Event Notification Report for November 8, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/05/1999 - 11/08/1999 ** EVENT NUMBERS ** 36287 36364 36400 36401 36402 36403 36404 36405 36406 36407 36408 36409 36410 36411 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36287 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 10/13/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 16:00[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 10/13/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 00:10[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/05/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |JOHN MADERA R3 | | DOCKET: 0707001 |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WALKER | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | At 0010 on 10/13/99, the PSS office was notified that a primary condensate | | alarm was received on the C-360 position 4 autoclave Water Inventory Control | | System (WICS). The WICS system is required to be operable while heating in | | mode 5 according to TSR 21.4.3. The autoclave was checked according to the | | alarm response procedure and subsequently removed from service and declared | | inoperable by the Plant Shift Superintendent. | | Troubleshooting was initiated and is continuing in order to determine the | | reason for the alarm. | | | | The NRC senior resident has been notified of this event. | | | | * * * UPDATE 2220EST ON 11/5/99 FROM E.G. WALKER TO S. SANDIN * * * | | | | "On 11/2/99, the same type of actuation occurred on the C-360 autoclave No. | | 1 while out of service and open. While investigating this invalid actuation, | | it was discovered that the gain adjustment on one of the WICS channels had | | drifted out of tolerance. Discussions with the component manufacturer | | concluded that the WICS alarm cards are susceptible to drift due to age and | | fluctuations in temperature. These cards are exposed to ambient | | temperatures, but the cards are rated for the range of temperatures at the | | autoclaves. Given this and other indications that the WICS actuation | | signals were invalid, i.e., not the result of water backing up in the drain, | | it has been concluded that the subject actuation on 10/13/99 was caused by | | [an] invalid signal (instrument drift) and thus does not meet the criteria | | for reporting and should be retracted." | | | | The NRC resident has been notified of this retraction. Notified | | R3DO(Creed). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36364 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 10/28/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 16:16[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 10/27/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 17:05[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/05/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |MIKE JORDAN R3 | | DOCKET: 0707001 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: W.F. CAGE | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | Safety System Actuation | | | | At 1705 CDT on 10/27/99, the Plant Shift Superintendent's (PSS) office was | | notified that a primary condensate alarm was received on the C-360 position | | 2 autoclave Water Inventory Control (WIC) System. The WIC system is | | required to be operable while heating in mode 5 according to TSR 2.1.4.3. | | The autoclave was checked according to the alarm response procedure, removed | | from service and declared inoperable by the PSS. Troubleshooting was | | initiated and is continuing in order to determine the reason for the alarm. | | | | The safety system actuation is reportable to the NRC as required by Safety | | Analysis Report, section 6.9, table 1 criteria J.2, Safety System actuation | | due to a valid signal as a 24-hour event notification. | | | | The NRC resident inspector has been notified. | | | | * * * UPDATE 2220EST ON 11/5/99 FROM E.G. WALKER TO S. SANDIN * * * | | | | "On 11/2/99, the same type of actuation occurred on the C-360 autoclave No. | | 1 while out of service and open. While investigating this invalid actuation, | | it was discovered that the gain adjustment on one of the WICS channels had | | drifted out of tolerance. Discussions with the component manufacturer | | concluded that the WICS alarm cards are susceptible to drift due to age and | | fluctuations in temperature. These cards are exposed to ambient | | temperatures, but the cards are rated for the range of temperatures at the | | autoclaves. Given this and other indications that the WICS actuation | | signals were invalid, i.e., not the result of water backing up in the drain, | | it has been concluded that the subject actuation on 10/27/99 was caused by | | [an] invalid signal (instrument drift) and thus does not meet the criteria | | for reporting and should be retracted." | | | | The NRC resident inspector has been notified of this retraction. Notified | | R3DO(Creed). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36400 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 11/05/1999| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 04:07[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 11/04/1999| +------------------------------------------------+EVENT TIME: 20:30[CST]| | NRC NOTIFIED BY: RICK ROBBINS |LAST UPDATE DATE: 11/05/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 0.25 INCH LONG CRACK WAS FOUND ON "1A" STEAM GENERATOR HEAD DRAIN VALVE. | | | | During a liquid penetrant examination of a weld on the top side of valve | | 1R-526A, the '1A' Steam Generator head drain, a 0.25" long crack was found. | | This appears to be a crack in the weld metal only, through wall of the | | Reactor Coolant System pressure boundary. | | | | During initial screening of this condition at 2030 hours on 11/04/99 it was | | not considered seriously degraded as no leak was detected while at power | | (boric acid crystals were found in the vicinity of the valve). Upon further | | review at 0200 hours on 11/05/99 this 4 hour non-emergency report was made. | | | | The NRC Resident Inspector will be notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36401 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 11/05/1999| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 05:21[EST]| | RXTYPE: [1] W-2-LP |EVENT DATE: 11/05/1999| +------------------------------------------------+EVENT TIME: 02:32[CST]| | NRC NOTIFIED BY: TIM SMITH |LAST UPDATE DATE: 11/05/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 97 Power Operation |97 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STEAM GENERATOR BLOWDOWN ISOLATION VALVES CLOSED | | | | At 0232 on 11/05/99 steam generator liquid radiation monitor R-19 failed. | | This failure caused the following valves to close: BT-2A/MV-32077, steam | | generator blowdown isolation valve A1; BT-2B/MV-32079, steam generator | | blowdown isolation valve B1; BT-3A/MV-32078, steam generator blowdown | | isolation valve A2; and BT-3B/MV-32080, steam generator blowdown isolation | | valve B2. These valves have a containment isolation function for a main | | steam line rupture within containment. Their post - Loss of Coolant | | Accident function is to provide steam generator isolation. | | | | The monitor failure will not allow the re-establishment of steam generator | | blowdown flow. Plant chemistry and instrument and control personnel have | | been contacted to determine corrective actions and to repair the radiation | | monitor. Radiation monitor R-15, Air Ejector Exhaust, is indicating normal | | readings and is being monitored by operations. Local indication of | | radiation monitor R-19 are the normal count rate. The actual problem appears | | to be that the Control Room indication for R-19 has failed. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36402 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 11/05/1999| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 11:14[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 11/05/1999| +------------------------------------------------+EVENT TIME: 10:00[CST]| | NRC NOTIFIED BY: BOB MURRELL |LAST UPDATE DATE: 11/05/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 60% THROUGH WALL CRACK DISCOVERED DURING AN ULTRASONIC EXAMINATION | | | | While performing ultrasonic examination of recirculation riser weld RRB-F002 | | (nozzle to safe-end weld) indications that are indicative of intragranular | | stress-corrosion cracking (IGSCC) were identified. Specifically, a 60% | | through wall crack was found on the "B" recirculation riser nozzle to | | safe-end weld. This weld was replaced in 1978. The licensee will take review | | the codes and expand the scope of work as appropriate. | | | | The NRC resident inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36403 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 11/05/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 11:51[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 11/05/1999| +------------------------------------------------+EVENT TIME: 10:51[EST]| | NRC NOTIFIED BY: ZAREMBA |LAST UPDATE DATE: 11/05/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 85 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TURBINE TRIP/REACTOR SCRAM ON "1B" MOISTURE SEPARATOR REHEATER HIGH WATER | | LEVEL. | | | | Turbine trip resulted in Reactor scram. Turbine trip was a result of a high | | level alarm in the "1B" Moisture Separator Reheater. Just prior to the | | turbine trip there appears to have been a level transient in the "4B" | | feedwater heater. All control rods fully inserted into the core. Reactor | | Feedwater Pumps tripped on High Reactor Vessel Water Level. A Reactor | | Feedwater Pump was restarted when Reactor Vessel Water level decreased and | | is currently maintaining Reactor Vessel Water Level. The Main Condenser is | | being used as the heat sink. No Emergency Core Cooling Systems started as a | | result of the turbine trip/Reactor scram. The offsite electrical grid is | | stable, and the Emergency Diesel Generators are fully operable if needed. | | | | The Licensee is investigating what caused the level transient in the "4B" | | feedwater heater. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36404 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 11/05/1999| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 13:28[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 11/05/1999| +------------------------------------------------+EVENT TIME: 10:50[EST]| | NRC NOTIFIED BY: MICHAEL WILLIAMS |LAST UPDATE DATE: 11/05/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PIERCE SKINNER R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | Unit 1 was manually scrammed following the unplanned trip of the "1B" | | Reactor Feed Pump during monthly surveillance testing. | | | | "On November 5,1999 at 1050 [hours] a manual Reactor Scram was inserted on | | Unit 1 after Reactor Feed Pump '1B' tripped during feed pump testing and | | Reactor Water Level was not maintained by the '1A' Reactor Feed Pump. | | Primary Containment Groups 2, 6 and 8 Isolations were received following the | | manual reactor scram from low Reactor Water Level. There is normally a level | | transient following a reactor scram, which is anticipated by the operating | | crew. Reactor Water Level lowered to 112 inches. The High Pressure Coolant | | Injection system was manually started, but was not used for injection. All | | required Isolations occurred as a result of the Reactor Water Level Low | | Level One initiation signal. Group 2 isolation valves include Drywell | | Equipment and Floor Drain, Traversing Incore Probe, Residual Heat Removal | | (RHR) Discharge Isolation to Radwaste and RHR Process Sampling Valves. | | Group 6 isolation valves include Containment Atmosphere Control System and | | Post Accident Valves. Group 8 isolation valves include RHR System Shutdown | | Cooling Isolation Valves, these valves were closed prior to the isolation | | sign. | | | | "[The initial safety significance is] minimal, all systems functioned as | | designed. The licensee took conservative action to insert a manual Reactor | | Scram. | | | | "The cause of the '1B' Reactor Feed Pump trip will be determined and | | corrected." | | | | All rods fully inserted. Decay heat is being removed via the Main | | Condenser. The automatic reactor scram level setpoint is 162 inches with | | HPCI injection occurring at 108 inches. | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36405 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ILLINOIS DEPT OF NUCLEAR SAFETY |NOTIFICATION DATE: 11/05/1999| |LICENSEE: |NOTIFICATION TIME: 17:06[EST]| | CITY: REGION: 3 |EVENT DATE: 11/01/1999| | COUNTY: STATE: IL |EVENT TIME: 16:00[CST]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 11/05/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JAMES CREED R3 | | |WAYNE HODGES NMSS | +------------------------------------------------+FRANK CONGEL IRO | | NRC NOTIFIED BY: BRUCE SANZA | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING INDIVIDUAL RECEIVING > 5X ANNUAL LIMIT ON | | INTAKE (ALI) OF TRITIUM (INHALATION) | | | | AT 1645 HOURS ON 11/2/99, THE ILLINOIS DEPARTMENT OF NUCLEAR SAFETY WAS | | INFORMED THAT AN INDIVIDUAL HAD SMASHED A TUBE ON 11/1/99 CONTAINING 2 | | CURIES TRITIUM FROM A SELF-POWERED EXIT SIGN INSIDE HIS RESIDENTIAL GARAGE. | | THIS QUANTITY EXCEEDS 5X THE (ALI) OF 10CFR20 APPENDIX B (1 ALI INHALATION | | IS 80 mCi). THE REMAINING THREE TUBES WERE SAFELY REMOVED FROM THE | | INDIVIDUAL'S GARAGE. THE INDIVIDUAL INITIALLY CONTACTED A POISON HOTLINE | | AND WAS REFERRED. INSPECTORS FROM THE STATE AGENCY HAVE SURVEYED THE GARAGE | | AND ARE FOLLOWING UP. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36406 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 11/05/1999| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 19:24[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 11/05/1999| +------------------------------------------------+EVENT TIME: 16:40[EST]| | NRC NOTIFIED BY: RICHARD MESSINA |LAST UPDATE DATE: 11/05/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR FITNESS FOR DUTY REPORT INVOLVING CONTRACTOR SUPERVISOR EMPLOYEE | | | | CONTRACTOR SUPERVISOR EMPLOYEE CONFIRMED POSITIVE FOR COCAINE FOLLOWING | | RANDOM DRUG TESTING. THE INDIVIDUAL'S ACCESS HAS BEEN DENIED. CONTACT THE | | HEADQUARTERS OPERATIONS CENTER FOR ADDITIONAL DETAILS. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36407 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 11/06/1999| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 09:12[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 11/05/1999| +------------------------------------------------+EVENT TIME: 15:38[CST]| | NRC NOTIFIED BY: RUSS GODWIN |LAST UPDATE DATE: 11/06/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLAUDE JOHNSON R4 | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 90 Power Operation |90 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR REPORT PURSUANT TO REGULATORY GUIDE 1.133 | | | | "At 1538 CST, on November 5, 1999, the River Bend Station (RBS) staff | | concluded that a loose part had been detected in the primary system. | | | | "The RBS staff was alerted to this condition when channel six of the Loose | | Parts Monitoring System (LPMS) began to alarm at approximately three to five | | minute intervals. Channel six monitors the Feedwater 45� line. Over the | | remainder of the day, the alarms gradually decreased to none and there is | | currently no alarming condition. No other Loose Parts Monitoring channels | | detected this condition. | | | | "The RBS staff and the LPMS vendor reviewed the data and concluded that the | | loose part is of relatively low mass, probably less than two pounds. The RBS | | staff will continue to evaluate this condition. | | | | "This report is submitted pursuant to Reg. Guide 1.133." | | | | The NRC resident inspector has been informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36408 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 11/06/1999| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 21:46[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 11/06/1999| +------------------------------------------------+EVENT TIME: 18:44[CST]| | NRC NOTIFIED BY: PHILLIP SHORT |LAST UPDATE DATE: 11/06/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |AMED 50.72(b)(2)(v) OFFSITE MEDICAL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INJURED POTENTIALLY CONTAMINATED WORKER TRANSPORTED TO LOCAL HOSPITAL | | | | "A WORKER SLIPPED AND FELL IN THE LAUNDRY ROOM. AN AMBULANCE WAS CALLED DUE | | TO A POSSIBLE HIP INJURY. A COMPLETE FRISK OF THE INDIVIDUAL WAS NOT ABLE | | TO BE PERFORMED PRIOR TO TRANSPORTING OFFSITE TO A LOCAL HOSPITAL. THE | | INJURED PERSON IS BEING CONSIDERED POTENTIALLY CONTAMINATED. A RADIATION | | PROTECTION TECHNICIAN IS ACCOMPANYING THE INJURED PERSON TO THE HOSPITAL." | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36409 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALISADES REGION: 3 |NOTIFICATION DATE: 11/07/1999| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 11:56[EST]| | RXTYPE: [1] CE |EVENT DATE: 11/07/1999| +------------------------------------------------+EVENT TIME: 09:35[EST]| | NRC NOTIFIED BY: HUGH NIXON |LAST UPDATE DATE: 11/07/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTAINMENT SUMP SCREEN INTEGRITY QUESTIONABLE DURING A DESIGN BASIS | | ACCIDENT | | | | "CONTAINMENT SUMP SCREENS (ESS RECIRC) ARE IN A DIFFERENT CONFIGURATION THAN | | PREVIOUSLY THOUGHT. THE SCREEN MATERIAL IS NOT WELDED TO THE SCREEN FRAME | | FOR AT LEAST ONE THIRD OF IT'S LENGTH. INSTEAD, THE PERIPHERY OF THE SCREEN | | IS CLAMPED AT NUMEROUS PLACES MAKING THE SCREEN INTEGRITY QUESTIONABLE IN | | THE EVENT OF A DESIGN BASIS ACCIDENT FLOW RATES." | | | | THIS CONDITION, DISCOVERED DURING THE REFUELING INSPECTION OF THE | | CONTAINMENT SUMP, MAY HAVE EXISTED SINCE INITIAL CONSTRUCTION. THE LICENSEE | | IS PERFORMING FURTHER ANALYSIS TO DETERMINE APPROPRIATE CORRECTIVE ACTIONS | | FOR IMPLEMENTATION PRIOR TO RESTART. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36410 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 11/07/1999| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 15:19[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 11/07/1999| +------------------------------------------------+EVENT TIME: 13:48[CST]| | NRC NOTIFIED BY: JIM McKAY |LAST UPDATE DATE: 11/07/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM DECLARED INOPERABLE DUE TO | | FAILURE OF THE ASSOCIATED ROOM COOLER | | | | "DURING NORMAL OPERATIONS, HPCI HAS BEEN DECLARED INOPERABLE IN ACCORDANCE | | WITH TECH SPEC SECTION 3.5.A.3.g. HPCI IS INOPERABLE DUE TO THE FAILURE OF | | SUPPORT AUXILIARY EQUIPMENT, i.e., THE VENTILATION COOLING COIL HAS A MAJOR | | LEAK REQUIRING ISOLATION OF THE VENTILATION UNIT. HPCI IS IN A 14-DAY | | LCO." | | | | THE LICENSEE WILL INFORM STATE/LOCAL AGENCIES AS A COURTESY AND THE NRC | | RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36411 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 11/07/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 22:36[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 11/07/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 04:00[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/07/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |JAMES CREED R3 | | DOCKET: 0707002 | | +------------------------------------------------+ | | NRC NOTIFIED BY: KURT SISLER | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 NOTIFICATION INVOLVING LOSS OF CRITICALITY | | CONTROL (MODERATION) | | | | "On 11/7/99 at 0400 hours, it was discovered that the standard solution used | | to calibrate X-344, Autoclave #2 conductivity system probes on 11/1/99 was | | past its shelf life expiration date as stated on the certificate of NIST | | traceability. This brings into question the operability (AQ-NCS boundary | | item) of the conductivity system. Autoclave #2 was operated in Mode II | | (Cylinder Heating) for approximately 30 minutes on 11/2/99. Conductivity | | system as-found readings were performed on 11/2/99 with a standard solution | | in date according to NIST requirements, The as-found results were within | | tolerance indicating that the system would have performed its intended | | safety function. | | | | "Nuclear Criticality Engineering has determined that the operation of the | | autoclave, after calibration of the conductivity system with out-dated | | conductivity standard solution, constitutes the loss of one (1) NCS control | | (moderation). The other control (Mass) was maintained throughout the | | duration of this event. The loss of one NCS control is reportable to the NRC | | as a 24-hour event. | | | | "THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. | | | | "SAFETY SIGNIFICANCE OF EVENTS: | | | | "The safety significance of this event is low. The conductivity probes are | | required to be operable and are tested semi-annually to verify this. The | | probes were tested on 11/1/99 however, the solution used to calibrate the | | probes was out of date. If the probes completely failed a UF6 release in | | quantities greater than the minimum critical mass would have to occur or a | | slow release could allow a dilute UO(2)F(2) solution to reach unfavorable | | geometry storm drains. There was no UF6 release during this event and the | | autoclave was only operated for 30 minutes in this condition (As-found | | testing with in-date standard on 11/2/99 revealed that the conductivity | | system was within allowable tolerance). | | | | "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | | | "The potential pathway to criticality is that a slow UF6 release occurs | | (less than 2 pounds per minute) and the conductivity probes fail to detect | | it. A release with greater than 2 pounds per minute would isolate the | | autoclave due to high pressure. This slow release could allow a dilute | | solution to reach unfavorable geometry storm drains. | | | | "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | | | "The controlled parameters are mass and moderation. | | | | "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | | | "The estimated amount of material is zero because there was no release, the | | maximum enrichment is 5% U235 and the form of material is UF6. | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES | | | | "The control that was lost was moderation. The conductivity probes were | | calibrated with a solution that was out of date and therefore the probes | | were inoperable. The autoclave was operated for 30 minutes in this | | condition. | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | | | "As found readings were completed with an in-date batch of conductivity | | standard solution. All as-found readings were in acceptable limits. | | Autoclave #2 is inoperable (since 11/4/99) for reasons other than this | | event." | | | | The standard solution used to calibrate the conductivity system expired on | | 10/12/99. Operations has the cause for this incident report under review; | | however, the preliminary investigation attributes the failure to personnel | | error. | | | | The NRC Resident Inspector was informed. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021