The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for November 1, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           10/29/1999 - 11/01/1999

                              ** EVENT NUMBERS **

35790  36369  36370  36371  36372  36373  36374  36375  36376  36377  36378  36379 


+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35790       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 06/03/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 14:44[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        06/02/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        16:30[CDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  10/31/1999|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |DAVID HILLS          R3      |
|  DOCKET:  0707001                              |DON COOL             NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  THOMAS WHITE                 |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBA 76.120(c)(2)(i)     ACCID MT EQUIP FAILS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THREE SPRINKLER SYSTEMS DECLARED INOPERABLE DUE TO CORRODED HEADS (24-hour   |
| report)                                                                      |
|                                                                              |
| "On 06/02/99 at 1630 CDT, the Plant Shift Superintendent (PSS) was notified  |
| that numerous sprinkler heads were corroded, affecting 16 sprinkler systems  |
| in C-337 and one system in C-333, such that the ability of the sprinklers to |
| flow sufficient water was called into question.  Subsequently, these         |
| sprinkler systems were declared inoperable, and TSR-required actions         |
| establishing roving fire patrols were initiated.  This deficiency was        |
| detected during scheduled system inspections conducted by Fire Protection    |
| personnel.  Currently, functionality of the sprinkler heads has not been     |
| fully evaluated by Fire Protection personnel, and the remaining cascade      |
| buildings are currently being inspected, and if necessary, this report will  |
| be updated to identify any additional areas.  It has been determined that    |
| this event is reportable under 10CFR76.120(c)(2) as an event in which        |
| equipment is disabled or fails to function as designed."  The NRC resident   |
| inspector has been notified of this event.                                   |
|                                                                              |
| * * * UPDATE AT 1022 EDT ON 06/04/99 FROM CAGE TO TROCINE * * *              |
|                                                                              |
| "Two sprinkler heads on system D-1 in C-337 and two sprinkler heads on       |
| system 27 in C-335 were identified to also be corroded.  These were          |
| identified to the PSS on 06/03/99 at 1600 CDT and 1601 CDT, respectively,    |
| and determined to require an update to this report by the PSS.  It has been  |
| determined that this event is reportable under 10CFR76.120(c)(2) as an event |
| in which equipment is disabled or fails to function as designed."  Paducah   |
| personnel notified the NRC resident inspector of this update.  The NRC       |
| operations officer notified the R3DO (Hills) and NMSS EO (Combs).            |
|                                                                              |
| * * * UPDATE AT 2152 EDT ON 06/17/99 FROM WALKER TO POERTNER * * *           |
|                                                                              |
| "Three sprinkler heads on system C-15 and five sprinkler heads on system B-8 |
| in C-333 were identified to also be corroded.  The PSS was notified of this  |
| condition at 1300 CDT on 06/17/99 and determined that an update to this      |
| report was required.  It has been determined that this event is reportable   |
| under 10CFR76.120(c)(2) as an event in which equipment is disabled or fails  |
| to function as designed."  Paducah personnel notified the NRC resident       |
| inspector of this update.  The NRC operations officer notified the R3DO      |
| (Madera).                                                                    |
|                                                                              |
| * * * UPDATE 1440 EDT 6/18/1999 FROM UNDERWOOD TAKEN BY STRANSKY * * *       |
|                                                                              |
| "Two sprinkler heads on system C-15 and one sprinkler head on system B-8 in  |
| C-333 were identified to have corrosion.  The PSS was notified of this       |
| condition at 1350 CDT on 06/18/99.  The area of the fire patrol for system   |
| C-15 was expanded to include the two heads identified as corroded.  The one  |
| head on system B-8 was in the area already being patrolled.  The PSS         |
| determined that an update to this report was required."  The NRC resident    |
| inspector has been informed of this update.  Notified R3DO (Madera).         |
|                                                                              |
| * * * UPDATE 1315 EDT 6/25/1999 FROM WALKER TAKEN BY STRANSKY * * *          |
|                                                                              |
| "Two sprinkler heads on system D-8 and three sprinkler heads on system D-7   |
| in C-337 were identified to have corrosion.  The PSS was notified of the     |
| condition on system D-8 at 0125 CDT on 06/25/99 and at 1019 CDT on 06/25/99  |
| for system D-7.  Both systems were immediately declared inoperable and LCO   |
| fire patrol actions were implemented.  It was determined that an update to   |
| this report was required."  The NRC resident inspector has been informed of  |
| this update.  Notified R3DO (Jordan).                                        |
|                                                                              |
| * * * UPDATE 2119 EDT 7/30/1999 FROM CAGE TAKEN BY STRANSKY * * *            |
|                                                                              |
| "Five sprinkler heads and one sprinkler piping tee on C-337 system D-7 were  |
| identified to have corrosion. The PSS was notified of these corroded system  |
| parts and declared the system inoperable at 0931 CDT on 07/30/99.  LCO       |
| required fire patrols of the affected area were initiated.  The PSS          |
| determined that an update to this event report was required."  The NRC       |
| resident inspector has been informed of this update.  Notified R3DO          |
| (Wright).                                                                    |
|                                                                              |
| * * * UPDATE 1655 EDT 7/31/1999 FROM WHITE TAKEN BY STRANSKY * * *           |
|                                                                              |
| "Two sprinkler heads on C-337 System D-1 were identified to have corrosion.  |
| The PSS was notified of these corroded system parts and declared the system  |
| inoperable at 1155 CDT on 7/31/99.  LCO required fire patrols of the         |
| affected area were initiated.  The PSS determined that an update to this     |
| report was required."  The NRC resident inspector has been informed of this  |
| update.  Notified R3DO (Wright).                                             |
|                                                                              |
| * * * UPDATE 1546 EDT 8/10/1999 FROM WHITE TAKEN BY STRANSKY * * *           |
|                                                                              |
| "Two sprinkler heads on C-337 system C-15 were identified to have corrosion. |
| The PSS was notified of these corroded system parts and declared the system  |
| inoperable at 1130 CDT on 8/10/99.  LCO required fire patrols of the         |
| affected area were initiated.  The PSS determined that an update to this     |
| report was required."  The NRC resident inspector has been informed of this  |
| update.  Notified R3DO (Burgess).                                            |
|                                                                              |
| * * * UPDATE AT 1154 EDT 8/22/99 FROM WALKER TO POERTNER * * *               |
|                                                                              |
| Four adjacent sprinkler heads on C-333 System B-1 were identified to have    |
| corrosion.  The PSS was notified of the corroded system parts and declared   |
| the system inoperable at 0918 CDT on 8/22/99.  LCO required fire patrols     |
| were initiated.  The PSS determined that an update to this report was        |
| required.  It has been determined that this event is reportable under        |
| 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to     |
| function as designed.  The NRC resident inspector will be notified.  The NRC |
| operations officer notified the R3DO (Clayton).                              |
|                                                                              |
| * * * UPDATE 2015 EDT ON 8/28/99 FROM W. F. GAGE TO S. SANDIN * * *          |
|                                                                              |
| "Two adjacent sprinkler heads on C-337 System D-11 were identified to have   |
| corrosion.  The PSS was notified of these corroded system parts and declared |
| the system inoperable at 1420 CDT on 8/28/99.   LCO required fire patrols of |
| the affected area were initiated. The PSS determined that an update to this  |
| report was required."                                                        |
| Paducah personnel informed the NRC resident inspector.  The NRC operations   |
| officer notified the R3DO (Leach) and NMSS EO (Piccone).                     |
|                                                                              |
| * * * UPDATE 2037 EDT ON 8/29/99 FROM KEVIN BEASLEY TO S. SANDIN * * *       |
|                                                                              |
| "Two adjacent sprinkler heads on C-337 System D-15 were identified to have   |
| corrosion and the PSS declared the system inoperable at 0925 [CDT] on        |
| 8/29/99.  Also two adjacent heads on C-337 System D-10 were identified to    |
| have corrosion and the PSS declared the system inoperable at 1450.   LCO     |
| required fire patrols for both of the affected areas were initiated in the   |
| time frame required by TSR.  The PSS determined that an update to this       |
| report was required."  Paducah personnel informed the NRC resident           |
| inspector.  The NRC operations officer notified the R3DO (Leach) and NMSS EO |
| (Piccone).                                                                   |
|                                                                              |
| * * * UPDATE AT 0930 EDT ON 9/1/99  BY ERIC WALKER TO FANGIE JONES * * *     |
|                                                                              |
| Add two adjacent sprinkler heads on C-337 D-14.  Paducah personnel informed  |
| the NRC Resident Inspector.  The NRC operations officer notified the R3DO    |
| (David Hills) and NMSS (Robert Pierson).                                     |
|                                                                              |
| * * * UPDATE AT 1133 EDT ON 9/8/99  BY TOM WHITE TO FANGIE JONES * * *       |
|                                                                              |
| Add two adjacent sprinkler heads on C-331 System 26, system declared         |
| inoperable at 2155 CDT on 9/7/99.  An LCO required fire patrol for the       |
| affected area was initiated in the time frame required by the TSR.  Paducah  |
| personnel informed the NRC Resident Inspector.  The NRC operations officer   |
| notified the R3DO (Monte Phillips) and NMSS (Josie Piccone).                 |
|                                                                              |
| * * * UPDATE AT 0948 ON 9/30/99 BY ERIC WALKER TO DOUG WEAVER * * *          |
|                                                                              |
| Add two adjacent sprinkler heads on C-333  System B-15 were identified to    |
| have corrosion and the PSS declared the system inoperable at 0815 CDT on     |
| 9/30/99.  An LCO required fire patrol for the affected area was initiated in |
| the time frame required by the TSR.  The PSS determined that an update to    |
| this report was required.                                                    |
| Paducah personnel informed the NRC resident inspector.   The NRC operations  |
| officer notified the R3DO (Vegel) and NMSS (Cool).                           |
|                                                                              |
| * * * UPDATE AT 1600 ON 10/13/99 BY WALKER TO GOULD * * *                    |
|                                                                              |
| Two adjacent sprinkler heads on C-333 System A-11 were Identified to have    |
| corrosion and the PSS declared the system inoperable at 1307 CDT on          |
| 10/13/99.  An LCO required fire patrol for the affected area was initiated   |
| in the time frame required by the TSR,  The PSS determined that an update to |
| this report was required.  Paducah personnel informed the NRC resident       |
| inspector.   The NRC operations officer notified the R3DO (Madera) and NMSS  |
| (Moore).                                                                     |
|                                                                              |
| * * * UPDATE AT 1520 ON 10/19/99 FROM UNDERWOOD TAKEN BY STRANSKY * * *      |
|                                                                              |
| Six sprinkler heads on C-337 System D-16 were identified to have corrosion   |
| and the PSS declared the system inoperable at 1052 CDT on 10/19/99.  An LCO  |
| required fire patrol for the affected area was initiated in the time frame   |
| required by the TSR.  The PSS determined that an update to this report was   |
| required.  The NRC resident inspector has been informed of this update.  The |
| NRC Operations Officer notified R3DO (Jorgensen).                            |
|                                                                              |
| * * * UPDATE AT 2140 ON 10/19/99 FROM WALKER TAKEN BY STRANSKY * * *         |
|                                                                              |
| Seven sprinkler heads on C-337 System A-7 were identified to have corrosion, |
| and another four had been painted over.  In addition, three adjacent         |
| sprinkler heads on C-337 System A-8 were identified to have corrosion.  The  |
| PSS declared the systems inoperable at 1900 CDT on 10/19/99.  An LCO         |
| required fire patrols for the affected areas were initiated in the time      |
| frame required by the TSR.  The PSS determined that an update to this report |
| was required.  The NRC resident inspector has been informed of this update.  |
| The NRC Operations Officer notified R3DO (Wright).                           |
|                                                                              |
| * * * UPDATE AT 1713 ON 10/21/99 FROM CAGE TAKEN BY JOLLIFFE * * *           |
|                                                                              |
| Four sprinkler heads on C-337 System A-5, twelve sprinkler heads on C-337    |
| System A-8, three sprinkler heads on C-337 System A-9, and six sprinkler     |
| heads on C-337 System B-8 were identified to have corrosion.  On 10/21/99,   |
| the PSS declared System A-5 and A-9 inoperable at 1028 CDT, System A-8       |
| inoperable at 1227 CDT and System B-8 inoperable at 1406 CDT.   An LCO       |
| required fire patrol for the affected areas was initiated in the time frame  |
| required by the TSR..  The PSS determined that an update to this report was  |
| required.  The NRC Resident Inspector has been informed of this update.  The |
| NRC Operations Officer notified the R3DO Bruce Jorgensen.                    |
|                                                                              |
| * * * UPDATE AT 2128 ON 10/22/99 FROM ERIC WALKER TAKEN BY JOLLIFFE * * *    |
|                                                                              |
| At 1400 CDT on 10/22/99, the PSS was notified that numerous corroded         |
| sprinkler heads were discovered in C-337 on sprinkler systems B-1, B-3, B-5, |
| B-6, B-7, B-11 and D-17.  Due to the number of systems called into question, |
| the PSS declared all of the sprinkler systems in C-337 on the cell floor (a  |
| total of 66 systems) inoperable and TSR required actions establishing roving |
| fire patrols were initiated within the required time frame.  The PSS         |
| determined that an update to this report was required.  It has been          |
| determined that this event Is reportable under 10CFR76.120(c)(2) as an event |
| in which equipment is disabled or fails to function as designed.             |
| The NRC Resident lnspector has been informed of this update.  The NRC        |
| Operations Officer notified the R3DO Bruce Jorgensen.                        |
|                                                                              |
| * * * UPDATE AT 1239 ON 10/24/99 FROM TOM WHITE TAKEN BY JOLLIFFE * * *      |
|                                                                              |
| At 1200 CDT on 10/23/99, the PSS was notified that numerous corroded         |
| sprinkler heads were discovered in C-337 on sprinkler systems B-13 and B-14  |
| on the ground floor,  The PSS declared these systems inoperable and TSR      |
| required actions establishing roving fire patrols were initiated within the  |
| required time frame.  At 1600 CDT on 10/23/99, the PSS  was notified that    |
| numerous corroded sprinkler heads were discovered in C-337 on sprinkler      |
| systems A-16, B-12, C-8, C-12, C-15, D-5 and D-8 on the cell floor,  These   |
| systems have already been declared inoperable and fire patrols are already   |
| being performed.  The PSS determined that an update to this report was       |
| required.  It has been determined that this event is reportable under        |
| I0CFR76.120(c)(2) as an event in which equipment is disabled or fails to     |
| function as designed.  The NRC resident inspector has been informed of this  |
| update.  The NRC Operations Officer notified the R3DO Bruce Jorgensen.       |
|                                                                              |
| * * * UPDATE AT 1117 ON 10/25/99 FROM W. F. CAGE TAKEN BY SANDIN * * *       |
|                                                                              |
| At 1940 CDT on 10/24/99, the PSS was notified that numerous corroded         |
| sprinkler heads had been discovered on High Pressure Fire Water systems C-4, |
| C-5, C-6 and C-8, located in the C-337 building.  These systems had          |
| previously been declared inoperable, and fire patrols were already being     |
| performed at the time of discovery.  The PSS determined that an update to    |
| this report was required.  It has been determined that this event is         |
| reportable under 10CFR76.120(c)(2) as an event in which equipment is         |
| disabled or fails to function as designed.                                   |
| The NRC Resident Inspector has been notified of this update.  The NRC        |
| Operations Officer notified R3DO (Lanksbury) and NMSS (Brain Smith).         |
|                                                                              |
| * * * UPDATE AT 2235 ON 10/27/99 BY WHITE TAKEN BY MACKINNON * * *           |
|                                                                              |
| At 1517 CDT on 10/27/99, the PSS was notified that 9 corroded sprinkler      |
| heads had been discovered on High Pressure Fire Water System A-12 located in |
| the C-333 building.  This system has been declared inoperable and fire       |
| patrols have been initiated.  The PSS determined that an update to this      |
| report was required.  The NRC Resident Inspector has been notified of this   |
| update.  The NRC Operations Officer notified R3DO (Jordan) and NMSS EO       |
| (Hickey).                                                                    |
|                                                                              |
|                                                                              |
| * * * UPDATE AT 2150 ON 10/30/99 BY UNDERWOOD TAKEN BY WEAVER * * *          |
| At 1950 on 10/30/1999, The Plant Shift Superintendent (PSS) was notified     |
| that numerous corroded sprinkler heads had been discovered on High Pressure  |
| Fire Water Systems A-5, A-9, A-11, C-5, and C-7 In C-333 building.           |
| Reference ATR-1 1999-6699 and 6702.  These systems have been declared        |
| inoperable and fire patrols have been initiated.  Also, due to the number of |
| inoperable sprinkler heads, the remaining systems on the cell floor of C-333 |
| were called into question and declared inoperable.  Fire patrols for the     |
| entire cell floor have been initialed.  The PSS determined that an update to |
| this report was required.                                                    |
|                                                                              |
| It has been determined that this event is reportable under 10CFR76.120(c)(2) |
| as an event in which equipment is disabled or fails to function as designed. |
| The NRC Operations Officer notified R3DO (Jordan) and NMSS EO (Hickey).      |
|                                                                              |
| The NRC resident inspector has been notified of this event.                  |
|                                                                              |
| * * * UPDATE AT 2111 ON 10/31/99 BY UNDERWOOD TAKEN BY WEAVER * * *          |
| At 1412 on 10/31/99, the PSS was notified that five corroded sprinkler heads |
| had been discovered on High Pressure Fire Water System 9 in C-335 building.  |
| There were two adjacent corroded heads discovered in two separate locations  |
| and a third individual head at a different location.  The system was         |
| declared inoperable and fire patrols were initiated.  The corroded heads     |
| have since been replaced and the system returned to operable status.   The   |
| license notified the NRC resident inspector.  The NRC Operations Officer     |
| notified R3DO (Jordan) and NMSS EO (Hickey).                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36369       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE              REGION:  2  |NOTIFICATION DATE: 10/29/1999|
|    UNIT:  [1] [] []                 STATE:  FL |NOTIFICATION TIME: 02:14[EST]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        10/29/1999|
+------------------------------------------------+EVENT TIME:        01:29[EDT]|
| NRC NOTIFIED BY:  EMLING                       |LAST UPDATE DATE:  10/29/1999|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MARK LESSER          R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       100      Power Operation  |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AUTOMATIC TURBINE TRIP/REACTOR TRIP DUE TO LOSS OF MAIN TURBINE BEARING OIL  |
| PRESSURE                                                                     |
|                                                                              |
| The reactor automatically tripped from 100% power when the main turbine      |
| tripped due to low bearing oil pressure. All control rods inserted           |
| completely, and all systems functioned as expected. The auxiliary feedwater  |
| system automatically started to feed the steam generators.                   |
|                                                                              |
| The licensee reported that a main turbine low bearing oil pressure alarm had |
| been received in the control room several minutes before the trip. An        |
| operator had just been dispatched to investigate the cause of the alarm when |
| the main turbine automatically tripped.                                      |
|                                                                              |
| The NRC resident inspector will be informed of this event by the licensee.   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36370       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DUANE ARNOLD             REGION:  3  |NOTIFICATION DATE: 10/29/1999|
|    UNIT:  [1] [] []                 STATE:  IA |NOTIFICATION TIME: 04:41[EST]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        10/29/1999|
+------------------------------------------------+EVENT TIME:        02:45[CDT]|
| NRC NOTIFIED BY:  MIKE DAVIS                   |LAST UPDATE DATE:  10/29/1999|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MIKE JORDAN          R3      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| STANDBY DIESEL GENERATOR AUTOSTART DUE TO LIGHTNING STRIKE                   |
|                                                                              |
| The licensee reported that one of the standby diesel generators autostarted, |
| but did not load, due to a lightning strike. The load dispatcher informed    |
| the site that numerous strikes were also taken on the electrical grid in the |
| vicinity of the site, causing some breaker repositioning. However, the site  |
| was unaffected, except for the autostart of the diesel generator.            |
|                                                                              |
| The NRC resident inspector has been informed of this event by the licensee.  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   36371       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  ARIZONA RADIATION REGULATORY AGENCY  |NOTIFICATION DATE: 10/29/1999|
|LICENSEE:  FOREE & VANN, INC                    |NOTIFICATION TIME: 09:29[EST]|
|    CITY:  PHOENIX                  REGION:  4  |EVENT DATE:        10/28/1999|
|  COUNTY:                            STATE:  AZ |EVENT TIME:             [MST]|
|LICENSE#:  7-263 (AZ)            AGREEMENT:  Y  |LAST UPDATE DATE:  10/29/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CHARLES MARSCHALL    R4      |
|                                                |                             |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  LINDA HOWELL (R4)            |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT - STOLEN MOISTURE DENSITY GAUGE                       |
|                                                                              |
| The following report from the State of Arizona was forwarded to the          |
| Operations Center by NRC Region IV:                                          |
|                                                                              |
| At approximately 8:00 p.m. 10/27/99 to 5:45 a.m. 10/28/99, a Troxler         |
| moisture density gauge, model 3411B, serial number 12764, containing less    |
| than 50 millicuries of americium-241/beryllium and less than 10 millicuries  |
| of cesium-137 was stolen from 8907 N. 53rd Drive, Glendale, AZ 85302. The    |
| Glendale Police were notified by the licensee as was the Arizona Highway     |
| Patrol.                                                                      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Hospital                                         |Event Number:   36372       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  LIBERTY HOSPITAL                     |NOTIFICATION DATE: 10/29/1999|
|LICENSEE:  LIBERTY HOSPITAL                     |NOTIFICATION TIME: 10:37[EST]|
|    CITY:  LIBERTY                  REGION:  3  |EVENT DATE:        10/27/1999|
|  COUNTY:                            STATE:  MO |EVENT TIME:             [CDT]|
|LICENSE#:                        AGREEMENT:  N  |LAST UPDATE DATE:  10/29/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |MIKE JORDAN          R3      |
|                                                |                             |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  TOM BROWN                    |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|LADM 35.33(a)            MED MISADMINISTRATION  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MEDICAL MISADMINISTRATION                                                    |
|                                                                              |
| On 10/27/1999, a patient was to receive a dose of 120 Gy (12,000 rad) by way |
| of implanted palladium seeds. The seeds that were ordered and delivered to   |
| the hospital each had an activity of 1.05 millicuries each, instead of 1.4   |
| millicuries, which would have been needed to obtain the prescribed dose. The |
| physicians treating the patient made a decision to implant the seeds anyway, |
| resulting in a dose of 90 Gy, and to supplement the dose by external beam.   |
| However, the written prescription kept in the hot lab was not annotated to   |
| include this change in treatment.                                            |
|                                                                              |
| Therefore, this condition is being reported as a medical misadministration,  |
| in that the  actual dose was 25% less than that prescribed. The licensee     |
| will contact the NRC Region III office regarding this issue.                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36373       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: RIVER BEND               REGION:  4  |NOTIFICATION DATE: 10/29/1999|
|    UNIT:  [1] [] []                 STATE:  LA |NOTIFICATION TIME: 15:38[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        10/29/1999|
+------------------------------------------------+EVENT TIME:        12:55[CDT]|
| NRC NOTIFIED BY:  HUSTON                       |LAST UPDATE DATE:  10/29/1999|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES MARSCHALL    R4      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       100      Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| GENERATOR TRIP - REACTOR SCRAM                                               |
|                                                                              |
| On October 29, 1999, at 1255 with the plant at 100% reactor power and in     |
| Mode 1, a generator trip followed by a reactor scram occurred at River Bend  |
| Station.  The plant responded as expected, except that recirculation pump    |
| 'A' failed to downshift to slow speed and tripped to off.  The plant is      |
| stable, and currently in Mode 3.  Hot -Shutdown.  Plant personnel continue   |
| with an orderly shutdown.  Work activities were in progress in the           |
| switchyard at the time of the event.  These activities are included in an    |
| investigation of the cause of the event.                                     |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   36374       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  SCIENTECH, INC.                      |NOTIFICATION DATE: 10/29/1999|
|LICENSEE:  NUSI                                 |NOTIFICATION TIME: 16:05[EST]|
|    CITY:  GAITHERSBURG             REGION:  1  |EVENT DATE:        10/22/1999|
|  COUNTY:  MONTGOMERY                STATE:  MD |EVENT TIME:        12:00[EDT]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  10/29/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |MARK LESSER          R2      |
|                                                |VERN HODGE           NRR     |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  PAUL LOCH                    |                             |
|  HQ OPS OFFICER:  DOUG WEAVER                  |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|CCCC 21.21               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| PART 21 REPORT                                                               |
|                                                                              |
| SCIENTECH, Inc.'s subsidiary NUS Instruments, Inc. (NUSI) has determined     |
| that a Basic Component, supplied to Carolina Power & Light Robinson Nuclear  |
| Plant under CP&L purchase orders 8Q3800CM and 9D3530CJ, contains a deviation |
| that is reportable under 10CFR21.  NUSI became aware of this potential       |
| deviation on October 22, 1999.  SCIENTECH, Inc's. President was informed     |
| October 28, 1999.  CP&L is aware of this problem and the components have     |
| been removed from service.  A formal written report will be provided within  |
| 30 days of this notification.  The components, Low Level Amplifier           |
| M/N:RTL850,  P/N:NUS-A002PA-1/3, Rev. 1 (1 ea.) and P/N:NUS-A002PA-1, Rev. 0 |
| (12 ea.), were manufactured by NUSI.  These components have been supplied to |
| no other utility for use in Safety Related Systems.  NUSI has opened a       |
| 10CFR21 file concerning this component and has numbered it as 21-99-01.      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36375       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE              REGION:  2  |NOTIFICATION DATE: 10/30/1999|
|    UNIT:  [1] [] []                 STATE:  FL |NOTIFICATION TIME: 07:28[EST]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        10/30/1999|
+------------------------------------------------+EVENT TIME:        06:42[EDT]|
| NRC NOTIFIED BY:  FIELDS                       |LAST UPDATE DATE:  10/30/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MARK LESSER          R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     M/R        Y       3        Startup          |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| PLANT HAD A MANUAL TRIP FROM 3% POWER.                                       |
|                                                                              |
| DURING PLANT STARTUP WITH THE REACTOR CRITICAL ABOVE THE POINT OF ADDING     |
| HEAT, THE "1A" STEAM GENERATOR LEVEL DECREASED WHILE BEING FED WITH THE      |
| AUXILIARY FEED SYSTEM.  THE REACTOR WAS MANUALLY TRIPPED WHEN THE STEAM      |
| GENERATOR LEVEL DECREASED BELOW THE PRE-TRIP SETPOINT.  ALL RODS FULLY       |
| INSERTED, NO ECCS INJECTION OCCURRED AND NO RELIEF VALVES LIFTED.  THE CAUSE |
| OF THE DECREASE IN STEAM GENERATOR LEVEL IS BEING INVESTIGATED.  THE HEAT    |
| SINK IS THE ATMOSPHERIC DUMP VALVES.                                         |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED.                                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36376       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 10/30/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 10:38[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        10/29/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        10:40[EDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  10/30/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |MIKE JORDAN          R3      |
|  DOCKET:  0707002                              |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  SPAETH                       |                             |
|  HQ OPS OFFICER:  CHAUNCEY GOULD               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24 HOUR 91-01 BULLETIN                                                       |
|                                                                              |
| On 10/29/99 at 1040 hours, the Plant Shift Superintendent (PSS) was notified |
| that Procedure XP2-GP-MM2000, Rev. 1, "Operation of the Negative Air         |
| Machine" was activated and used prior to the implementation of Nuclear       |
| Criticality Safety Approval (NCSA) PLANT068.A01. Procedure (XP2-GP-MM2000,   |
| Rev. 0) was revised (Rev. 1) and implemented on 9/1/99. This revised         |
| procedure contained the flowdown requirements from the new                   |
| revision or the NCSA, without the NCSA being implemented. Several            |
| requirements of the original NCSA were removed in the revision process,      |
| including the requirement to have a second, knowledgeable person VERIFY that |
| the Negative Air Machine (NAM) is only used on equipment containing 5.25%    |
| U235 enrichment or less.                                                     |
|                                                                              |
| Since personnel operating the NAM were utilizing the newly revised           |
| procedure, which reflects the requirements of the revised NCSA, they failed  |
| to complete the requirement for the second person verification. This lack of |
| verification is deemed to be the loss of one control because the governing   |
| NCSA (Rev.0) still lists this verification as a requirement.                 |
|                                                                              |
| The Negative Air Machine was immediately tagged out of service, Procedure    |
| XP2-GP-MM2000, Rev. 1 was placed on hold, and the previously approved        |
| procedure was reactivated until NCSA PLANT068A01 is activated. This          |
| Criticality Safety Incident is a Level 3 Severity Index (Loss of controls    |
| such that only one double contingency control remains in place).             |
|                                                                              |
| SAFETY SIGNIFICANCE                                                          |
|                                                                              |
| The safety significance, or this event is very low. The lack of documented   |
| verification of enrichment for the Negative Air Machine since 9/10/99 did    |
| not result in a loss of the enrichment parameter. Virtually all of the       |
| equipment in X-333 is operated below 5.25% assay.  A review of equipment     |
| worked on with the NAM was performed and none of the equipment worked on had |
| been operated above 5.25% U-235 enrichment in the time period of interest.   |
|                                                                              |
| POTENTIAL CRITICALITY PATHWAYS                                               |
|                                                                              |
| The components of the negative air machine are not favorable geometry for    |
| all enrichments. Current approved analysis limits uranium to 5.25%. however  |
| a revised analysis which has been PORC approved has shown that an enrichment |
| up to 20% U-235 is safe in the Negative Air Machine. Therefore, an           |
| enrichment above 20% would have to be present for a criticality to be        |
| possible. However, this is extremely unlikely In the X-333 Facility.         |
|                                                                              |
| CONTROLLED PARAMETERS                                                        |
|                                                                              |
| Enrichment is controlled with a first check arid a second verification.      |
| Interaction Is controlled and mass is inherently controlled through the      |
| physical limits of the filtration system to tolerate significant plugging.   |
| Neither mass nor interaction were violated in this event.                    |
|                                                                              |
| ESTIMATED AMOUNT, ENRICHMENT                                                 |
|                                                                              |
| The filter units at PORTS typically contain less than 10 grams U-235 (<1.5%  |
| critical mass). Since the negative air machine is used primarily to protect  |
| personnel from hydrogen fluoride fumes, no significant mass of U-235 is      |
| expected in the equipment.  Due to the enrichment limits on the cascade      |
| equipment In the X-333, enrichment is not expected to exceed 5%.             |
|                                                                              |
| NUCLEAR CRITICALITY SAFETY CONTROLS                                          |
|                                                                              |
| The control on this system included a first and second check to ensure the   |
| enrichment limit was not violated for the negative air machine. The          |
| requirement to perform the second check was removed from the procedure       |
| without implementing a new analysis to support its removal. The second check |
| was not performed on over 15 maintenance jobs.                               |
|                                                                              |
| CORRECTIVE ACTION                                                            |
|                                                                              |
| At the direction of the Plant Shift Superintendent, the Negative Air Machine |
| was immediately tagged out of service and the procedure was placed on hold.  |
|                                                                              |
| THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR                       |
| RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS THE RESULT OF THIS        |
| EVENT.                                                                       |
|                                                                              |
| THE NRC RESIDENT INSPECTOR WAS NOTIFIED.  THE DOE REPRESENTATIVE WILL BE     |
| NOTIFIED.                                                                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36377       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LASALLE                  REGION:  3  |NOTIFICATION DATE: 10/31/1999|
|    UNIT:  [1] [2] []                STATE:  IL |NOTIFICATION TIME: 14:00[EST]|
|   RXTYPE: [1] GE-5,[2] GE-5                    |EVENT DATE:        10/31/1999|
+------------------------------------------------+EVENT TIME:        12:03[CST]|
| NRC NOTIFIED BY:  SHANE MARIK                  |LAST UPDATE DATE:  10/31/1999|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MIKE JORDAN          R3      |
|10 CFR SECTION:                                 |                             |
|AARC 50.72(b)(1)(v)      OTHER ASMT/COMM INOP   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| Station Vent Stack Monitoring Inoperable.                                    |
|                                                                              |
| The Station Vent Stack Wide Range Gaseous Monitor is deenergized for planned |
| maintenance.  At 1203 the Pre-planned alternate Particulate Iodine and Noble |
| Gas (PING) was found to have its sample pump tripped.  Initial attempts to   |
| restart the sample pump were unsuccessful.  Instrument Maintenance           |
| Department repairs are in progress.  Chemistry personnel are preparing       |
| alternate sampling capability.                                               |
|                                                                              |
| The licensee will notify the NRC resident inspector.                         |
|                                                                              |
| * * * UPDATE AT 1705 ON 10/31/99 BY COVEYOU TAKEN BY WEAVER * * *            |
| Repairs have been made to the pre-planned alternate (PING) and functional    |
| testing has been completed as of 1527 CST.  The PING was declared operable   |
| at that time.  Normal sampling of the  Station Vent Stack has been resumed   |
| via this alternate method.    The NRC resident inspector will be informed.   |
| The HOO notified the R3DO (Jordan).                                          |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36378       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SURRY                    REGION:  2  |NOTIFICATION DATE: 10/31/1999|
|    UNIT:  [1] [2] []                STATE:  VA |NOTIFICATION TIME: 22:14[EST]|
|   RXTYPE: [1] W-3-LP,[2] W-3-LP                |EVENT DATE:        10/31/1999|
+------------------------------------------------+EVENT TIME:        20:24[EST]|
| NRC NOTIFIED BY:  BILL WEBSTER                 |LAST UPDATE DATE:  10/31/1999|
|  HQ OPS OFFICER:  DOUG WEAVER                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MARK LESSER          R2      |
|10 CFR SECTION:                                 |                             |
|AINB 50.72(b)(2)(iii)(B) POT RHR INOP           |                             |
|AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD  |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TWO DIESEL GENERATORS INOPERABLE DURING TESTING                              |
|                                                                              |
| During performance of the monthly testing of the #3 Emergency Diesel         |
| Generator (EDG), the voltage regulator (control power) would not adjust      |
| incoming voltage lower than 120 volts.  The diesel was declared inoperable   |
| pending further troubleshooting of the voltage regulator.                    |
|                                                                              |
| As required by Surry Technical Specifications, the #1 EDG and the #2 EDG     |
| were scheduled for operability testing on a daily basis. The #1 EDG was      |
| inoperable from 2024 hours to 2203 hours for required testing which rendered |
| inoperable both EDGs for Unit 1.  The #1 EDG was available at all times      |
| during testing, however, it would have required operator action to load on   |
| the bus.                                                                     |
|                                                                              |
| This report is being made pursuant 10CFR50.72(b)(2)(iii)(A) & (D) for a      |
| condition that alone could have prevented the fulfillment of safety          |
| structures or systems needed to shut down the reactor and maintain it in a   |
| safe condition and mitigate the consequences of an accident.                 |
|                                                                              |
| The licensee will notify the NRC resident inspector.                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36379       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: COOK                     REGION:  3  |NOTIFICATION DATE: 11/01/1999|
|    UNIT:  [1] [] []                 STATE:  MI |NOTIFICATION TIME: 01:50[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        10/31/1999|
+------------------------------------------------+EVENT TIME:        20:30[EST]|
| NRC NOTIFIED BY:  MUTZ                         |LAST UPDATE DATE:  11/01/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MIKE JORDAN          R3      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| SAFEGUARDS DEGRADATION RELATED TO MONITORING A CONTROL ACCESS                |
|                                                                              |
| COMPENSATORY MEASURES TAKEN.                                                 |
|                                                                              |
| THE NRC RESIDENT INSPECTOR WAS NOTIFIED.                                     |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021