Event Notification Report for September 24, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/23/1999 - 09/24/1999 ** EVENT NUMBERS ** 36079 36082 36188 36189 36211 36215 36216 36217 36218 36219 36220 36221 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36079 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 08/27/1999| | UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 06:48[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/27/1999| +------------------------------------------------+EVENT TIME: 06:00[EDT]| | NRC NOTIFIED BY: DAVE WALSH |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KATHLEEN MODES R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY SERVICE WATER SYSTEM DEGRADATION (ONLY ONE OF FOUR PUMPS | | OPERABLE) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 08/26/99, Susquehanna Unit 1 and Unit 2 were operating at 100% power | | with the 'B' loop of emergency service water [(ESW)] out of service for | | scheduled maintenance. During testing on the ESW system, with all ESW pumps | | in service, it was identified that the 'C' and 'D' ESW pumps' discharge | | check valves were closed. The ESW flow surveillance was performed, and the | | 'C' and 'D' ESW pumps failed to achieve the required flow and were declared | | inoperable. Concurrently, the 'B' loop of ESW was returned to service. | | During the time the 'B' ESW loop was inoperable, the 'A' ESW pump was the | | only one operable ESW pump. This constitutes a serious degradation of the | | plant in that it is a condition which is outside of design basis and, | | therefore, reportable under 10 CFR 50.72(b)(1)(ii) requiring a 1-hour ENS | | notification." | | | | The licensee notified the NRC resident inspector. | | | | * * * UPDATE 1453EDT ON 9/3/99 FROM GRANT FERNSLER TO S. SANDIN * * * | | | | "This Notification is a retraction of a previous ENS Notification made | | 8/27/99 (Event # 36079)." | | | | "Subsequent evaluation by Engineering has concluded that the plant had at | | least two Emergency Service | | Water pumps capable of performing their specified safety function at all | | times. As such, the plant was not | | in a condition outside of its design basis and the report previously made | | pursuant to 10CFR50.72(b)(1)(ii) | | is hereby retracted." | | | | The licensee informed the NRC Resident Inspector. Notified R1DO(Rogge). | | | | * * *UPDATE 0316EDT ON 09/23/99 FROM MIKE PEAL TAKEN BY MACKINNON* * * | | | | The licensee is Retracting the Retraction they called in on 09/03/99 at | | 1453EDT. | | | | "On 09/22/99 at 2230, an Engineering evaluation concluded that the | | operability determination associated with the above stated event was not | | adequate, specifically relating to the potential for pump interaction to | | create low flow conditions. " | | | | "The Engineering evaluation was being performed in response to an anomaly | | identified on 09/20/99 during the run of 'D' Diesel Generator. During the | | preparation of the operability statement for the 09/20/99 anomaly, | | engineering personnel realized that incorrect assumptions were used in the | | previous operability statement. The 'C' and 'D' ESW pumps were declared | | inoperable at 2230 on 09/22/99. Evaluation continues to determine if other | | combinations of equipment out of service times result in additional | | reportable conditions." R1DO (Bob Summers) notified. | | | | The NRC Resident Inspector will be notified of the Retraction to the | | Retraction of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36082 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: INOVISION |NOTIFICATION DATE: 08/27/1999| |LICENSEE: AMPHENOL |NOTIFICATION TIME: 16:58[EDT]| | CITY: CLEVELAND REGION: 3 |EVENT DATE: 08/27/1999| | COUNTY: STATE: OH |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 09/23/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MELVYN LEACH R3 | | |KATHLEEN MODES R1 | +------------------------------------------------+SCOTT SPARKS R2 | | NRC NOTIFIED BY: JANICE BROWNLEE/FAX |CHARLES CAIN R4 | | HQ OPS OFFICER: STEVE SANDIN |VERN HODGE (FAX) NRR | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PART 21 NOTIFICATION INVOLVING UNACCEPTABLE RETENTION CAPABILITY FOR BNC | | CONNECTORS | | | | "In accordance with the requirements for basic components regulated by the | | Nuclear Regulatory Commission, as specified in 10 CFR 21.21, I am providing | | this notification. In June 1999, the reliability engineer with the 'systems | | group' department of our company sent me a memo that suggested we might have | | accepted an unacceptable part for the 30-4 connector, which is a regulated | | component. He had connected an AMP BNC connector to a cable to determine | | its equivalency to the other qualified part from Amphenol p/n 31-2. He | | found that when the wires were combed out as directed on the instructions | | that came with the AMP connector, it did not appear to perform correctly | | with respect to cable retention, and [he] asked if someone in QA could | | verify his preliminary testing. | | | | "Subsequently, our Quality Manager examined the connector and obtained | | instructions from the manufacturer that said the wires should be left | | braided, not combed out, and that if you left it braided, a stronger grip | | was achieved. The reliability engineer tried the braided connection and did | | find that the retention was improved. However, in investigating the matter | | further with the manufacturer, it was found that the manufacturer did have | | conflicting instructions but said the drawing specifying a braided | | connection should be considered the official one since it was a controlled | | document. It was also found that the part from AMP was not the originally | | qualified part number - 221552-1. AMP had obsoleted that part in 1992 and | | substituted the 221265-0 in its place. The new part, however, did not carry | | a military specification for shock (MIL-Std. 202) and was not military type | | UG-88 like the previous one - conditions which provided assurance that it | | met certain criteria needed for Seismic Class 1 rating. This information | | was presented at the company's Quality Review Meeting on August 12, 1999. A | | technical evaluation was conducted and reported in an abstract for the 30-4 | | BNC Connector by the reliability engineer on August 26, 1999. | | | | "The connectors for part 30-4 that were in stock were inspected, and it was | | found that all of them were this incorrect AMP part number. The connectors | | were subsequently put on hold by the Quality Manager, and correct connectors | | have been ordered from Amphenol. | | | | "One hundred pieces of the incorrect part (AMP 1-221265) were received at | | Victoreen (now a part of Inovision) in January 1997. A search has been | | conducted to identify those parts, assemblies, and kits which list part 30-4 | | as part of their bill of material. From those, a review will be done to | | identify those that have been produced since the receipt of the incorrect | | part and, therefore, have the potential for being incorrect. The customers | | who have received the identified products will be sent a notification within | | 30 days. If acceptable replacement parts can be obtained with that time | | frame, they will be sent with the notification. | | | | "A notification was sent to the Plant Manager/Senior Executive and to the | | Chief Operating Officer of Inovision on August 26, 1999. The Plant Manager | | has authorized me to submit this report by facsimile to the NRC Operations | | Center. A written report containing the information specified at 10 CFR | | 21.21(d)(4) will be submitted to the NRC within 30 days." | | | | (Call the NRC operations officer for contact telephone numbers.) | | | | * * * UPDATE AT 1609 EDT ON 9/23/99 BY DAVE SMITH TO FANGIE JONES * * * | | | | Inovision corrective actions are completed, the unacceptable parts were | | removed from stock and scrapped. An investigation on part usage since | | January, 1997 (the date that the unacceptable part was received into stock) | | indicated that four (4) unacceptable parts may have been sent to Rochester | | Gas and Electric. The utility has been notified by phone and certified | | mail. | | | | R1DO (Robert Summers), R3DO (Roger Lanksbury), and NRR (Vern Hodges) have | | been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36188 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 09/17/1999| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 11:38[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 09/17/1999| +------------------------------------------------+EVENT TIME: 10:50[EDT]| | NRC NOTIFIED BY: SANTINI |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |NIEL DELLA GRECA R1 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | GREATER THAN 10% OF THE EMERGENCY SIRENS ARE INOPERABLE DUE TO TROPICAL | | STORM FLOYD. (See similar Indian Point Unit 3 event: #36189.) | | | | The licensee was notified at 1050 EDT that 14 out of 77 emergency sirens in | | Westchester County were inoperable, 10 out of 10 emergency sirens in Putnam | | county are inoperable, 14 out of 16 emergency sirens in Orange county are | | inoperable, and it is expected that a significant number of emergency | | sirens in Rockland county are inoperable. Counties have initiated route | | alerting procedures. The licensee is currently in the process of trying to | | restore the inoperable sirens. | | | | The NRC resident inspector will be informed of this event by the licensee. | | | | * * * UPDATE AT 1558 EDT ON 9/23/99 BY JOHN LAMB TO FANGIE JONES * * * | | | | "This notification is a status update to the notification provided on | | September 17, 1999, (Log No. 36188) which reported that a recent storm | | (Hurricane Floyd) caused a loss of electric and telephone lines that | | resulted in greater than 10% of the emergency sirens (60 of 154) not being | | operational. The emergency siren notification system remains degraded in | | one of the four counties covered by the emergency plan. Orange County | | continues to have greater than 10% of its emergency sirens not operational | | due to power outages. Three (3) in Harriman State Park of sixteen (16) | | emergency sirens total in Orange County are inoperable. There are two (2) | | inoperable sirens in Rockland County and two (2) inoperable sirens in | | Westchester County. All sirens in Putnam County are operational. The | | emergency plan will continue to use route alerting and public radio | | announcements to notify the public in lieu of the non-operational sirens. | | Restoration of the sirens will be coordinated with the restoration plans of | | the electric and telephone companies." | | | | The licensee notified the NRC Resident Inspector. The R1DO (Robert Summers) | | was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36189 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 09/17/1999| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 11:40[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 09/17/1999| +------------------------------------------------+EVENT TIME: 10:50[EDT]| | NRC NOTIFIED BY: BRIAN ROKES |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |NIEL DELLA GRECA R1 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | GREATER THAN 10% OF THEIR EMERGENCY SIRENS HAVE BECOME INOPERABLE DUE TO | | TROPICAL STORM FLOYD. (See similar Indian Point Unit 2 event: # 36188.) | | | | At 1050 EDT, it was determined that the emergency siren notification system | | was degraded in each of the four counties (Orange County, Putnam County, | | Rockland County, and Westchester County). A recent storm caused electric | | power line outages and telephone line outages in all four counties. The | | loss of electric and telephone lines resulted in greater than 10% of the | | sirens not being operational in each county. It is estimated that | | approximately 60 of the 154 sirens are not operational. The emergency plan | | would utilize route alerting and public radio announcements to notify the | | public in lieu of the non-operating sirens. Restoration of the sirens will | | be coordinated with the restoration plans of the electric companies and | | telephone companies. | | | | The NRC resident inspector will be notified of this event by the licensee. | | | | * * * UPDATE AT 1609 EDT ON 9/23/99 BY BRIAN ROKES TO FANGIE JONES * * * | | | | "This notification is a status update to the notification provided on | | September 17, 1999, (Log No. 36189) which reported that a recent storm | | (Hurricane Floyd) caused a loss of electric and telephone lines that | | resulted in greater than 10% of the emergency sirens (60 of 154) not being | | operational. The emergency siren notification system remains degraded in | | one of the four counties covered by the emergency plan. Orange County | | continues to have greater than 10% of its emergency sirens not operational | | due to power outages. Three (3) in Harriman State Park of sixteen (16) | | emergency sirens total in Orange County are inoperable. There are two (2) | | inoperable sirens in Rockland County and two (2) inoperable sirens in | | Westchester County. All sirens in Putnam County are operational. The | | emergency plan will continue to use route alerting and public radio | | announcements to notify the public in lieu of the non-operational sirens. | | Restoration of the sirens will be coordinated with the restoration plans of | | the electric and telephone companies." | | | | The licensee notified the NRC Resident Inspector. The R1DO (Robert Summers) | | was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36211 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 09/22/1999| | UNIT: [1] [] [] STATE: MD |NOTIFICATION TIME: 10:40[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 09/22/1999| +------------------------------------------------+EVENT TIME: 09:08[EDT]| | NRC NOTIFIED BY: THOMAS O'MEARA |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT SUMMERS R1 | |10 CFR SECTION: |JIM LYONS NRR | |ARPS 50.72(b)(2)(ii) RPS ACTUATION |JOSEPH GIITTER IRO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 WAS MANUALLY TRIPPED FOLLOWING THE LOSS OF MAIN FEEDWATER | | | | Planned maintenance was being performed on the feeder breaker to non-vital | | Motor Control Center # 116. While the feeder breaker was being worked on, | | Motor Control Centers # 116 and # 106 were tied together through one tie | | breaker. The amps limits for the tie breaker were misinterpreted in the | | procedure and the feeder breaker that was supplying Motor Control Centers # | | 116 and # 106 tripped on overcurrent (The operators that performed the | | evolution verified that each Motor Control Center was less than 500 amps but | | the total for both Motor Control Centers was greater than 500 amps). The | | normal feeder tripped open on the feed that was supplying both Motor Control | | Centers. The loss of power to the Motor Control Centers caused a loss of | | control oil to both Main Feedwater Pumps and a loss of oil to the Main | | Condenser air removal pumps. The loss of both Main Feedwater pumps caused a | | loss of feedwater to the both Steam Generators. Both Motor Driven Auxiliary | | Feedwater Pumps and the Turbine Driven Auxiliary Feedwater Pump started. The | | licensee manually tripped the reactor before the reactor would have | | automatically tripped on low Steam Generator Water Level. All rods fully | | inserted into the core. The loss of the oil pumps to the Main Condenser air | | removal pumps caused a loss of condenser vacuum. The Main Steam Isolation | | Valves were closed due to the loss of condenser vacuum. At the present | | time, the Motor Driven Auxiliary Feedwater Pumps and the Steam Generator | | Atmospheric valves are maintaining the plant in Hot Standby. The licensee | | said that they have a very small Steam Generator tube leak on Unit 1, but | | there is no detectable release. | | | | All Emergency Core Cooling Systems and the Emergency Diesel Generators are | | fully operable if needed. The electrical grid is stable. The licensee | | notified the NRC Resident Inspector and Calvert County of the reactor trip. | | | | * * * UPDATE AT 2026 EDT 0N 9/23/99 BY MONTY SECKENS TO FANGIE JONES * * * | | | | "Unit 1 is at normal operating temperature and pressure and being maintained | | in hot stand-by. Preliminary results are that the normal feeder breaker to | | non-vital Motor Control Center (MCC) 106 tripped. MCC 116 was tied to MCC | | 106 for maintenance on MCC 116's feeder breaker. The direct cause of the | | feeder breaker tripping was the actual current through the breaker was | | approximately 690 amps. This value is sufficient to cause the amp detector | | long-time delay to start timing the circuit breaker function as designed. | | The reason the actual current was above the procedure limit of 500 amps was | | that the readings were taken incorrectly and only half the current was | | measured. There are two conductors per phase feeding MCC's 116 and 106. A | | technician used a clamp-on amp meter for the procedure but only measured one | | of the two conductors. The design curve specifies that the breaker should | | trip at 18 minutes at 690 amps and this is precisely what occurred. | | | | "Vacuum has been reestablished and the plant is back on main feedwater, | | therefore, aux feedwater is now in stand-by. At the present main feedwater | | and turbine by-pass valves steaming to the condenser are maintaining the | | plant in hot stand-by. Preparations for reactor start-up are in progress." | | | | The licensee has notified the NRC Resident Inspector. The R1DO (Robert | | Summers) has been informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36215 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 09/23/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 03:13[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 09/22/1999| +------------------------------------------------+EVENT TIME: 23:55[CDT]| | NRC NOTIFIED BY: McLAUGHLIN |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 90 Power Operation |90 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DIVISION 3 EMERGENCY DIESEL GENERATOR TRIPPED ON OVER SPEED DURING MONTHLY | | SURVEILLANCE TESTING. | | | | While performing monthly surveillance start of the High Pressure Core Spray | | system Emergency Diesel Generator, the Diesel automatically tripped off on | | an overspeed signal. The diesel does not appear to have been damaged but | | remains shutdown and unavailable for on-going investigation of the failure. | | The High Pressure Core Spray system is inoperable but available from normal | | power source only. The failure mechanism is being investigated and | | corrective actions will be performed. The Reactor Core Isolation Cooling | | pump and all other Emergency Core Cooling Systems are also fully operable. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36216 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 09/23/1999| | UNIT: [1] [2] [3] STATE: SC |NOTIFICATION TIME: 16:05[EDT]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 09/23/1999| +------------------------------------------------+EVENT TIME: 15:36[EDT]| | NRC NOTIFIED BY: RANDY TODD |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |ADEG 50.72(b)(1)(ii) DEGRAD COND DURING OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE IDENTIFIED AN INADEQUATE RESPONSE BY THE EMERGENCY OPERATING | | PROCEDURE | | | | "Oconee is currently conducting a special project to review and validate the | | Oconee Emergency Operating Procedure (EOP). Part of this project includes an | | assessment of procedural guidance to address design basis single failure | | scenarios. This assessment has accordingly identified that the way the EOP | | is written may | | not be adequate to effectively mitigate certain single failure scenarios | | associated with the Low Pressure Injection (LPI) and High Pressure Injection | | (HPI) systems. | | | | "The specific issue found to date is a Small Break LOCA with a failure of | | one of the Borated Water Storage Tank (BWST) isolation valves to close. If | | Reactor Building pressure is less than approximately 12 PSIG, during the | | time that the Emergency Sump suction valves are opened, calculations predict | | that the BWST will continue to drain until voids are drawn into the LPI and | | HPI Pumps. Either air voids or significantly decreased available NPSH could | | adversely affect pump performance. Although the EOP provides compensatory | | guidance to locally close a manual valve, the engineering evaluation | | concluded that the guidance did not assure that action could be completed | | within the required time frame. | | | | "Because the LPI and HPI systems are required to perform their intended | | safety function with a single failure, Oconee concluded at 1536 hours today | | that this EOP adequacy issue placed Oconee in a condition outside its design | | basis and is therefore reportable. | | | | "This is a procedural adequacy issue that does not affect current | | operability. No event has occurred, no equipment has been declared | | inoperable, and no Tech Spec action statements have been entered due to this | | issue. Interim guidance will be provided to the Operators for this | | deficiency. Additionally, prompt corrective actions are underway to | | implement formal procedural changes. | | | | "The review is continuing. An LER will be submitted to address the details | | of the current issue and any similar reportable deficiencies associated with | | this review found prior to the LER submittal." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36217 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 09/23/1999| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 16:47[EDT]| | RXTYPE: [2] GE-4 |EVENT DATE: 09/23/1999| +------------------------------------------------+EVENT TIME: 13:45[EDT]| | NRC NOTIFIED BY: SENJEEV ARAB |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 97 Power Operation |91 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PRIMARY CONTAINMENT VALVE FAILED THE LOCAL LEAK RATE TESTING | | | | "On 09/22/99 at 1345 a primary containment valve T4803F601, [Drywell] DW | | Inlet Isolation Valve, failed the Local Leakage Rate Testing (LLRT) , | | measured leakage rate exceeded the limit of 0.05 La when pressurized to Pa. | | Immediate action was to enter Technical Specification (TS) 3.6.1.8, Drywell | | and Suppression Chamber Purge System, action 'b', and declare T4803F601 | | valve inoperable and effected penetration was isolated by closing and | | deactivating the valves T4800F407, DW Air Inlet Isolation valve and | | T4800F408, DW Nitrogen Inlet Isolation valve in accordance with TS 3.6.3 | | action 'a' which was completed at 1447 on 09/22/99. | | | | "T4803F601 is a supply purge valve with resilient seal (24 inch), TS 3.6.1.8 | | action 'b' gives 24 hrs to restore the | | valve to operable status or be in hot shutdown in next 12 hrs and cold | | shutdown in next 24 hrs. The reason for valve T4803F601 failing LLRT is | | likely due to seal failure. | | | | "Plant shutdown commenced at 1600 on 09/23/99 in order to meet TS 3.6.1.8 | | action 'b'." | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE AT 1825 EDT ON 9/23/99 BY SENJEEV ARAB TO FANGIE JONES * * * | | | | The licensee has received approval of Notice of Enforcement Discretion from | | NRC/NRR and the shutdown has been terminated. Power will be restored to | | 97%. The licensee notified the NRC Resident Inspector. R3DO (Roger | | Lanksbury) has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36218 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 09/23/1999| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 17:08[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 08/06/1999| +------------------------------------------------+EVENT TIME: 10:00[EDT]| | NRC NOTIFIED BY: MICHAEL ZACCONE |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: |VERN HODGE (FAX) NRR | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 10 CFR PART 21 REPORT - ABB K-LINE BREAKER DEFECT AFTER REPAIR | | | | "This report is being made pursuant to 10CFR21.21 to identify a Substantial | | Safety Hazard with an ABB K-line Breaker. | | | | "On August 6,1999, Virgil C. Summer Nuclear Station (VCSNS) determined that | | a Substantial Safety Hazard could exist with ABB K-line breakers failing to | | trip, Improper routing/support of the shunt trip wires during refurbishment | | caused interference with the red, trip shaft paddle on the left side of the | | breaker. This condition was found on a breaker installed in safety-related | | switchgear at VCSNS. This breaker condition-was compared to several other | | ABB K-line breakers at the plant site. The other breakers were found to have | | the wires routed in a different direction, precluding interference with the | | red, trip shaft paddle. | | | | "VCSNS utilizes these breakers in many applications, including the 480 VAC, | | safety related electrical buses. The shunt trip wiring problem is considered | | a defect in repair. This condition represents a potential for a | | common mode failure for safety-related K-line breakers. | | | | "The vendor has been notified of the shunt trip wiring problem and has | | agreed to modify the procedure for the refurbishment of these breakers. | | VCSNS Engineering has determined that vendor procedure changes | | should prevent recurrence of this problem." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36219 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 09/23/1999| | UNIT: [1] [2] [3] STATE: AL |NOTIFICATION TIME: 18:50[EDT]| | RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 09/23/1999| +------------------------------------------------+EVENT TIME: 16:55[CDT]| | NRC NOTIFIED BY: RAY SWAFFORD |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY REPORT | | | | Discovery of compromise of safeguards information, compensatory measures not | | fully implemented. The licensee notified the NRC Resident Inspector. | | | | Refer to the HOO Log for additional details. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36220 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 09/23/1999| | UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 20:15[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/23/1999| +------------------------------------------------+EVENT TIME: 20:00[EDT]| | NRC NOTIFIED BY: PHIL CHASE |LAST UPDATE DATE: 09/23/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |ROBERT SUMMERS R1 | |10 CFR SECTION: |JOHN HANNON NRR | |AAEC 50.72 (a) (1) (I) EMERGENCY DECLARED |CHARLES MILLER IRO | |AESF 50.72(b)(2)(ii) ESF ACTUATION |DAN RISHE FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT ENTERED AN UNUSUAL EVENT - TOXIC GAS DETECTED IN UNIT 2 TURBINE | | ENCLOSURE | | | | An Unusual Event was declared due to readings of 65 ppm hydrogen sulfide | | (HS) and 115 ppm carbon monoxide (CO) in the Unit 2 Turbine Enclosure. | | | | The oncoming shift reported the smell of rotten eggs when they arrived on | | site. Inspection around the site determined the only place toxic gas was | | detectable was in the Unit 2 Turbine Enclosure. There were no detectable | | levels of any toxic gas existing anywhere else around the plant. | | Inspections are on going around the plant. The Unit 2 Turbine Enclosure has | | been evacuated after an inspection for a source of the gasses. | | | | The licensee isolated the control room by manually initiating chlorine | | isolation as a precaution at 1922 EDT, this is an Engineered Safety Feature | | activation and reportable as a 4-hour notification. | | | | The licensee notified the NRC Resident Inspector and the state/local | | government agencies. | | | | * * * UPDATE AT 2321 EDT ON 9/23/99 BY TOM DOUGHERTY TO JOHN MacKINNON * * | | * | | | | The site de-escalated from the Unusual Event at 2312 EDT. The toxic gas | | levels were verified to be nominal 0% in all areas inside and outside the | | power block. The source of the toxic gas is still unknown and under | | investigation. The licensee notified the NRC Resident Inspector and the | | state/local government agencies. The R1DO (Robert Summers), NRR EO (John | | Hannon), IRO Manager (Charles Miller), and FEMA (Cegielski) have been | | informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36221 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 09/24/1999| | UNIT: [1] [] [] STATE: CA |NOTIFICATION TIME: 02:13[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/23/1999| +------------------------------------------------+EVENT TIME: 17:52[PDT]| | NRC NOTIFIED BY: STEVE WILSON |LAST UPDATE DATE: 09/24/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOSEPH TAPIA R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Standby |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A TRANSFER IN OFFSITE POWER SOURCES CAUSED THE TURBINE DRIVEN AUXILIARY | | FEEDWATER PUMP TO AUTOMATICALLY START AND DISCHARGE WATER INTO THE STEAM | | GENERATORS. | | | | During restoration of relaying in the 500 kV switchyard an actuation caused | | the opening of the PCB breakers (Main Generator Breakers) supplying Unit 1 | | from Auxiliary Power System). Unit 1 power automatically transferred to the | | Start-Up power supply. The momentary loss of power during the transfer | | caused the Turbine Driven Auxiliary Feedwater Pump to start from an ESF | | actuation signal (12 kV Buses) and discharge into the Main Steam Generators. | | | | | | Reactor Coolant Temperature decreased approximately 7 degrees F due to the | | operation of the Turbine Driven Auxiliary Feedwater Pump (Tave no load is | | 547 degrees F). The Turbine Driven Auxiliary Feedwater pump operated for | | approximately 18 minutes before it was secured. A Reactor Operator | | immediately closed the Turbine Driven Auxiliary Feedwater discharge valve(s) | | to secure auxiliary feedwater to the Steam Generators, so there was very | | little discharge of auxiliary feedwater into the Steam Generators. Reactor | | Coolant System cooldown was mainly due to the Turbine Driven Auxiliary | | Feedwater Turbine using the steam from the Steam Generators for its motive | | force. | | | | The NRC Resident Inspector will be informed of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021