Event Notification Report for September 21, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/20/1999 - 09/21/1999 ** EVENT NUMBERS ** 36091 36197 36201 36202 36203 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36091 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 08/31/1999| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 02:21[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 08/30/1999| +------------------------------------------------+EVENT TIME: 22:22[CDT]| | NRC NOTIFIED BY: GREEN |LAST UPDATE DATE: 09/21/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF A SINGLE TRAIN SYSTEM THAT IS REQUIRED TO MITIGATE THE | | CONSEQUENCES OF AN ACCIDENT | | | | On 8/30/99 at 2222 while performing maintenance on SW-MOV-650MV, Reactor | | Equipment Cooling (REC) heat exchanger "A" Service Water (SW) Outlet Valve, | | SW-MOV-650MV was manually opened while disconnecting Limit Switches. The | | valve was opened to a point that allowed 2475 Gallons Per Minute (GPM) of | | service water flow thru the "A" REC heat exchanger. Service water flow | | greater than 1200 GPM thru the "A" REC heat exchanger results in the "A" | | Service Water subsystem being inoperable (LCO 3.7.2) which requires | | restoration of the "A" Service Water subsystem within 30 days. LCO 3.8.1 | | was entered for Diesel Generator 1 (DG1) because it was declared inoperable | | due to the Service Water being inoperable. The Control Room Emergency | | Filtration System (CREFS), which is a single train system, was aligned to a | | bus that would be powered from DG1 in the event of an accident. This | | condition resulted in CREFS also being declared inoperable (LCO 3.7.4) | | | | When the increased flow though the "A" REC heat exchanger was discovered by | | a Control Room Operator, the Valve Technicians performing the maintenance | | were instructed to manually close SW-MOV-650MV until Service Water flow | | through the "A" REC Heat Exchanger was reduced below 1200 GPM, which was | | completed at 2238. All of the previously mentioned LCO's were also exited at | | this time. | | | | At the time this event occurred both sources of offsite power were available | | and DG2 was determined to not be affected by this condition. | | | | The Resident Inspector was notified. | | | | | | *** UPDATE ON 9/21/99 @ 0259 BY GREEN TO GOULD *** EVENT RETRACTION | | | | SUBSEQUENT INVESTIGATION HAS DETERMINED THAT D/G#1 WAS ALWAYS CAPABLE OF | | PERFORMING ITS SAFETY FUNCTION DURING THE EVENT. THEREFORE, CREFS REMAINED | | OPERABLE AND THIS EVENT IS BEING RETRACTED. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36197 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 09/18/1999| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 13:29[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 09/18/1999| +------------------------------------------------+EVENT TIME: 01:00[CDT]| | NRC NOTIFIED BY: JOHN SELL |LAST UPDATE DATE: 09/20/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SHEAR R3 | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | |NLTR LICENSEE 24 HR REPORT | | |NLCO TECH SPEC LCO A/S | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RESPONSE TO NRC BULLETIN 80-24 REGARDING LEAKAGE OF SERVICE WATER INTO | | REACTOR CONTAINMENTS (24-HOUR REPORT) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "At 0100 [CDT] on 09/18/99, a pin hole leak was identified on the 'A' Unit 1 | | containment fan cooler. The unit had been in a 72-hour [limiting condition | | for operation (LCO)] for partial blockage of this cooler by zebra mussels. | | The leak was discovered during treatment for the zebra mussels. The LCO | | expires at 1035 [CDT] on 09/19/99. The plan is presently to isolate the | | leaking tube section and restore the cooler as operable but degraded." | | | | There was nothing unusual or not understood and all systems functioned as | | required. The licensee stated that there are four containment fan coolers | | per unit. The licensee also stated the NRC Bulletin 80-24 has been | | superceded but that they are still committed to the provisions of this | | bulletin. | | | | The licensee notified the NRC resident inspector. | | | | * * * UPDATE AT 1345 ON 09/20/99 FROM JOHN SELL TAKEN BY JOLLIFFE * * * | | | | Upon further review of this event, the licensee determined that only leakage | | greater than 1 GPM should be reportable to the NRC and that reporting this | | event to the NRC was a conservative action. The 1 GPM value is consistent | | with Point Beach Tech Spec requirements for evaluation of RCS leakage. The | | pinhole leak did not meet this criteria. Thus, the licensee desires to | | retract this event. The 72 hour LCO for the 'A' Unit 1 containment fan | | cooler was exited at 2140 CDT on 09/18/99. The fan cooler remains operable | | but degraded. | | | | The licensee informed the NRC Resident Inspector. The NRC Operations | | Officer notified the R3DO Roger Lanksbury. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36201 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 09/20/1999| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 03:59[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 09/20/1999| +------------------------------------------------+EVENT TIME: 00:09[EDT]| | NRC NOTIFIED BY: CHISM |LAST UPDATE DATE: 09/20/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHRIS CHRISTENSEN R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 4 Startup |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE REACTOR WAS MANUALLY SCRAMMED AT 4% POWER. | | | | While in mode 2 at approximately 450 psig during unit 2 startup, an | | automatic group 1 (MSIV's, steam line drain and reactor sample valves) | | isolation occurred. The main steam line isolation caused reactor pressure to | | rise. The licensee inserted control rods and stabilized reactor pressure at | | approximately 950 psig. After verifying that the automatic isolation signal | | had cleared, the licensee equalized around and reopened the MSIV's in order | | to restart a reactor feed pump and restore RPV level control. When feed flow | | was restored, a rapid power rise was observed prompting the licensee to | | insert a manual reactor scram. All control rods fully inserted as expected, | | and no ECCS actuation occurred or safety relief valves lifted. The licensee | | took conservative action to insert a manual scram. | | | | The systems affected by the automatic isolations were returned to service. | | Unit 2 is currently in hot shutdown. The licensee has formed an event | | investigation team for this event. The cause of the automatic isolation has | | not been positively determined, but it appears the isolation occurred when | | the licensee was draining the condenser pressure sensing lines for the | | pressure transmitters resulting in a Group 1 isolation on low condenser | | vacuum in accordance with 0GP-02, APPROACH TO CRITICALITY AND PRESSURIZATION | | OF THE REACTOR. | | | | The Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36202 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 09/20/1999| | UNIT: [] [3] [] STATE: PA |NOTIFICATION TIME: 17:53[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 09/20/1999| +------------------------------------------------+EVENT TIME: 14:35[EDT]| | NRC NOTIFIED BY: CAMERON CAMPBELL |LAST UPDATE DATE: 09/20/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT SUMMERS R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 82 Power Operation |82 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Channel 'B' manual half scram signal received due to an electrical short | | in the reactor protection system logic - | | | | A channel 'B' manual half scram signal was received during modification | | installation when drilling activities inadvertently contacted a wire in the | | reactor protection system (RPS) logic. The shorted wire resulted in a blown | | fuse which deenergized power to the channel 'B' manual half scram logic. | | The outboard scram discharge volume vent valves and drain valve shut per | | design on receipt of the channel 'B' manual half scram signal. | | | | The damaged RPS wire has been repaired and the fuse has been replaced. The | | channel 'B' manual half scram signal has been reset and the outboard scram | | discharge volume vent valves and drain valve have been reopened per station | | procedures by 1638. The channel 'B' manual half scram signal and subsequent | | reset had no impact on plant operation. | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36203 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: THREE MILE ISLAND REGION: 1 |NOTIFICATION DATE: 09/21/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 00:56[EDT]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP |EVENT DATE: 09/21/1999| +------------------------------------------------+EVENT TIME: 00:50[EDT]| | NRC NOTIFIED BY: BOYER |LAST UPDATE DATE: 09/21/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT SUMMERS R1 | |10 CFR SECTION: | | |AMED 50.72(b)(2)(v) OFFSITE MEDICAL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIALLY CONTAMINATED INJURED PERSON TRANSPORTED OFFSITE. | | | | THE LICENSEE TRANSPORTED AN INDIVIDUAL WHO INJURED HIS LOWER BACK WHILE | | WORKING INSIDE CONTAINMENT ON THE UPPER MANWAY TO THE HERSHEY MEDICAL | | CENTER. HE MAY HAVE BEEN CONTAMINATED, SO HE WAS ACCOMPANIED BY HEALTH | | PHYSICS PERSONNEL TO THE HOSPITAL. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED | | | | *** UPDATE ON 9/21/99 @ 0209 BY BOYER TO GOULD *** | | | | THE INDIVIDUAL WAS NOT CONTAMINATED, HOWEVER, HIS CLOTHING WAS AND IT IS | | BEING RETURNED TO THE SITE. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021