Event Notification Report for September 13, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/10/1999 - 09/13/1999 ** EVENT NUMBERS ** 35688 36110 36143 36144 36145 36146 36147 36148 36149 36150 +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35688 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: USAF RADIOISOTOPE COMMITTEE |NOTIFICATION DATE: 05/07/1999| |LICENSEE: USAF RADIOISOTOPE COMMITTEE |NOTIFICATION TIME: 10:45[EDT]| | CITY: Sumptor REGION: 2 |EVENT DATE: 05/07/1999| | COUNTY: STATE: SC |EVENT TIME: 09:38[EDT]| |LICENSE#: 42-23539-01AF AGREEMENT: Y |LAST UPDATE DATE: 09/10/1999| | DOCKET: 03028641 |+----------------------------+ | |PERSON ORGANIZATION | | |CHRIS CHRISTENSEN R2 | | |BILL JONES R4 | +------------------------------------------------+DON COOL NMSS | | NRC NOTIFIED BY: MAJOR JAMES HICKS |FRANK CONGEL IRO | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A MISSING CHEMICAL AGENT MONITOR CONTAINING 15 mCi OF NICKEL-63 | | FROM SHAW AIR FORCE BASE LOCATED IN SUMTER, SOUTH CAROLINA | | | | At 0938 on 05/07/99, Shaw Air Force Base (AFB) located in Sumter, South | | Carolina, notified the U.S. Air Force Radioisotope Committee located at | | Bolling AFB located in Washington D.C. of a missing chemical agent monitor | | (CAM) containing a 15-mCi nickel-63 source. | | | | On 04/27/99, the base radiation safety officer (RSO) at Shaw AFB conducted | | an inventory of CAMs located in building #1981. The correct number of CAMs | | were there, but one had the wrong serial number. Examination of previous | | inventories shows one CAM with a different serial number. The building had | | been searched with no success. The 20CES/CEX RSO has no explanation for the | | different serial number on one CAM or where the correct CAM may be located. | | | | | | It is suspected that the CAM may have been exchanged with another Air Force | | Unit or may have been sent off for calibration. At this time, the U.S. Air | | Force Radioisotope Committee believes that the CAM is still in Air Force | | possession. Past shipping records will be researched, and calibration labs | | that serve Shaw AFB will be notified. The completion time for these actions | | is currently estimated to be 06/07/99. | | | | Call the NRC Operations Officer for a licensee contact telephone number. | | | | The licensee plans to notify the NRC Region 4 office and plans to issue a | | 30-day written report. | | | | *** UPDATE ON 6/11/99 @ 1242 BY HICKS TO GOULD *** INTERIM REPORT | | | | MISSING CAM SERIAL NUMBER: CAN-C-04646 | | | | RADIOACTIVITY MATERIAL CONTAINED: 10 mCi OF Ni-63 | | | | ACTIVITY: 0.05 Ci | | | | CHEMICAL AND PHYSICAL FORM: SOLID | | | | A SERIAL NUMBER DISCREPANCY WAS NOTED DURING A SEMIANNUAL CAM INVENTORY | | CONDUCTED 4/27/99. THE PREVIOUS INVENTORY CONDUCTED 10/98 INDICATED NO | | DISCREPANCIES. | | | | A DISPOSITION, OR PROBABLE DISPOSITION, OF THE MATERIAL IS UNDETERMINABLE. | | | | THERE EXISTS THE POSSIBILITY THAT CALIBRATION SERVICES MAY HAVE SWAPPED OUT | | THE CAM WITH ANOTHER MONITOR. ALSO, A POLICE INVESTIGATION MAY BE REQUIRED | | SINCE THE DEVICE IS WORTH OVER $3,000.00. | | | | NOTIFIED REG 2 RDO(BONSER), REG 4 RDO(ANDREWS), AND NMSS EO(COOL). | | | | *** UPDATE ON 9/10/99 AT 1316 FROM HICKS (FAX) TO POERTNER *** | | | | The investigative officer concluded a one-for-one swap out of a CAM must | | have occurred. There is no supporting documentation, but numerically this | | unit is in possession of 5 CAMS which is consistent with the quantity always | | on hand. They believe the CAM was exchanged with one belonging to a unit | | deployed overseas. The investigation is closed. | | | | Notified R4DO (SANBORN), R2DO (HAAG), and NMSS (PICCONE). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36110 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 09/01/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 11:57[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/31/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 14:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/10/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |DAVID HILLS R3 | | DOCKET: 0707002 |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOE HALCOMB | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MICROFILTRATION SYSTEM pH PROBES DISCOVERED TO BE OUT OF TOLERANCE | | | | "On 8/31/99 at 1200 hrs, the Plant Shift Superintendent was notified that a | | previously discovered X-705 Microfiltration System (MFS) pH probe out of | | tolerance condition likely existed during a time period when the MFS was in | | operation. The out of tolerance condition was in a non-conservative | | direction and previously discovered during a routine weekly surveillance on | | 8/27/99. An evaluation to determine the condition existed while the MFS was | | in operation was initiated at that time. Engineering suspected that the | | probe calibration may have been affected when the probes were exposed to a | | high pH solution on 8/23/99. Subsequent discussion with the probe | | manufacturer confirmed that a high pH solution could affect probe | | calibration. As a result, it was concluded that the out of tolerance | | condition likely existed from approximately 8/23/99 to 8/27/99. | | | | "The out of tolerance condition affected 2 of the 3 pH probes (2 out of 3 | | logic required to activate the safety system). The as found data for the 2 | | probes indicated they would actuate at 6.73 pH and 6.65 pH, which is below | | the 7 pH required setpoint. A review of the MFS operational history | | indicated that the MFS pH was maintained above a 7 pH during the time the | | probes are suspected to have been out of tolerance." | | | | The NRC resident inspector has been informed of this notification. | | | | *** RETRACTION AT 1145 EDT ON 9/10/99 FROM SPAETH TO POERTNER *** | | | | Based on completion of Engineering Evaluation EVAL-PS-1999-0523, the plant | | has determined that the pH probes were out of tolerance in a conservative | | direction and therefore would have actuated earlier than required. | | | | The NRC resident inspector has been notified. | | | | Notified R3DO (Phillips), and NMSS (Piccone). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36143 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 09/10/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 11:39[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 09/09/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/10/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MONTE PHILLIPS R3 | | DOCKET: 0707002 |JOSIE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: WILLIAM POERTNER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CRITICALITY ACCIDENT ALARM SYSTEM HORN INOPERABLE DUE TO IMPROPER | | CONNECTION | | | | At 1500 hours, on 9/9/99, the Criticality Accident Alarm System (CAAS) slave | | horn in the X-344B building was discovered to be not connected to the X-344A | | CAAS evacuation alarm as designed. During troubleshooting activities, | | maintenance personnel found that the horn was connected to the gas release | | alarm system instead of the CAAS evacuation horn system. | | | | This condition is reportable to the NRC per 10CFR76.120(c) "Safety Equipment | | Failure/Actuation", the equipment is required by a TSR to be available and | | operable and no redundant equipment is available and operable to perform the | | required safety function. | | | | There was no loss of hazardous material or radioactive/radiological | | contamination exposure as a result of this event. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36144 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 09/10/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 12:01[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 09/10/1999| +------------------------------------------------+EVENT TIME: 08:13[EDT]| | NRC NOTIFIED BY: PETER ABBOTT |LAST UPDATE DATE: 09/10/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM INOPERABLE DUE TO INOPERABLE | | TRIP MODULE. | | | | During routine High Pressure Coolant Injection (HPCI) system temperature | | isolation logic testing, an isolation trip module was found to be | | inoperable. Per Technical Specification requirements, the HPCI system steam | | supply primary containment isolation outboard valves must be closed within | | four hours. This renders the HPCI system inoperable. The isolation valves | | were closed and deactivated at 1153 EDT. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36145 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 09/10/1999| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 14:53[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 09/10/1999| +------------------------------------------------+EVENT TIME: 14:00[EDT]| | NRC NOTIFIED BY: MICHAEL TESORIERO |LAST UPDATE DATE: 09/10/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 87 Power Operation |86 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT SHUTDOWN REQUIRED BY TECHNICAL SPECIFICATIONS DUE TO PINHOLE LEAK IN | | THE ESSENTIAL SERVICE WATER SYSTEM. | | | | At approximately 1400 hours on September 10, 1999, a plant shutdown was | | commenced as scheduled to enter a refueling outage. The ENS notification is | | being made because a portion of the Essential Service Water (SW) header was | | declared inoperable at approximately 1215 hours. A pinhole leak on 18 inch | | SW pipe number 408 was evaluated using the guidance of Generic Letter 90-05 | | and it was determined that the SW pipe could not be declared operable using | | the criteria provided in the Generic Letter. Concurrent with the planned | | shutdown, Technical Specification 3.3.F.2 requires the reactor be brought to | | the cold shutdown condition starting no later than 12 hours after the SW | | pipe was declared inoperable. The SW pipe will be repaired prior to plant | | startup. | | | | The SW pipe leak is located outside containment and can not be isolated for | | repairs until the plant is in cold shutdown. The SW pipe supplies the | | containment Fan Cooler units which are required by Technical Specifications. | | The leak rate is I to 2 drops per minute. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36146 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 09/10/1999| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 21:27[EDT]| | RXTYPE: [3] CE |EVENT DATE: 09/10/1999| +------------------------------------------------+EVENT TIME: 19:58[CDT]| | NRC NOTIFIED BY: NEAL BERNARD |LAST UPDATE DATE: 09/10/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP AND FEEDWATER ACTUATION DUE TO RCP 2B SEAL FAILURE. | | | | The licensee performed a manual reactor trip due to failure of the Reactor | | Coolant Pump 2B seals. Emergency feedwater actuated following the trip. | | All control rods fully inserted. No relief valves or safety valves opened | | and excess energy is being released via steam to the main condenser. RCP 2B | | was secured following the trip. RCP 2B seal pressures are significantly | | lower than normal and seal leakoff flow is also low. The plant is in hot | | standby and stable. The licensee plans to go to cold shutdown to repair the | | RCP. | | | | The NRC resident was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36147 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 09/11/1999| | UNIT: [1] [] [] STATE: AR |NOTIFICATION TIME: 06:00[EDT]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 09/11/1999| +------------------------------------------------+EVENT TIME: 03:01[CDT]| | NRC NOTIFIED BY: FRED VANBUSKERK |LAST UPDATE DATE: 09/11/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY FEEDWATER AUTO STARTED ON TRIPPING OF ALL REACTOR COOLANT PUMPS | | | | "During a planned shutdown for refueling, while securing 2 of 4 Reactor | | Coolant Pumps (RCP), 'D' Reactor Coolant Pump experienced reverse rotation | | when it was secured. In this condition, the Abnormal Operating Procedure | | directs operators to stop all RCPs. In response to the loss of all 4 RCPs, | | the Emergency Feedwater (EFW) System auto-actuated, as expected, and Natural | | Circulation Cooling initiated. | | | | "Natural Circulation Cooling is in progress. All systems responded normally | | to this event. | | | | "The current plan is to install a restraining device to prevent 'D' RCP | | rotation and then reestablish forced-flow cooling with two operable RCPs | | (one per loop)." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36148 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 09/12/1999| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 06:31[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/12/1999| +------------------------------------------------+EVENT TIME: 03:44[CDT]| | NRC NOTIFIED BY: GREG JANAK |LAST UPDATE DATE: 09/12/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DURING TURBINE TRIP SYSTEM TESTING | | | | During the performance of Main Turbine Emergency Trip System testing on | | Channel 1, the plant experienced an automatic turbine trip which initiated a | | reactor trip. All control rods fully inserted and systems responded as | | expected including the start of the Auxiliary Feedwater System, an | | Engineered Safety Feature system. No relief valves or safety valves opened | | and excess energy is being released via steam to the main condensers. The | | licensee is investigating exact cause of trip. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36149 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 09/12/1999| | UNIT: [1] [2] [] STATE: VA |NOTIFICATION TIME: 09:30[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 09/12/1999| +------------------------------------------------+EVENT TIME: 09:04[EDT]| | NRC NOTIFIED BY: VICKY HARTE |LAST UPDATE DATE: 09/12/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |AENS 50.72(b)(1)(v) ENS INOPERABLE | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 60 Power Operation |60 Power Operation | |2 N N 0 Hot Standby |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST SAFETY PARAMETER DISPLAY SYSTEM AND THE TECHNICAL SUPPORT CENTER | | COMPUTER | | | | Power was lost to the Safety Parameter Display System (SPDS) and the | | Technical Support Center (TSC) computer system at 0904 EDT on 9/12/99. The | | bus supplying power to the battery charger for the SPDS and TSC computer was | | lost when the supply breaker opened on a ground detection, on the | | underground cable supply. The normal alternate power supply to the battery | | charger was previously lost, some time ago, due to another ground on its | | underground cable supply. The licensee made the decision to preserve the | | battery and deenergized the battery bus. Also, with the TSC computer system | | out-of-service, the control room will serve as the alternate TSC facility. | | | | This event is a major loss of emergency assessment capability and is | | reportable. Troubleshooting and repairs to the electrical distribution | | system are in progress. Also, the licensee is investigating an alternate | | methods to power the battery charger. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36150 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 09/12/1999| | UNIT: [2] [3] [] STATE: PA |NOTIFICATION TIME: 16:17[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 09/12/1999| +------------------------------------------------+EVENT TIME: 15:30[EDT]| | NRC NOTIFIED BY: RICHARD TRUAX |LAST UPDATE DATE: 09/13/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 85 Power Operation |85 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF POWER TO THE TSC DUE TO BREAKER FAILURE. | | | | During planned electrical switching at the Unit 1 training center a breaker | | failed to close causing a loss of power to the Unit 1 training center which | | provides power to the Technical Support Center (TSC). This resulted in a | | loss of assessment capability from the TSC . Assessment capability is still | | available from the main control room and Emergency Operation Facility. | | | | The licensee is investigating the cause of the breaker failure. | | | | The NRC resident will be notified. | | | | * * * UPDATE AT 0155 EDT ON 9/13/99 BY ED EILOLA TO FANGIE JONES * * * | | | | Repairs were made and power was restored to the TSC at 0145 EDT on 9/13/99. | | The licensee intends to notify the NRC Resident Inspector. The NRC | | operations officer notified the R1DO (Tom Moslak). | +------------------------------------------------------------------------------+
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