The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for November 8, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           11/05/1999 - 11/08/1999

                              ** EVENT NUMBERS **

36287  36364  36400  36401  36402  36403  36404  36405  36406  36407  36408  36409 
36410  36411  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36287       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 10/13/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 16:00[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        10/13/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        00:10[CDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/05/1999|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |JOHN MADERA          R3      |
|  DOCKET:  0707001                              |SCOTT MOORE          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  WALKER                       |                             |
|  HQ OPS OFFICER:  CHAUNCEY GOULD               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NCFR                     NON CFR REPORT REQMNT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| At 0010 on 10/13/99, the PSS office was notified that a primary condensate   |
| alarm was received on the C-360 position 4 autoclave Water Inventory Control |
| System (WICS). The WICS system is required to be operable while heating in   |
| mode 5 according to TSR 21.4.3. The autoclave was checked according to the   |
| alarm response procedure and subsequently removed from service and declared  |
| inoperable by the Plant Shift Superintendent.                                |
| Troubleshooting was initiated and is continuing in order to determine the    |
| reason for the alarm.                                                        |
|                                                                              |
| The NRC senior resident has been notified of this event.                     |
|                                                                              |
| * * * UPDATE 2220EST ON 11/5/99 FROM E.G. WALKER TO S. SANDIN * * *          |
|                                                                              |
| "On 11/2/99, the same type of actuation occurred on the C-360 autoclave No.  |
| 1 while out of service and open. While investigating this invalid actuation, |
| it was discovered that the gain adjustment on one of the WICS channels had   |
| drifted out of tolerance.  Discussions with the component manufacturer       |
| concluded that the WICS alarm cards are susceptible to drift due to age and  |
| fluctuations in temperature.  These cards are exposed to ambient             |
| temperatures, but the cards are rated for the range of temperatures at the   |
| autoclaves.  Given this and other indications that the WICS actuation        |
| signals were invalid, i.e., not the result of water backing up in the drain, |
| it has been concluded that the subject actuation on 10/13/99 was caused by   |
| [an] invalid signal (instrument drift) and thus does not meet the criteria   |
| for reporting and should be retracted."                                      |
|                                                                              |
| The NRC resident has been notified of this retraction.  Notified             |
| R3DO(Creed).                                                                 |
+------------------------------------------------------------------------------+

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36364       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 10/28/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 16:16[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        10/27/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        17:05[CDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/05/1999|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |MIKE JORDAN          R3      |
|  DOCKET:  0707001                              |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  W.F. CAGE                    |                             |
|  HQ OPS OFFICER:  DOUG WEAVER                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NLTR                     LICENSEE 24 HR REPORT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| Safety System Actuation                                                      |
|                                                                              |
| At  1705 CDT on 10/27/99, the Plant Shift Superintendent's (PSS) office was  |
| notified that a primary condensate alarm was received on the C-360 position  |
| 2 autoclave Water Inventory Control (WIC) System.  The WIC system is         |
| required to be operable while heating in mode 5 according to TSR 2.1.4.3.    |
| The autoclave was checked according to the alarm response procedure, removed |
| from service and declared inoperable by the PSS. Troubleshooting was         |
| initiated and is continuing in order to determine the reason for the alarm.  |
|                                                                              |
| The safety system actuation is reportable to the NRC as required by Safety   |
| Analysis Report, section 6.9, table 1 criteria J.2, Safety System actuation  |
| due to a valid signal as a 24-hour event notification.                       |
|                                                                              |
| The NRC resident inspector has been notified.                                |
|                                                                              |
| * * * UPDATE 2220EST ON 11/5/99 FROM E.G. WALKER TO S. SANDIN * * *          |
|                                                                              |
| "On 11/2/99, the same type of actuation occurred on the C-360 autoclave No.  |
| 1 while out of service and open. While investigating this invalid actuation, |
| it was discovered that the gain adjustment on one of the WICS channels had   |
| drifted out of tolerance.  Discussions with the component manufacturer       |
| concluded that the WICS alarm cards are susceptible to drift due to age and  |
| fluctuations in temperature.  These cards are exposed to ambient             |
| temperatures, but the cards are rated for the range of temperatures at the   |
| autoclaves.  Given this and other indications that the WICS actuation        |
| signals were invalid, i.e., not the result of water backing up in the drain, |
| it has been concluded that the subject actuation on 10/27/99 was caused by   |
| [an] invalid signal (instrument drift) and thus does not meet the criteria   |
| for reporting and should be retracted."                                      |
|                                                                              |
| The NRC resident inspector has been notified of this retraction.  Notified   |
| R3DO(Creed).                                                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36400       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: POINT BEACH              REGION:  3  |NOTIFICATION DATE: 11/05/1999|
|    UNIT:  [1] [] []                 STATE:  WI |NOTIFICATION TIME: 04:07[EST]|
|   RXTYPE: [1] W-2-LP,[2] W-2-LP                |EVENT DATE:        11/04/1999|
+------------------------------------------------+EVENT TIME:        20:30[CST]|
| NRC NOTIFIED BY:  RICK ROBBINS                 |LAST UPDATE DATE:  11/05/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED          R3      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 0.25 INCH LONG CRACK WAS FOUND ON "1A" STEAM GENERATOR HEAD DRAIN VALVE.     |
|                                                                              |
| During a liquid penetrant examination of a weld on the top side of valve     |
| 1R-526A, the '1A' Steam Generator head drain, a 0.25" long crack was found.  |
| This appears to be a crack in the weld metal only, through wall of the       |
| Reactor Coolant System pressure boundary.                                    |
|                                                                              |
| During initial screening of this condition at 2030 hours on 11/04/99 it was  |
| not considered seriously degraded as no leak was detected while at power     |
| (boric acid crystals were found in the vicinity of the valve).  Upon further |
| review at 0200 hours on 11/05/99 this 4 hour non-emergency report was made.  |
|                                                                              |
| The NRC Resident Inspector will be notified of this event by the licensee.   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36401       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: KEWAUNEE                 REGION:  3  |NOTIFICATION DATE: 11/05/1999|
|    UNIT:  [1] [] []                 STATE:  WI |NOTIFICATION TIME: 05:21[EST]|
|   RXTYPE: [1] W-2-LP                           |EVENT DATE:        11/05/1999|
+------------------------------------------------+EVENT TIME:        02:32[CST]|
| NRC NOTIFIED BY:  TIM SMITH                    |LAST UPDATE DATE:  11/05/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED          R3      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       97       Power Operation  |97       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| STEAM GENERATOR BLOWDOWN ISOLATION VALVES CLOSED                             |
|                                                                              |
| At 0232 on 11/05/99 steam generator liquid radiation monitor R-19  failed.   |
| This failure caused the following valves to close: BT-2A/MV-32077, steam     |
| generator blowdown isolation valve A1; BT-2B/MV-32079, steam generator       |
| blowdown isolation valve B1; BT-3A/MV-32078, steam generator blowdown        |
| isolation valve A2; and BT-3B/MV-32080, steam generator blowdown isolation   |
| valve B2.  These valves have a containment isolation function for a main     |
| steam line rupture within containment.  Their post - Loss of Coolant         |
| Accident function is to provide steam generator isolation.                   |
|                                                                              |
| The monitor failure will not allow the re-establishment of steam generator   |
| blowdown flow.  Plant chemistry and instrument and control personnel have    |
| been contacted to determine corrective actions and to repair the radiation   |
| monitor.  Radiation monitor R-15, Air Ejector Exhaust, is indicating normal  |
| readings and is being monitored by operations.  Local indication of          |
| radiation monitor R-19 are the normal count rate. The actual problem appears |
| to be that the Control Room indication for R-19 has failed.                  |
|                                                                              |
| The NRC Resident Inspector was notified of this event by the licensee.       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36402       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DUANE ARNOLD             REGION:  3  |NOTIFICATION DATE: 11/05/1999|
|    UNIT:  [1] [] []                 STATE:  IA |NOTIFICATION TIME: 11:14[EST]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        11/05/1999|
+------------------------------------------------+EVENT TIME:        10:00[CST]|
| NRC NOTIFIED BY:  BOB MURRELL                  |LAST UPDATE DATE:  11/05/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED          R3      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 60% THROUGH WALL CRACK DISCOVERED DURING AN ULTRASONIC EXAMINATION           |
|                                                                              |
| While performing ultrasonic examination of recirculation riser weld RRB-F002 |
| (nozzle to safe-end weld) indications that are indicative of intragranular   |
| stress-corrosion cracking (IGSCC) were identified.  Specifically, a 60%      |
| through wall crack was found on the "B" recirculation riser nozzle to        |
| safe-end weld. This weld was replaced in 1978. The licensee will take review |
| the codes and expand the scope of work as appropriate.                       |
|                                                                              |
| The NRC resident inspector was notified of this event by the licensee.       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36403       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FITZPATRICK              REGION:  1  |NOTIFICATION DATE: 11/05/1999|
|    UNIT:  [1] [] []                 STATE:  NY |NOTIFICATION TIME: 11:51[EST]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        11/05/1999|
+------------------------------------------------+EVENT TIME:        10:51[EST]|
| NRC NOTIFIED BY:  ZAREMBA                      |LAST UPDATE DATE:  11/05/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MOHAMED SHANBAKY     R1      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       85       Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TURBINE TRIP/REACTOR SCRAM ON "1B" MOISTURE SEPARATOR REHEATER HIGH WATER    |
| LEVEL.                                                                       |
|                                                                              |
| Turbine trip resulted in Reactor scram. Turbine trip was a result of a high  |
| level alarm in the "1B" Moisture Separator Reheater.  Just prior to the      |
| turbine trip there appears to have been a level transient in the "4B"        |
| feedwater heater.  All control rods fully inserted into the core. Reactor    |
| Feedwater Pumps tripped on High Reactor Vessel Water Level.  A Reactor       |
| Feedwater Pump was restarted when Reactor Vessel Water level decreased and   |
| is currently maintaining Reactor Vessel Water Level.  The Main Condenser is  |
| being used as the heat sink.  No Emergency Core Cooling Systems started as a |
| result of the turbine trip/Reactor scram.  The offsite electrical grid is    |
| stable, and the Emergency Diesel Generators are fully operable if needed.    |
|                                                                              |
| The Licensee is investigating what caused the level transient in the "4B"    |
| feedwater heater.                                                            |
|                                                                              |
| The NRC Resident Inspector was notified of this event by the licensee.       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36404       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRUNSWICK                REGION:  2  |NOTIFICATION DATE: 11/05/1999|
|    UNIT:  [1] [] []                 STATE:  NC |NOTIFICATION TIME: 13:28[EST]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        11/05/1999|
+------------------------------------------------+EVENT TIME:        10:50[EST]|
| NRC NOTIFIED BY:  MICHAEL WILLIAMS             |LAST UPDATE DATE:  11/05/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |PIERCE SKINNER       R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     M/R        Y       100      Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| Unit 1 was manually scrammed following the unplanned trip of the "1B"        |
| Reactor Feed Pump during monthly surveillance testing.                       |
|                                                                              |
| "On November 5,1999 at 1050 [hours] a manual Reactor Scram was inserted on   |
| Unit 1 after Reactor Feed Pump '1B'  tripped during feed pump testing and    |
| Reactor Water Level was not maintained by the '1A' Reactor Feed Pump.        |
| Primary Containment Groups 2, 6 and 8 Isolations were received following the |
| manual reactor scram from low Reactor Water Level. There is normally a level |
| transient following a reactor scram, which is anticipated by the operating   |
| crew.  Reactor Water Level lowered to 112 inches.  The High Pressure Coolant |
| Injection system was manually started, but was not used for injection.   All |
| required Isolations occurred as a result of the Reactor Water Level Low      |
| Level One initiation signal.  Group 2 isolation valves include Drywell       |
| Equipment and Floor Drain, Traversing Incore Probe, Residual Heat Removal    |
| (RHR) Discharge Isolation to Radwaste and RHR Process Sampling Valves.       |
| Group 6 isolation valves include Containment Atmosphere Control System and   |
| Post Accident Valves.  Group 8 isolation valves include RHR System Shutdown  |
| Cooling Isolation Valves, these valves were closed prior to the isolation    |
| sign.                                                                        |
|                                                                              |
| "[The initial safety significance is] minimal, all systems functioned as     |
| designed.  The licensee took conservative action to insert a manual Reactor  |
| Scram.                                                                       |
|                                                                              |
| "The cause of the '1B' Reactor Feed Pump trip will be determined and         |
| corrected."                                                                  |
|                                                                              |
| All rods fully inserted.  Decay heat is being removed via the Main           |
| Condenser.  The automatic reactor scram level setpoint is 162 inches with    |
| HPCI injection occurring at 108 inches.                                      |
|                                                                              |
| The licensee informed the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   36405       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  ILLINOIS DEPT OF NUCLEAR SAFETY      |NOTIFICATION DATE: 11/05/1999|
|LICENSEE:                                       |NOTIFICATION TIME: 17:06[EST]|
|    CITY:                           REGION:  3  |EVENT DATE:        11/01/1999|
|  COUNTY:                            STATE:  IL |EVENT TIME:        16:00[CST]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  11/05/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |JAMES CREED          R3      |
|                                                |WAYNE HODGES         NMSS    |
+------------------------------------------------+FRANK CONGEL         IRO     |
| NRC NOTIFIED BY:  BRUCE SANZA                  |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT INVOLVING INDIVIDUAL RECEIVING > 5X ANNUAL LIMIT ON   |
| INTAKE (ALI) OF TRITIUM (INHALATION)                                         |
|                                                                              |
| AT 1645 HOURS ON 11/2/99, THE ILLINOIS DEPARTMENT OF NUCLEAR SAFETY WAS      |
| INFORMED THAT AN INDIVIDUAL HAD SMASHED A TUBE ON 11/1/99 CONTAINING 2       |
| CURIES TRITIUM FROM A  SELF-POWERED EXIT SIGN INSIDE HIS RESIDENTIAL GARAGE. |
| THIS QUANTITY EXCEEDS 5X THE  (ALI) OF 10CFR20 APPENDIX B (1 ALI  INHALATION |
| IS  80 mCi).  THE REMAINING THREE TUBES WERE SAFELY REMOVED FROM THE         |
| INDIVIDUAL'S GARAGE.  THE INDIVIDUAL INITIALLY CONTACTED A POISON HOTLINE    |
| AND WAS REFERRED.  INSPECTORS FROM THE STATE AGENCY HAVE SURVEYED THE GARAGE |
| AND ARE FOLLOWING UP.                                                        |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36406       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SEABROOK                 REGION:  1  |NOTIFICATION DATE: 11/05/1999|
|    UNIT:  [1] [] []                 STATE:  NH |NOTIFICATION TIME: 19:24[EST]|
|   RXTYPE: [1] W-4-LP                           |EVENT DATE:        11/05/1999|
+------------------------------------------------+EVENT TIME:        16:40[EST]|
| NRC NOTIFIED BY:  RICHARD MESSINA              |LAST UPDATE DATE:  11/05/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MOHAMED SHANBAKY     R1      |
|10 CFR SECTION:                                 |                             |
|HFIT 26.73               FITNESS FOR DUTY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24-HOUR FITNESS FOR DUTY REPORT INVOLVING CONTRACTOR SUPERVISOR EMPLOYEE     |
|                                                                              |
| CONTRACTOR SUPERVISOR EMPLOYEE CONFIRMED POSITIVE FOR COCAINE FOLLOWING      |
| RANDOM DRUG TESTING.  THE INDIVIDUAL'S ACCESS HAS BEEN DENIED.  CONTACT THE  |
| HEADQUARTERS OPERATIONS CENTER FOR ADDITIONAL DETAILS.                       |
|                                                                              |
| THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR.                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36407       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: RIVER BEND               REGION:  4  |NOTIFICATION DATE: 11/06/1999|
|    UNIT:  [1] [] []                 STATE:  LA |NOTIFICATION TIME: 09:12[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        11/05/1999|
+------------------------------------------------+EVENT TIME:        15:38[CST]|
| NRC NOTIFIED BY:  RUSS GODWIN                  |LAST UPDATE DATE:  11/06/1999|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CLAUDE JOHNSON       R4      |
|10 CFR SECTION:                                 |                             |
|NCFR                     NON CFR REPORT REQMNT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       90       Power Operation  |90       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24-HOUR REPORT PURSUANT TO REGULATORY GUIDE 1.133                            |
|                                                                              |
| "At 1538 CST, on November 5, 1999, the River Bend Station (RBS) staff        |
| concluded that a loose part had been detected in the primary system.         |
|                                                                              |
| "The RBS staff was alerted to this condition when channel six of the Loose   |
| Parts Monitoring System (LPMS) began to alarm at approximately three to five |
| minute intervals. Channel six monitors the Feedwater 45� line. Over the      |
| remainder of the day, the alarms gradually decreased to none and there is    |
| currently no alarming condition. No other Loose Parts Monitoring channels    |
| detected this condition.                                                     |
|                                                                              |
| "The RBS staff and the LPMS vendor reviewed the data and concluded that the  |
| loose part is of relatively low mass, probably less than two pounds. The RBS |
| staff will continue to evaluate this condition.                              |
|                                                                              |
| "This report is submitted pursuant to Reg. Guide 1.133."                     |
|                                                                              |
| The NRC resident inspector has been informed of this notification by the     |
| licensee.                                                                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36408       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: POINT BEACH              REGION:  3  |NOTIFICATION DATE: 11/06/1999|
|    UNIT:  [1] [2] []                STATE:  WI |NOTIFICATION TIME: 21:46[EST]|
|   RXTYPE: [1] W-2-LP,[2] W-2-LP                |EVENT DATE:        11/06/1999|
+------------------------------------------------+EVENT TIME:        18:44[CST]|
| NRC NOTIFIED BY:  PHILLIP SHORT                |LAST UPDATE DATE:  11/06/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED          R3      |
|10 CFR SECTION:                                 |                             |
|AMED 50.72(b)(2)(v)      OFFSITE MEDICAL        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| INJURED POTENTIALLY CONTAMINATED WORKER TRANSPORTED TO LOCAL HOSPITAL        |
|                                                                              |
| "A WORKER SLIPPED AND FELL IN THE LAUNDRY ROOM.  AN AMBULANCE WAS CALLED DUE |
| TO A POSSIBLE HIP INJURY.  A COMPLETE FRISK OF THE INDIVIDUAL WAS NOT ABLE   |
| TO BE PERFORMED PRIOR TO TRANSPORTING OFFSITE TO A LOCAL HOSPITAL.  THE      |
| INJURED PERSON IS BEING CONSIDERED POTENTIALLY CONTAMINATED.  A RADIATION    |
| PROTECTION TECHNICIAN IS ACCOMPANYING THE INJURED PERSON TO THE HOSPITAL."   |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36409       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PALISADES                REGION:  3  |NOTIFICATION DATE: 11/07/1999|
|    UNIT:  [1] [] []                 STATE:  MI |NOTIFICATION TIME: 11:56[EST]|
|   RXTYPE: [1] CE                               |EVENT DATE:        11/07/1999|
+------------------------------------------------+EVENT TIME:        09:35[EST]|
| NRC NOTIFIED BY:  HUGH NIXON                   |LAST UPDATE DATE:  11/07/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED          R3      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| CONTAINMENT SUMP SCREEN INTEGRITY QUESTIONABLE DURING A DESIGN BASIS         |
| ACCIDENT                                                                     |
|                                                                              |
| "CONTAINMENT SUMP SCREENS (ESS RECIRC) ARE IN A DIFFERENT CONFIGURATION THAN |
| PREVIOUSLY THOUGHT.  THE SCREEN MATERIAL IS NOT WELDED TO THE SCREEN FRAME   |
| FOR AT LEAST ONE THIRD OF IT'S LENGTH.  INSTEAD, THE PERIPHERY OF THE SCREEN |
| IS CLAMPED AT NUMEROUS PLACES MAKING THE SCREEN INTEGRITY QUESTIONABLE IN    |
| THE EVENT OF A DESIGN BASIS ACCIDENT FLOW RATES."                            |
|                                                                              |
| THIS CONDITION, DISCOVERED DURING THE REFUELING INSPECTION OF THE            |
| CONTAINMENT SUMP, MAY HAVE EXISTED SINCE INITIAL CONSTRUCTION.  THE LICENSEE |
| IS PERFORMING FURTHER ANALYSIS TO DETERMINE APPROPRIATE CORRECTIVE ACTIONS   |
| FOR IMPLEMENTATION PRIOR TO RESTART.                                         |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36410       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MONTICELLO               REGION:  3  |NOTIFICATION DATE: 11/07/1999|
|    UNIT:  [1] [] []                 STATE:  MN |NOTIFICATION TIME: 15:19[EST]|
|   RXTYPE: [1] GE-3                             |EVENT DATE:        11/07/1999|
+------------------------------------------------+EVENT TIME:        13:48[CST]|
| NRC NOTIFIED BY:  JIM McKAY                    |LAST UPDATE DATE:  11/07/1999|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES CREED          R3      |
|10 CFR SECTION:                                 |                             |
|AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD  |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM DECLARED INOPERABLE DUE TO     |
| FAILURE OF THE ASSOCIATED ROOM COOLER                                        |
|                                                                              |
| "DURING NORMAL OPERATIONS, HPCI HAS BEEN DECLARED INOPERABLE IN ACCORDANCE   |
| WITH TECH SPEC SECTION 3.5.A.3.g.  HPCI IS INOPERABLE DUE TO THE FAILURE OF  |
| SUPPORT AUXILIARY EQUIPMENT, i.e., THE VENTILATION COOLING COIL HAS A MAJOR  |
| LEAK REQUIRING ISOLATION OF THE VENTILATION UNIT.  HPCI IS IN A 14-DAY       |
| LCO."                                                                        |
|                                                                              |
| THE LICENSEE WILL INFORM  STATE/LOCAL AGENCIES AS A COURTESY AND THE NRC     |
| RESIDENT INSPECTOR.                                                          |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36411       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 11/07/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 22:36[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        11/07/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        04:00[EST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  11/07/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |JAMES CREED          R3      |
|  DOCKET:  0707002                              |                             |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  KURT SISLER                  |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24-HOUR NRC BULLETIN 91-01 NOTIFICATION INVOLVING LOSS OF CRITICALITY        |
| CONTROL (MODERATION)                                                         |
|                                                                              |
| "On 11/7/99 at 0400 hours, it was discovered that the standard solution used |
| to calibrate X-344, Autoclave #2 conductivity system probes on 11/1/99 was   |
| past its shelf life expiration date as stated on the certificate of NIST     |
| traceability. This brings into question the operability (AQ-NCS boundary     |
| item) of the conductivity system. Autoclave #2 was operated in Mode II       |
| (Cylinder Heating) for approximately 30 minutes on 11/2/99. Conductivity     |
| system as-found readings were performed on 11/2/99 with a standard solution  |
| in date according to NIST requirements, The as-found results were within     |
| tolerance indicating that the system would have performed its intended       |
| safety function.                                                             |
|                                                                              |
| "Nuclear Criticality Engineering has determined that the operation of the    |
| autoclave, after calibration of the conductivity system with out-dated       |
| conductivity standard solution, constitutes the loss of one (1) NCS control  |
| (moderation). The other control (Mass) was maintained throughout the         |
| duration of this event. The loss of one NCS control is reportable to the NRC |
| as a 24-hour event.                                                          |
|                                                                              |
| "THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR                      |
| RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT.   |
|                                                                              |
| "SAFETY SIGNIFICANCE OF EVENTS:                                              |
|                                                                              |
| "The safety significance of this event is low. The conductivity probes are   |
| required to be operable and are tested semi-annually to verify this. The     |
| probes were tested on 11/1/99 however, the solution used to calibrate the    |
| probes was out of date. If the probes completely failed a UF6 release in     |
| quantities greater than the minimum critical mass would have to occur or a   |
| slow release could allow a dilute UO(2)F(2) solution to reach unfavorable    |
| geometry storm drains. There was no UF6 release during this event and the    |
| autoclave was only operated for 30 minutes in this condition (As-found       |
| testing with in-date standard on 11/2/99 revealed that the conductivity      |
| system was within allowable tolerance).                                      |
|                                                                              |
| "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW           |
| CRITICALITY COULD OCCUR):                                                    |
|                                                                              |
| "The potential pathway to criticality is that a slow UF6 release occurs      |
| (less than 2 pounds per minute) and the conductivity probes fail to detect   |
| it.  A release with greater than 2 pounds per minute would isolate the       |
| autoclave due to high pressure. This slow release could allow a dilute       |
| solution to reach unfavorable geometry storm drains.                         |
|                                                                              |
| "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.):    |
|                                                                              |
| "The controlled parameters are mass and moderation.                          |
|                                                                              |
| "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS    |
| LIMIT AND % WORST CASE OF CRITICAL MASS):                                    |
|                                                                              |
| "The estimated amount of material is zero because there was no release, the  |
| maximum enrichment is 5% U235 and the form of material is UF6.               |
|                                                                              |
| "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION  |
| OF THE FAILURES OR DEFICIENCIES                                              |
|                                                                              |
| "The control that was lost was moderation. The conductivity probes were      |
| calibrated with a solution that was out of date and therefore the probes     |
| were inoperable. The autoclave was operated for 30 minutes in this           |
| condition.                                                                   |
|                                                                              |
| "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED:  |
|                                                                              |
| "As found readings were completed with an in-date batch of conductivity      |
| standard solution. All as-found readings were in acceptable limits.          |
| Autoclave #2 is inoperable (since 11/4/99) for reasons other than this       |
| event."                                                                      |
|                                                                              |
| The standard solution used to calibrate the conductivity system expired on   |
| 10/12/99.  Operations has the cause for this incident report under review;   |
| however, the preliminary investigation attributes the failure to personnel   |
| error.                                                                       |
|                                                                              |
| The NRC Resident Inspector was informed.                                     |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021