Event Notification Report for September 29, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/28/1999 - 09/29/1999 ** EVENT NUMBERS ** 36171 36233 36234 36235 36236 36237 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36171 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 09/16/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 04:30[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/16/1999| +------------------------------------------------+EVENT TIME: 01:15[EDT]| | NRC NOTIFIED BY: DOUG AMTSFIELD |LAST UPDATE DATE: 09/28/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |NIEL DELLA GRECA R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Secondary containment integrity lost due to a hatch cover being removed | | during maintenance activities - | | | | At 0115 on 09/16/99, Limerick Generating Station Unit 2 experienced a loss | | of secondary containment integrity. At the time of the event, the Standby | | Gas Treatment (SBGT) System was in service. The Reactor Enclosure HVAC | | System was not in service due to maintenance activities. The SBGT System was | | unable to maintain reactor enclosure pressure greater than 0.25 inches of | | vacuum water gauge per technical specifications due to a hatch cover being | | removed for maintenance inspection activities. This event could have | | prevented the fulfillment of the safety function of structures or systems | | that are needed to control the release of radioactive materials or mitigate | | the consequences of an accident. The hatch cover was reinstalled properly | | by 0126, and the SBGT System was able to draw a vacuum on the reactor | | enclosure area greater than 0.25 inches of vacuum water gauge. | | | | The licensee informed the NRC resident inspector. | | | | * * * RETRACTION AT 0828 ON 09/28/1999 FROM GAMBLE TAKEN BY STRANSKY * * * | | | | "This is a retraction of a notification made on 09/16/99 at 0434 hours, | | (event #36171). This event was reported as a loss of safety function under | | requirement 10CFR50.72(b)(2)(iii)(D). | | | | "Unit 2 Reactor Enclosure HVAC was secured to perform an internal ductwork | | inspection. SGTS was in service maintaining negative pressure in the Reactor | | Enclosure. An inspection hatch located outside of secondary containment was | | removed to perform the internal inspection. This created an unplanned breach | | of secondary containment. Unit 2 Reactor Enclosure pressure increased but | | remained negative. The hatch was replaced, and integrity was restored within | | 11 minutes. | | | | "The basis for this retraction is that the safety analysis assumes drawdown | | of the Reactor Enclosure will take 930 seconds post accident. T.S. | | 4.6.5.1.1.c.1 surveillance drawdown of the Reactor Enclosure must be | | completed within 916 seconds (15.26 minutes). Test results indicate drawdown | | is complete within 2.5 minutes. The sum of the hatch removal time (11 | | minutes) plus drawdown time (2.5 minutes) totals 13.5 minutes. This is less | | than the 15.26 minute requirement for establishing rated negative pressure | | in the Reactor Enclosure. The safety function of mitigating the consequences | | of an accident was maintained. Therefore, this event is not reportable per | | the guidance of NUREG-1022, Rev 1." | | | | The NRC resident inspector has been informed of this retraction by the | | licensee. The NRC operations officer notified the R1DO (Silk). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36233 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ROBINSON REGION: 2 |NOTIFICATION DATE: 09/28/1999| | UNIT: [2] [] [] STATE: SC |NOTIFICATION TIME: 00:47[EDT]| | RXTYPE: [2] W-3-LP |EVENT DATE: 09/27/1999| +------------------------------------------------+EVENT TIME: 22:33[EDT]| | NRC NOTIFIED BY: DON KNIGHT |LAST UPDATE DATE: 09/28/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NORMAL POWER SUPPLY TO EMERGENCY ELECTRICAL BUS LOST DUE TO PERSONNEL | | ERROR | | | | Emergency bus E2 was temporarily deenergized after a plant worker bumped 4kV | | breaker 5215, the normal supply breaker to the bus, causing it to trip. The | | B emergency diesel generator (EDG) automatically started due to an | | undervoltage condition on bus E2 and loaded to the bus, restoring power. The | | licensee reported that the operating residual heat removal (RHR) pump | | stopped running due to the loss of power to bus E2, but operators manually | | started the standby pump and restored shutdown cooling within 2 minutes. | | Reactor coolant system temperature did not increase appreciably during the | | alignment of the standby RHR pump. | | | | The EDG continues to supply power to bus E2 while the licensee makes | | preparations to transfer back to the normal power supply. The NRC resident | | inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36234 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 09/28/1999| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 08:34[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 09/28/1999| +------------------------------------------------+EVENT TIME: 07:30[EST]| | NRC NOTIFIED BY: BRIAN ROKES |LAST UPDATE DATE: 09/28/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID SILK R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION DUE TO RAW SEWAGE RELEASE TO HUDSON RIVER | | | | The licensee notified the New York Department of Environmental Conservation | | (spill report 9907789) regarding the release of less than ten gallons of | | sewage to the Hudson River. At approximately 2043 on 9/27/1999, sewage was | | spilled from the warehouse sewage holding pit to a storm drain, which | | discharges to the Hudson River. Plant personnel secured the spill source, | | diked the drain, and cleaned up the residue. The NRC resident inspector has | | been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36235 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 09/28/1999| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 12:09[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 09/28/1999| +------------------------------------------------+EVENT TIME: 09:09[CST]| | NRC NOTIFIED BY: RODNEY WHITLEY |LAST UPDATE DATE: 09/28/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JEFF SHACKELFORD R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SUPPRESSION POOL CLEANUP ISOLATED DURING LEVEL INSTRUMENTATION CALIBRATION. | | | | The following text is a portion of a facsimile received from the licensee: | | | | "While performing a scheduled calibration of Containment Spent Fuel Pool | | Level Transmitter, SFC-LT11B, a low level isolation signal was actuated, | | which resulted in the [Division] II Suppression Pool Cleanup (SPC) isolation | | valve, RHS-AOV62, isolating. The SPC system responded as designed. | | Abnormal Operating Procedure, AOP-0003, Automatic Isolations, was entered, | | and the SPC system was secured per the System Operating Procedure (SOP). | | Calibration on the level transmitter was secured. The work instructions and | | referenced calibration data did not include any note or potential isolation | | of the SPC system. As written, the work instructions only referenced input | | to a computer point, an alarm, and a control room indication. At the time | | of this event, the SPC system was not aligned to the dryer pool, and thus | | was not causing any changes in the bulk water volume of the pool. Operation | | of the SPC system did not contribute to this event. Also, the SPC system | | performs a non-safety function. Thus, its isolation did not impact safe | | plant operation." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36236 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 09/28/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 12:24[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 09/27/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:09[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/28/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |TONY VEGEL R3 | | DOCKET: 0707002 |JOSIE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOE HALCOMB | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VALID ACTUATION OF A 'Q' SAFETY SYSTEM (24-hour report) | | | | The following text is a portion of a facsimile received from Portsmouth: | | | | "On 09/27/99 at 1609 hours, the X-333 Cascade Building operation personnel | | received three cascade automatic data processing (CADP) smoke head alarm | | actuations. These smoke heads were monitoring operating cell 33-2-4 which | | was promptly taken off stream and shut down. Emergency response personnel | | monitored the area, and all air sample results for hydrogen fluoride and UF6 | | were below detectable levels." | | | | "This event is reportable due to the valid actuation of a 'Q' safety | | system." | | | | "This event is reportable to the NRC per Safety Analysis Report (SAR) | | Section 6.9, Table 6.9-1. This is a 24-hour reportable event." | | | | "There was no loss of hazardous/radioactive material or | | radioactive/radiological contamination exposure as a result of this event." | | | | Portsmouth personnel notified the NRC resident inspector and plan to notify | | the Department of Energy site representative. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36237 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 09/28/1999| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 17:43[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 09/18/1999| +------------------------------------------------+EVENT TIME: 08:48[EST]| | NRC NOTIFIED BY: GORDON FIEDLER |LAST UPDATE DATE: 09/28/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID SILK R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 0 Startup |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE TO PERFORM RCIC AND HPCI RESET PRIOR TO EXCEEDING 150 PSI DURING | | UNIT STARTUP | | | | On 09/18/99 while the unit was in startup, reactor core isolation cooling | | (RCIC) and high pressure coolant injection (HPCI) reset was not performed | | prior to exceeding 150 psi. The reset was performed at 167 psi at 0848, and | | 150 psi was exceeded at 0830. Therefore, both RCIC and HPCI were inoperable | | for 18 minutes. | | | | The licensee stated that this issue was determined to be reportable at about | | 1730 on 09/28/99 during performance of a reportability evaluation in | | accordance with 10 CFR 50.73. The unit is currently operating at 100% power | | (steady state). | | | | The licensee plans to notify the NRC resident inspector and the state | | (Massachusetts Civil Defense). | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021