Event Notification Report for November 4, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/03/1999 - 11/04/1999 ** EVENT NUMBERS ** 36303 36385 36390 36391 36392 36393 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36303 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 10/17/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 14:24[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 10/17/1999| +------------------------------------------------+EVENT TIME: 13:32[EDT]| | NRC NOTIFIED BY: ED HYNE |LAST UPDATE DATE: 11/03/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INTEGRATED LEAK TEST FAILURE IN THE REACTOR BUILDING CLOSED COOLING WATER | | SYSTEM | | | | "Failure of IST [Integrated System Test] testing for RBCLC [reactor building | | closed loop cooling] containment isolation AOVs resulted in performance of | | 'as-found' Type-C LLRT. Results of local leak test was 'gross' failure. | | The failure was determined from inability to obtain test pressure and | | quantify leakage. Based on these results, it is assumed Tech Spec allowable | | containment leakage has been exceeded." | | | | The plant will remain shutdown until repairs are made. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE AT 1422 ON 11/03/99 BY MARK ABRANSKI TO JOLLIFFE * * * | | | | The licensee desires to retract this event for the following rational: | | | | The RBCLC piping forms a closed loop inside containment which serves as a | | redundant containment isolation barrier in the event an RBCLC containment | | isolation valve fails. Therefore, it need not be assumed that Tech Spec | | allowable leakage had been exceeded as reported above. | | | | The licensee notified the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R1DO Mohamed Shanbaky. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36385 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALISADES REGION: 3 |NOTIFICATION DATE: 11/02/1999| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 11:45[EST]| | RXTYPE: [1] CE |EVENT DATE: 11/02/1999| +------------------------------------------------+EVENT TIME: 09:00[EST]| | NRC NOTIFIED BY: BOB VINCENT |LAST UPDATE DATE: 11/03/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - INDICATIONS DISCOVERED ON CONTROL ROD DRIVE SEAL HOUSINGS - | | | | At 0900 on 11/02/99, a dye penetrant (PT) examination of the control rod | | drive seal housing for control rod #44 revealed a potential crack-like | | indication in the Reactor Coolant System pressure boundary. The PT | | examination was performed to investigate a boric acid deposit on the | | exterior surface of the housing which was discovered during a previous | | visual inspection. A small indication was also found on the seal housing | | for control rod #30. The plant is in a refueling outage. An investigation | | to characterize the indications and determine their cause and extent is in | | progress. This situation will be resolved prior to plant restart. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE AT 1432 ON 11/03/99 BY HUGH NIXON TO JOLLIFFE * * * | | | | At 1215 on 11/03/99, a PT examination revealed a circumferential indication | | on the seal housing for control rod #26. | | | | The licensee notified the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R3DO Jim Creed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36390 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 11/03/1999| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 13:10[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 11/03/1999| +------------------------------------------------+EVENT TIME: 13:00[EST]| | NRC NOTIFIED BY: JOHN LAMB |LAST UPDATE DATE: 11/03/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 99 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - FOUR OF SIXTEEN OFFSITE EMERGENCY SIRENS INOPERABLE AND BEING REPAIRED - | | | | Four of 16 offsite emergency sirens in Harriman State Park, Orange County, | | NY, are inoperable due to the loss of an electrical line to the park during | | a thunderstorm. The line is being repaired. | | | | The licensee plans to notify the NRC Resident Inspector. | | | | Refer to identical Event #36391 for Unit 3. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36391 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 11/03/1999| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 13:51[EST]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 11/03/1999| +------------------------------------------------+EVENT TIME: 13:15[EST]| | NRC NOTIFIED BY: STEVE DAVIS |LAST UPDATE DATE: 11/03/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - FOUR OF SIXTEEN OFFSITE EMERGENCY SIRENS INOPERABLE AND BEING REPAIRED - | | | | Four of 16 offsite emergency sirens in Harriman State Park, Orange County, | | NY, are inoperable due to the loss of an electrical line to the park during | | a thunderstorm. The line is being repaired. | | | | The licensee notified the NRC Resident Inspector. | | | | Refer to identical Event # 36390 for Unit 2. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36392 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 11/03/1999| | UNIT: [] [] [3] STATE: SC |NOTIFICATION TIME: 15:09[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 11/03/1999| +------------------------------------------------+EVENT TIME: 02:30[EST]| | NRC NOTIFIED BY: RANDY TODD |LAST UPDATE DATE: 11/03/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Low Pressure Injection System removed from Engineered Safeguards alignment | | due to erroneous procedure - | | | | At 0230 on 11/03/99, both trains of the Low Pressure Injection (LPI) System | | were removed from their normal Engineered Safeguards (ES) alignment due to | | an erroneous procedure. Approximately 20 minutes later, the proper ES | | alignment was restored after the operators questioned the valve position | | specified by the procedure. | | | | Although this event was terminated at approximately 0250 on 11/03/99, the | | potential impact on system operability remained in question. Engineering | | was notified and began evaluating operability. This included discussions | | with Operations as to expected actions, alarm responses, etc. It was | | concluded that operability could not be assured without a detailed analysis. | | At 1330 on 11/03/99, Engineering and Operations concluded that there was no | | longer "reasonable expectation" of past operability. Pending the results of | | a full evaluation by Engineering, Duke Power decided that this was | | potentially a "Condition that alone could have prevented the fulfillment of | | the safety function...to...mitigate the consequences of an accident." | | Therefore, this event is considered reportable. | | | | Impact on Postulated Accident: | | The valves that were opened were #3LP-92 and #3LP-93, the train 'A' and 'B' | | Decay Heat Cooler Bypass Valves. As a result of the alignment, flow | | immediately after an accident could have been higher than expected. This | | could affect the available NPSH to the LPI and Reactor Building Spray (RBS) | | System pumps. Per the Emergency Operating Procedure, operators would have | | throttled the cooler outlet valves to establish the desired total flow. | | | | Later in the scenario, the Borated Water Storage Tank inventory would be | | depleted and operators would realign the LPI and RBS suctions to the Reactor | | Building Emergency Sump. Also, Low Pressure Service Water would be aligned | | to the decay heat coolers to cool the sump water. With #3LP-92 and #3LP-93 | | open, a large portion of the LPI System flow would bypass the coolers, | | resulting in cooling flow at higher temperatures than expected. Inadequate | | core cooling might result until the inappropriate alignment could be | | diagnosed and corrected. | | | | Cause: | | Operators were performing a periodic procedure "Tech Spec Flow Path | | Verification" which had recently been changed to include additional valves. | | They repositioned two of the newly added valves to "OPEN" as directed by the | | procedure. Subsequently, they questioned this action and verified from | | other procedures that the proper position for these valves is "CLOSED". The | | valves were reclosed within approximately 20 minutes. | | | | The root cause for the inaccurate procedure change will be investigated. | | | | Corrective action: | | The proper positions of the valves were questioned and the valves were | | returned to the original positions, thus ending the event. | | | | Because the impact on operability of the affected systems was not | | immediately apparent, and it did not become apparent until well after the | | termination of the event, no Tech Spec Action Statements were entered. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36393 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 11/03/1999| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 17:02[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 10/19/1999| +------------------------------------------------+EVENT TIME: 17:20[CDT]| | NRC NOTIFIED BY: DUANE BISTODEAU |LAST UPDATE DATE: 11/03/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - REACTOR CORE ISOLATION COOLING SYSTEM INOPERABLE FOR EIGHT DAYS - | | | | At 1720 CDT on 10/19/99, the Reactor Core Isolation Cooling (RCIC) System | | was removed from service for a surveillance test and corrective maintenance. | | During post maintenance testing following corrective maintenance, a problem | | was identified that may have made the RCIC System inoperable. Subsequently, | | the RCIC System was repaired, tested, returned to service and operable | | status at 0135 CDT on 10/27/99. This event was originally determined to be | | not reportable to the NRC. However, at 1500 CST on 11/03/99, plant | | management decided to report this event to the NRC. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021