Event Notification Report for November 3, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/02/1999 - 11/03/1999 ** EVENT NUMBERS ** 35790 36385 36386 36387 36388 36389 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35790 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/03/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:44[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/02/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:30[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 11/02/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |DAVID HILLS R3 | | DOCKET: 0707001 |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: THOMAS WHITE | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THREE SPRINKLER SYSTEMS DECLARED INOPERABLE DUE TO CORRODED HEADS (24-hour | | report) | | | | "On 06/02/99 at 1630 CDT, the Plant Shift Superintendent (PSS) was notified | | that numerous sprinkler heads were corroded, affecting 16 sprinkler systems | | in C-337 and one system in C-333, such that the ability of the sprinklers to | | flow sufficient water was called into question. Subsequently, these | | sprinkler systems were declared inoperable, and TSR-required actions | | establishing roving fire patrols were initiated. This deficiency was | | detected during scheduled system inspections conducted by Fire Protection | | personnel. Currently, functionality of the sprinkler heads has not been | | fully evaluated by Fire Protection personnel, and the remaining cascade | | buildings are currently being inspected, and if necessary, this report will | | be updated to identify any additional areas. It has been determined that | | this event is reportable under 10CFR76.120(c)(2) as an event in which | | equipment is disabled or fails to function as designed." The NRC resident | | inspector has been notified of this event. | | | | * * * UPDATE AT 1022 EDT ON 06/04/99 FROM CAGE TO TROCINE * * * | | | | "Two sprinkler heads on system D-1 in C-337 and two sprinkler heads on | | system 27 in C-335 were identified to also be corroded. These were | | identified to the PSS on 06/03/99 at 1600 CDT and 1601 CDT, respectively, | | and determined to require an update to this report by the PSS. It has been | | determined that this event is reportable under 10CFR76.120(c)(2) as an event | | in which equipment is disabled or fails to function as designed." Paducah | | personnel notified the NRC resident inspector of this update. The NRC | | operations officer notified the R3DO (Hills) and NMSS EO (Combs). | | | | * * * UPDATE AT 2152 EDT ON 06/17/99 FROM WALKER TO POERTNER * * * | | | | "Three sprinkler heads on system C-15 and five sprinkler heads on system B-8 | | in C-333 were identified to also be corroded. The PSS was notified of this | | condition at 1300 CDT on 06/17/99 and determined that an update to this | | report was required. It has been determined that this event is reportable | | under 10CFR76.120(c)(2) as an event in which equipment is disabled or fails | | to function as designed." Paducah personnel notified the NRC resident | | inspector of this update. The NRC operations officer notified the R3DO | | (Madera). | | | | * * * UPDATE 1440 EDT 6/18/1999 FROM UNDERWOOD TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on system C-15 and one sprinkler head on system B-8 in | | C-333 were identified to have corrosion. The PSS was notified of this | | condition at 1350 CDT on 06/18/99. The area of the fire patrol for system | | C-15 was expanded to include the two heads identified as corroded. The one | | head on system B-8 was in the area already being patrolled. The PSS | | determined that an update to this report was required." The NRC resident | | inspector has been informed of this update. Notified R3DO (Madera). | | | | * * * UPDATE 1315 EDT 6/25/1999 FROM WALKER TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on system D-8 and three sprinkler heads on system D-7 | | in C-337 were identified to have corrosion. The PSS was notified of the | | condition on system D-8 at 0125 CDT on 06/25/99 and at 1019 CDT on 06/25/99 | | for system D-7. Both systems were immediately declared inoperable and LCO | | fire patrol actions were implemented. It was determined that an update to | | this report was required." The NRC resident inspector has been informed of | | this update. Notified R3DO (Jordan). | | | | * * * UPDATE 2119 EDT 7/30/1999 FROM CAGE TAKEN BY STRANSKY * * * | | | | "Five sprinkler heads and one sprinkler piping tee on C-337 system D-7 were | | identified to have corrosion. The PSS was notified of these corroded system | | parts and declared the system inoperable at 0931 CDT on 07/30/99. LCO | | required fire patrols of the affected area were initiated. The PSS | | determined that an update to this event report was required." The NRC | | resident inspector has been informed of this update. Notified R3DO | | (Wright). | | | | * * * UPDATE AT 1655 EDT ON 07/31/99 FROM WHITE TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on C-337 System D-1 were identified to have corrosion. | | The PSS was notified of these corroded system parts and declared the system | | inoperable at 1155 CDT on 7/31/99. LCO required fire patrols of the | | affected area were initiated. The PSS determined that an update to this | | report was required." The NRC resident inspector has been informed of this | | update. Notified R3DO (Wright). | | | | * * * UPDATE AT 1546 EDT ON 08/10/99 FROM WHITE TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on C-337 system C-15 were identified to have corrosion. | | The PSS was notified of these corroded system parts and declared the system | | inoperable at 1130 CDT on 8/10/99. LCO required fire patrols of the | | affected area were initiated. The PSS determined that an update to this | | report was required." The NRC resident inspector has been informed of this | | update. Notified R3DO (Burgess). | | | | * * * UPDATE AT 1154 EDT ON 08/22/99 FROM WALKER TO POERTNER * * * | | | | Four adjacent sprinkler heads on the C-333 building System B-1 were | | identified to have corrosion. The PSS was notified of the corroded system | | parts and declared the system inoperable at 0918 CDT on 08/22/99. LCO | | required fire patrols were initiated. The NRC Resident Inspector will be | | notified. The NRC Operations Officer notified the R3DO (Clayton). | | | | * * * UPDATE 2015 EDT ON 08/28/99 FROM W. F. GAGE TO S. SANDIN * * * | | | | Two adjacent sprinkler heads on the C-337 building System D-11 were | | identified to have corrosion. The PSS was notified of these corroded system | | parts and declared the system inoperable at 1420 CDT on 08/28/99. LCO | | required fire patrols of the affected area were initiated. Paducah | | personnel informed the NRC Resident Inspector. The NRC Operations Officer | | notified the R3DO (Leach) and NMSS EO (Piccone). | | | | * * * UPDATE 2037 EDT ON 08/29/99 FROM KEVIN BEASLEY TO S. SANDIN * * * | | | | Two adjacent sprinkler heads on the C-337 building System D-15 were | | identified to have corrosion and the PSS declared the system inoperable at | | 0925 CDT on 08/29/99. Also two adjacent heads on the C-337 building System | | D-10 were identified to have corrosion and the PSS declared the system | | inoperable at 1450 CDT. LCO required fire patrols for both of the affected | | areas were initiated in the time frame required by TSR. Paducah personnel | | informed the NRC Resident Inspector. The NRC Operations Officer notified | | the R3DO (Leach) and NMSS EO (Piccone). | | | | * * * UPDATE AT 0930 EDT ON 09/01/99 BY ERIC WALKER TO FANGIE JONES * * * | | | | Add two adjacent sprinkler heads on the C-337 building System D-14 were | | declared inoperable. Paducah personnel informed the NRC Resident Inspector. | | The NRC Operations Officer notified the R3DO (David Hills) and NMSS (Robert | | Pierson). | | | | * * * UPDATE AT 1133 EDT ON 09/08/99 BY TOM WHITE TO FANGIE JONES * * * | | | | Add two adjacent sprinkler heads on the C-331 building System 26 were | | declared inoperable at 2155 CDT on 09/07/99. An LCO required fire patrol | | for the affected area was initiated in the time frame required by the TSR. | | Paducah personnel informed the NRC Resident Inspector. The NRC Operations | | Officer notified the R3DO (Monte Phillips) and NMSS (Josie Piccone). | | | | * * * UPDATE AT 0948 ON 09/30/99 BY ERIC WALKER TO DOUG WEAVER * * * | | | | Add two adjacent sprinkler heads on the C-333 building System B-15 were | | identified to have corrosion and the PSS declared the system inoperable at | | 0815 CDT on 9/30/99. An LCO required fire patrol for the affected area was | | initiated in the time frame required by the TSR. Paducah personnel informed | | the NRC Resident Inspector. The NRC operations officer notified the R3DO | | (Vegel) and NMSS (Cool). | | | | * * * UPDATE AT 1600 ON 10/13/99 BY WALKER TO GOULD * * * | | | | Two adjacent sprinkler heads on the C-333 building System A-11 were | | Identified to have corrosion and the PSS declared the system inoperable at | | 1307 CDT on 10/13/99. An LCO required fire patrol for the affected area was | | initiated in the time frame required by the TSR. Paducah personnel informed | | the NRC Resident Inspector. The NRC operations officer notified the R3DO | | (Madera) and NMSS (Moore). | | | | * * * UPDATE AT 1520 ON 10/19/99 FROM UNDERWOOD TAKEN BY STRANSKY * * * | | | | Six sprinkler heads on the C-337 building System D-16 were identified to | | have corrosion and the PSS declared the system inoperable at 1052 CDT on | | 10/19/99. An LCO required fire patrol for the affected area was initiated | | in the time frame required by the TSR. The NRC Resident Inspector has been | | informed of this update. The NRC Operations Officer notified R3DO | | (Jorgensen). | | | | * * * UPDATE AT 2140 ON 10/19/99 FROM WALKER TAKEN BY STRANSKY * * * | | | | Seven sprinkler heads on the C-337 building System A-7 were identified to | | have corrosion, and another four had been painted over. In addition, three | | adjacent sprinkler heads on the C-337 building System A-8 were identified to | | have corrosion. The PSS declared the systems inoperable at 1900 CDT on | | 10/19/99. An LCO required fire patrols for the affected areas were | | initiated in the time frame required by the TSR. The NRC Resident Inspector | | has been informed of this update. The NRC Operations Officer notified R3DO | | (Wright). | | | | * * * UPDATE AT 1713 ON 10/21/99 FROM CAGE TAKEN BY JOLLIFFE * * * | | | | Four sprinkler heads on the C-337 building System A-5, twelve sprinkler | | heads on the C-337 building System A-8, three sprinkler heads on the C-337 | | building System A-9, and six sprinkler heads on the C-337 building System | | B-8 were identified to have corrosion. On 10/21/99, the PSS declared | | Systems A-5 and A-9 inoperable at 1028 CDT, System A-8 inoperable at 1227 | | CDT and System B-8 inoperable at 1406 CDT. An LCO required fire patrol for | | the affected areas was initiated in the time frame required by the TSR.. | | The NRC Resident Inspector has been informed of this update. The NRC | | Operations Officer notified the R3DO Bruce Jorgensen. | | | | * * * UPDATE AT 2128 ON 10/22/99 FROM ERIC WALKER TAKEN BY JOLLIFFE * * * | | | | At 1400 CDT on 10/22/99, the PSS was notified that numerous corroded | | sprinkler heads were discovered in the C-337 building on sprinkler systems | | B-1, B-3, B-5, B-6, B-7, B-11 and D-17. Due to the number of systems called | | into question, the PSS declared all of the sprinkler systems in C-337 on the | | cell floor (a total of 66 systems) inoperable and TSR required actions | | establishing roving fire patrols were initiated within the required time | | frame. The NRC Resident lnspector has been informed of this update. The | | NRC Operations Officer notified the R3DO Bruce Jorgensen. | | | | * * * UPDATE AT 1239 ON 10/24/99 FROM TOM WHITE TAKEN BY JOLLIFFE * * * | | | | At 1200 CDT on 10/23/99, the PSS was notified that numerous corroded | | sprinkler heads were discovered in the C-337 building on sprinkler systems | | B-13 and B-14 on the ground floor, The PSS declared these systems | | inoperable and TSR required actions establishing roving fire patrols were | | initiated within the required time frame. At 1600 CDT on 10/23/99, the PSS | | was notified that numerous corroded sprinkler heads were discovered in the | | C-337 building on sprinkler systems A-16, B-12, C-8, C-12, C-15, D-5 and D-8 | | on the cell floor, These systems have already been declared inoperable and | | fire patrols are already being performed. The NRC Resident Inspector has | | been notified of this update. The NRC Operations Officer notified the R3DO | | Bruce Jorgensen. | | | | * * * UPDATE AT 1117 ON 10/25/99 FROM W. F. CAGE TAKEN BY SANDIN * * * | | | | At 1940 CDT on 10/24/99, the PSS was notified that numerous corroded | | sprinkler heads had been discovered on High Pressure Fire Water Systems C-4, | | C-5, C-6 and C-8, located in the C-337 building. These systems had | | previously been declared inoperable and fire patrols were already being | | performed at the time of discovery. The NRC Resident Inspector has been | | notified of this update. The NRC Operations Officer notified R3DO | | (Lanksbury) and NMSS (Brain Smith). | | | | * * * UPDATE AT 2235 ON 10/27/99 BY WHITE TAKEN BY MACKINNON * * * | | | | At 1517 CDT on 10/27/99, the PSS was notified that nine corroded sprinkler | | heads had been discovered on High Pressure Fire Water System A-12 located in | | the C-333 building. This system has been declared inoperable and fire | | patrols have been initiated. The NRC Resident Inspector has been notified | | of this update. The NRC Operations Officer notified R3DO (Jordan) and NMSS | | EO (Hickey). | | | | * * * UPDATE AT 2150 ON 10/30/99 BY UNDERWOOD TAKEN BY WEAVER * * * | | | | At 1950 CDT on 10/30/99, the PSS was notified that numerous corroded | | sprinkler heads had been discovered on High Pressure Fire Water Systems A-5, | | A-9, A-11, C-5, and C-7 in the C-333 building. Reference ATR-1 1999-6699 | | and 6702. These systems have been declared inoperable and fire patrols have | | been initiated. Also, due to the number of inoperable sprinkler heads, the | | remaining systems on the cell floor of C-333 were called into question and | | declared inoperable. Fire patrols for the entire cell floor have been | | initialed. The PSS determined that an update to this report was required. | | The NRC Resident Inspector has been notified of this update. The NRC | | Operations Officer notified R3DO (Jordan) and NMSS EO (Hickey). | | | | * * * UPDATE AT 2111 ON 10/31/99 BY UNDERWOOD TAKEN BY WEAVER * * * | | | | At 1412 CDT on 10/31/99, the PSS was notified that five corroded sprinkler | | heads had been discovered on High Pressure Fire Water System 9 in the C-335 | | building. There were two adjacent corroded heads discovered in two separate | | locations and a third individual head at a different location. The system | | was declared inoperable and fire patrols were initiated. The corroded heads | | have since been replaced and the system returned to operable status. The | | NRC Resident Inspector was notified of this update. The NRC Operations | | Officer notified R3DO (Jordan) and NMSS EO (Hickey). | | | | * * * UPDATE AT 2121 ON 11/01/99 BY KEVIN BEASLEY TAKEN BY JOLLIFFE * * * | | | | At 0930 CST on 11/01/99, the PSS was notified that three corroded sprinkler | | heads had been discovered on the High Pressure Fire Water System B-4 in the | | C-337 building. Two of these sprinkler heads are adjacent. Two adjacent | | corroded sprinkler heads were also discovered on the High Pressure Fire | | Water System B-5 in the C-337 building. These systems were declared | | inoperable and fire patrols were initiated. Work has been initiated to | | replace the corroded heads. The NRC Resident Inspector has been notified of | | this update. The NRC Operations Officer notified the R3DO Jim Creed. | | | | * * * UPDATE AT 2143 ON 11/02/99 BY KEVIN BEASLEY TAKEN BY JOLLIFFE * * * | | | | At 1400 CST on 11/02/99, the PSS was notified that numerous corroded | | sprinkler heads had been discovered on High Pressure Fire Water Systems C-8 | | and D-7 in the C-333 building. These systems had been previously declared | | inoperable and fire patrols were being performed at the time of discovery. | | Work has been initiated to replace the corroded heads. The NRC Resident | | Inspector has been notified of this update. The NRC Operations Officer | | notified the R3DO Jim Creed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36385 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALISADES REGION: 3 |NOTIFICATION DATE: 11/02/1999| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 11:45[EST]| | RXTYPE: [1] CE |EVENT DATE: 11/02/1999| +------------------------------------------------+EVENT TIME: 09:00[EST]| | NRC NOTIFIED BY: BOB VINCENT |LAST UPDATE DATE: 11/02/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - INDICATIONS DISCOVERED ON CONTROL ROD DRIVE SEAL HOUSINGS - | | | | At 0900 on 11/02/99, a dye penetrant (PT) examination of the control rod | | drive seal housing for control rod #44 revealed a potential crack-like | | indication in the Reactor Coolant System pressure boundary. The PT | | examination was performed to investigate a boric acid deposit on the | | exterior surface of the housing which was discovered during a previous | | visual inspection. A small indication was also found on the seal housing | | for control rod #30. The plant is in a refueling outage. An investigation | | to characterize the indications and determine their cause and extent is in | | progress. This situation will be resolved prior to plant restart. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36386 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FT CALHOUN REGION: 4 |NOTIFICATION DATE: 11/02/1999| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 17:45[EST]| | RXTYPE: [1] CE |EVENT DATE: 11/02/1999| +------------------------------------------------+EVENT TIME: 16:00[CST]| | NRC NOTIFIED BY: ERICK MATZKE |LAST UPDATE DATE: 11/02/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLAUDE JOHNSON R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - STATE NOTIFIED OF AN OIL/GREASE RELEASE IN EXCESS OF THEIR NPDES RELEASE | | PERMIT LIMIT - | | | | On 10/04/99, a mixture of oil and grease was released from the plant. The | | licensee sent a composite sample of the mixture to an offsite facility for | | analysis. At 1600 CST on 11/02/99, the licensee received the results of the | | analysis and notified the State of Nebraska that the release (13 mg/l) was | | in excess of the station's NPDES release permit limit (10 mg/l). | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36387 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 11/02/1999| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 19:06[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 11/02/1999| +------------------------------------------------+EVENT TIME: 16:56[CST]| | NRC NOTIFIED BY: ERNEST MATHES |LAST UPDATE DATE: 11/02/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLAUDE JOHNSON R4 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - MSIVs LEAKING ABOVE ACCEPTABLE LEAK RATE DURING AN LLRT - | | | | During a local leak rate test with the plant in a refueling outage, the | | licensee discovered excess leakage past the 'A' main steam line inboard and | | outboard main steam isolation valves (#B21-F022A and #B21-F028A). This | | condition exceeded the acceptable leak rate. The licensee is determining | | corrective action. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36388 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 11/02/1999| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 20:57[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 11/02/1999| +------------------------------------------------+EVENT TIME: 19:01[CST]| | NRC NOTIFIED BY: TOM OSELAND |LAST UPDATE DATE: 11/02/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM INOPERABLE - | | | | During performance of the HPCI Steam Exhaust Vacuum Breaker Line Check | | Valves IST Functional Test, one of four check valves failed to meet its | | acceptance criteria. The licensee isolated the check valve, declared the | | HPCI System inoperable, and entered a 14 day LCO. All other Emergency Core | | Cooling Systems are operable. | | | | The licensee plans to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36389 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 11/02/1999| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 21:16[EST]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 11/02/1999| +------------------------------------------------+EVENT TIME: 19:47[CST]| | NRC NOTIFIED BY: LARRY BLUNK |LAST UPDATE DATE: 11/02/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - OFFSITE AGENCIES NOTIFIED OF THE PRESENCE OF OIL LADEN GRAVEL ONSITE - | | | | The licensee notified the Illinois Emergency Management Agency and the | | National Response Center of the presence of oil in the pea gravel around the | | oil filling station underground storage tanks. The oil was present in a two | | inch layer of gravel at the top of the water table approximately five feet | | below ground level. The filling station consists of a 10,000 gallon diesel | | fuel tank, a 10,000 gallon gasoline tank, and a 1,000 gallon waste oil tank. | | No fire, explosion, or vapor hazards have been identified. The tanks will | | continue to be excavated for State Fire Marshall inspection on 11/04/99. | | The oil laden pea gravel will be removed and disposed of properly. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021