefore, this event has been retracted. The licensee notified the NRC | | resident inspector. The NRC Operations Officer notified R1DO (Dan Holody). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36338 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FT CALHOUN REGION: 4 |NOTIFICATION DATE: 10/23/1999| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 20:59[EDT]| | RXTYPE: [1] CE |EVENT DATE: 10/23/1999| +------------------------------------------------+EVENT TIME: 16:45[CDT]| | NRC NOTIFIED BY: KEVIN BOSTON |LAST UPDATE DATE: 11/11/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA SMITH R4 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Steam Generator #RC-2B is in Tech Spec Category C-3 - | | | | In accordance with Tech Spec Section 3.17(5), Reporting Requirements, the | | following 4-hour non-emergency report is being made: | | | | During eddy current testing of tubes of Steam Generator (SG) #RC-2B, greater | | than 1% of the tubes tested were found to be defective. The number of | | tested tubes during the 1999 refueling outage is 4905 in SG #RC-2B. The | | number of tubes considered defective and require plugging exceeded 49 | | tubes. | | | | SG #RC-2B was declared in Tech Spec 3.17, Table 3-13, Category C-3, at 1645 | | CDT on 10/23/99. Tube testing is being conducted under procedure | | SE-ST-RC-0003, Inservice Testing of Steam Generator Tubes. | | | | The licensee notified the NRC Resident Inspector. | | | | Note: Refer to related Event #36331. | | | | * * * RETRACTION AT 0923 ON 11/09/99 FROM MATZKE TAKEN BY STRANSKY * * | | * | | | | "Both steam generators were declared in Category C-3 per Technical | | Specification 3.17 due to having greater than 1% of the inspected tubes | | being found defective. In steam generator RC-2A, 63 tubes were found | | defective out of 4901 inspected tubes. In steam generator RC-2B, 57 tubes | | were found defective out of 4905 inspected tubes. | | | | "The technical specifications contain provisions for plugging tubes when | | they are found to contain defects that penetrate greater than 40% | | through-wall. Under this technical specification, it is expected that the | | plant may operate for a period of time with defects greater than 40% | | through-wall prior to being found and plugged. The tubes that were found to | | contain defects were plugged in accordance with technical specifications. | | The plugging criteria currently in use at Fort Calhoun Station requires that | | all indications of corrosion detected by eddy current are plugged on | | detection due to the absence of a qualified technique for sizing | | indications. | | | | "Following eddy current testing of the steam generator tubes, in-situ | | pressure testing was performed on certain defects which exceeded the | | screening criteria. The criteria is based on the potential to exceed the | | performance criteria for leakage or structural integrity. The leakage | | performance criterion requires that leakage from all defects within a steam | | generator shall not exceed 1 gallon per minute under worst case accident | | differential pressure and the structural integrity performance criterion | | states that the tubes shall withstand pressure of up to three times normal | | operating differential pressure without burst. Selected indications which | | are representative of the worst of the population of indications found in | | the steam generators successfully passed in-situ pressure tests with no | | leakage at worst case accident differential pressure and no leakage at three | | times normal operating differential pressure. There was no detectable | | primary-to-secondary leakage during operation prior to shutdown for the | | current refueling outage. Therefore, the steam generators were both | | available to perform their required safety functions as verified through | | in-situ pressure testing. Based on the testing performed, the tubes are not | | considered to have been seriously degraded, the plant was not in an | | unanalyzed condition, the steam generators would have performed their design | | basis functions during accident conditions, and this did not constitute a | | condition outside the plant's operating and emergency procedures. | | | | "The original reports were made conservatively awaiting the completion of | | the inspection and testing program. The reports are now being retracted | | based on the complete testing results. The Fort Calhoun Station Technical | | Specification 30-day plugging report and 6-month inspection report will be | | submitted as required." | | | | The licensee notified the NRC Resident Inspector. The NRC Operations Officer | | notified R4DO (Linda Smith). | | | | * * * UPDATE AT 1605 ON 11/11/99 BY MATZKE TO GOULD * * * UNRETRACT A | | RETRACTION | | | | As a result of discussions with NRC personnel on 11/10/99 regarding | | reporting requirements, OPPD is withdrawing the retraction notification of | | 11/09/99, and changing the basis of the original notification to | | "voluntary". This is because the reporting requirements of 10CFR50.72 were | | determined to be not applicable, and thus it is not clear that reporting | | pursuant to the technical specifications is required. However, due to NRC | | desire for formal, prompt notification of this type of event and the absence | | of explicit regulatory guidance, reporting on a voluntary basis appears | | appropriate. | | | | The 30 day steam generator tube plugging report to the NRC pursuant to | | Technical Specification 3.17(5)(i) has been sent. The six month steam | | generator inspection report pursuant to Technical Specification 3.17(5)(ii) | | will be sent as required and will include the information requested in the | | second sentence of Technical Specification 3.1 7(5)(iii). | | | | The licensee notified the NRC Resident Inspector. The NRC Operations | | Officer notified R4DO (Linda Smith). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36418 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 11/10/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:33[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 11/10/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: [EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/10/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MICHAEL PARKER R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+JOSEPH GIITTER IRO | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 4 HOUR BULLETIN 91-01 REPORT | | | | On November 11, 1999 at 1020, the Nuclear Criticality Safety (NCS) staff | | determined that a Nuclear Criticality Safely Approval (NCSA) for X-705 was | | deficient. The compressor turnover pit located in the equipment disassembly | | north tear down area, has a sump pump which activates if solution should | | accumulate above 2.3 inches. NCSA-0705_031.AOO analyzed the turnover pit, | | assuming a maximum enrichment of 3%. The Nuclear Criticality Safety | | Evaluation (NCSE) for this operation failed to consider the contingency that | | the Geometrically Safe Storage (GSS) located overhead, which was analyzed at | | 100% enrichment, could leak into the compressor turnover pit. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36419 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: STATE OF LOUISIANA |NOTIFICATION DATE: 11/10/1999| |LICENSEE: MOORE & ASSOCIATES, INC. |NOTIFICATION TIME: 16:00[EST]| | CITY: REGION: 4 |EVENT DATE: 11/10/1999| | COUNTY: E. BATON ROUGE PAR. STATE: LA |EVENT TIME: 07:00[CST]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 11/10/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LINDA SMITH R4 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: TORY MEAUX | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - STOLEN MOISTURE/DENSITY GAUGE | | | | The state of Louisiana reported that a Campbell moisture/density gauge, | | model MC3, serial number 6368, was stolen on 11/10/99. The gauge was | | reported missing at 0700 CST on 11/10/99. The gauge contains 10 �Ci of | | Cs-137 and a 50 �Ci AmBe source. The gauge was stolen from the back of a | | truck at the offices of Moore & Associates. The lock on the gauge had been | | cut. The theft was reported to the local and state police departments. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36420 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 11/10/1999| | UNIT: [1] [2] [] STATE: GA |NOTIFICATION TIME: 17:39[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 11/10/1999| +------------------------------------------------+EVENT TIME: 15:49[EST]| | NRC NOTIFIED BY: BARRY COLEMAN |LAST UPDATE DATE: 11/10/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES OGLE R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS FOR DUTY REPORT | | | | A supervisory contract employee was found to have used two illegal drugs | | during a random drug screening. | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36421 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 11/10/1999| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 19:09[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 11/10/1999| +------------------------------------------------+EVENT TIME: 18:15[EST]| | NRC NOTIFIED BY: DAN HARDIN |LAST UPDATE DATE: 11/10/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES OGLE R2 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY REPORT | | | | UNESCORTED ACCESS GRANTED INAPPROPRIATELY. IMMEDIATE CORRECTIVE ACTIONS | | TAKEN UPON DISCOVERY. THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. | | SEE THE HOO LOG FOR ADDITIONAL DETAILS. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36422 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 11/10/1999| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 21:27[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 11/10/1999| +------------------------------------------------+EVENT TIME: 19:10[CST]| | NRC NOTIFIED BY: DICK FOWLER |LAST UPDATE DATE: 11/10/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MICHAEL PARKER R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INTERGRANULAR STRESS CORROSION CRACKING IDENTIFIED ON RECIRCULATION RISER | | WELD | | | | While performing ultrasonic examination of recirculation riser weld | | #RRF-F002, nozzle to safe end weld, indications of Intergranular Stress | | Corrosion Cracking (IGSCC) were identified. Specifically, a 0.3 inch X 13 | | inch long crack on the nozzle to safe end weld. This nozzle was being | | inspected as part of an expanded inspection scope as a result of similar | | indications found on the 'B' recirc riser to safe end weld. To date, | | indications have been found on the 'B', 'D', and 'F' nozzles with no | | indications on the 'A' and 'C' nozzles. The 'E', 'G' and 'H' inspections | | have not been completed. | | | | The licensee notified the NRC resident inspector. | | | | See events #36402 and #36416. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36423 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 11/10/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 22:02[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 11/09/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 23:15[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/10/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MICHAEL PARKER R3 | | DOCKET: 0707002 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JEFF CASTLE | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR BULLETIN 91-01 REPORT | | | | At 2315 on 11/09/99, a maintenance mechanic in the X-330 building identified | | four pieces of equipment which violated NCSA-PLANT062.A02 requirement #4 | | which states "Openings / penetrations made during maintenance activities | | shall be covered to minimize the potential for moderator collection and | | moist air exposure when unattended". The violations were corrected by | | repairing or replacing the damaged covers by 0218 on 11/10/99. One | | additional violation of the NCSA requirement was identified during followup | | facility walkdowns. The additional piece of equipment was discovered in | | the X-330 building at 1030 on 11/10/99. This deficiency was corrected at | | 1259 on 11/10/99. This constitutes a loss of control such that only one | | double contingency control remains in place. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36424 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BYRON REGION: 3 |NOTIFICATION DATE: 11/11/1999| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 03:06[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/10/1999| +------------------------------------------------+EVENT TIME: 22:20[CST]| | NRC NOTIFIED BY: MARRI MARCHIONDA |LAST UPDATE DATE: 11/11/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MICHAEL PARKER R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - S/G LEVEL DROPPED TO REACTOR TRIP/AFW AUTO START SETPOINT DURING | | MAINTENANCE - | | | | At 2220 CST on 11/10/99 with Unit 2 in Mode 5 (Cold Shutdown), priming of | | the feedwater isolation valves to support maintenance activities was in | | progress. While priming the 'B' steam generator (S/G) feedwater isolation | | valve #2FW009B, the valve was opened and water back-flowed from the 'B' S/G | | into the feedwater piping and the S/G level decreased to the low level 2 | | reactor trip setpoint of 36.3% which is also the setpoint for the autostart | | of the auxiliary feedwater (AFW) system. The initial level in the 'B' S/G | | was 50%. A reactor protection system actuation and engineered safety | | features actuation occurred and all plant systems responded normally for | | Mode 5. The reactor trip breakers opened but the control rod drive system | | was out of service and not capable of control rod withdrawal. The AFW | | auxiliary lube oil pumps auto started but the AFW pumps were in pull-to-lock | | due to current plant conditions so the AFW pumps did not start. The cause | | of the level decrease is due to unfilled feedwater piping following outage | | restoration. Corrective action is being determined. This event is | | reportable under the requirements of 10CFR50.72(b)(2)(ii). | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36425 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 11/11/1999| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 09:59[EST]| | RXTYPE: [2] GE-4 |EVENT DATE: 11/11/1999| +------------------------------------------------+EVENT TIME: 07:15[EST]| | NRC NOTIFIED BY: MIKE PHILIPPON |LAST UPDATE DATE: 11/11/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MICHAEL PARKER R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 97 Power Operation |97 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - REACTOR WATER CLEANUP SYSTEM ISOLATION DUE TO HIGH DIFFERENTIAL | | TEMPERATURE - | | | | A Reactor Water Cleanup (RWCU) System steam leak detection high differential | | temperature alarm was received and the subsequent isolation of the outboard | | isolation valves #G33F004 and #G33F220 occurred. The reactor building was | | immediately evacuated and access was restricted as a precaution until the | | cause of the high temperature alarm and RWCU System isolation could be | | determined. Although it was confirmed that there was no steam leak, the | | RWCU System isolation signal was considered valid because an actual high | | differential temperature condition existed. The valid isolation signal was | | a result of a trip of the Reactor Building HVAC System and the failure of | | the RWCU pump 'B' room cooler to automatically start on high room | | temperature. Investigation revealed that the thermal overloads on the RWCU | | room cooler were tripped. The Reactor Building HVAC System had tripped on | | low freezstat (temperature switch) temperature. All other systems operated | | as expected, and the RWCU System remains shut down pending investigation of | | the failure of the 'B' room cooler to start. | | | | The NRC Resident Inspector was notified by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36426 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALISADES REGION: 3 |NOTIFICATION DATE: 11/11/1999| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 11:18[EST]| | RXTYPE: [1] CE |EVENT DATE: 11/10/1999| +------------------------------------------------+EVENT TIME: 14:00[EST]| | NRC NOTIFIED BY: STEVE ELLIS |LAST UPDATE DATE: 11/11/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MICHAEL PARKER R3 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - TWO EMPTY BEER CANS FOUND IN A TRAILER INSIDE THE PLANT PROTECTED AREA - | | | | Plant janitors found two empty beer cans in a shower trailer in a | | maintenance workers area inside the plant protected area. The licensee is | | interviewing the janitors and searched the trailer for additional cans; none | | were found. The licensee sent the cans to the local police for possible | | identification of fingerprints; results are pending. The licensee searched | | the hand held items of people exiting the plant protected area; nothing | | unusual was found. The licensee notified the NRC Resident Inspector and is | | continuing to investigate this incident. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36427 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 11/11/1999| | UNIT: [] [2] [] STATE: AR |NOTIFICATION TIME: 17:53[EST]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 11/11/1999| +------------------------------------------------+EVENT TIME: 16:45[CST]| | NRC NOTIFIED BY: SCOTT |LAST UPDATE DATE: 11/11/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA SMITH R4 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF INSIDE AND OUTSIDE CCW CONTAINMENT ISOLATION VALVES. | | | | ON 11/09/99, WHILE IN MODE 5, COLD SHUTDOWN, FOR MID-CYCLE OUTAGE, THE | | OUTSIDE CONTAINMENT ISOLATION VALVE FOR COMPONENT COOLING WATER (CCW) RETURN | | (2CV-5255-1) FAILED TO FULLY CLOSE BASED ON FLOW NOISE DURING THE INITIAL | | STROKE. THE VALVE WAS STROKED 10 TIMES AND APPEARED TO CLOSE ON ALL STROKES | | FOLLOWING THE INITIAL ATTEMPT. ON 11/10/99, THE INSIDE CONTAINMENT | | ISOLATION VALVE FOR CCW RETURN (2CV-5254-2) FAILED TO REACH THE TRAVEL LIMIT | | ON ITS FIRST STROKE. AN IMPROMPTU LEAK TEST USING WATER WITH 2CV-5254-2 IN | | ITS INITIAL POSITION INDICATED 300-500 ML/MIN LEAKAGE VIA THE VALVE SEAT. | | BOTH VALVES WERE OVERHAULED DURING THE REFUELING OUTAGE IN EARLY 1999 AND | | SUCCESSFULLY PASSED POST-MAINTENANCE TESTING. DETERMINATION OF THE CAUSE(S) | | AND RESTORATION OF BOTH VALVES TO AN OPERABLE STATUS WILL BE COMPLETED | | BEFORE PLANT STARTUP. THERE DOES NOT APPEAR TO BE FIRM EVIDENCE CONCERNING | | A TIME OF FAILURE BEFORE THE CONDITIONS WERE DISCOVERED. ON NOVEMBER 11, | | 1999, DURING A REVIEW OF THESE CONDITIONS AFFECTING THE SAME CONTAINMENT | | PENETRATION, IT WAS DETERMINED THAT THEY MET THE REPORTING CRITERION OF | | 10CFR5O.72(b)(2)(I) AS A SERIOUS DEGRADATION OF A PRINCIPAL SAFETY BARRIER | | (REACTOR CONTAINMENT) FOUND WHILE SHUTDOWN. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021