The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for September 3, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           09/02/1999 - 09/03/1999

                              ** EVENT NUMBERS **

35964  36018  36113  36114  36115  36116  36117  36118  36119  36120  

+------------------------------------------------------------------------------+
|Other Nuclear Material                           |Event Number:   35964       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  UNITED STATES AIR FORCE              |NOTIFICATION DATE: 07/27/1999|
|LICENSEE:  UNITED STATES AIR FORCE              |NOTIFICATION TIME: 16:58[EDT]|
|    CITY:  WASHINGTON DC            REGION:  1  |EVENT DATE:        07/26/1999|
|  COUNTY:                            STATE:  DC |EVENT TIME:        10:00[EDT]|
|LICENSE#:  42-23539-01AF         AGREEMENT:  N  |LAST UPDATE DATE:  09/02/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |ROBERT HAAG          R2      |
|                                                |BILL JONES           R4      |
+------------------------------------------------+CHARLEY HAUGHNEY     NMSS    |
| NRC NOTIFIED BY:  MAJOR HICKS                  |                             |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|BAE1 20.2202(b)(1)       PERS OVEREXPOSURE      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| USAF PERSON INHALED DEPLETED URANIUM DUST                                    |
|                                                                              |
| THE USAF RADIOISOTOPE COMMITTEE, BOLLING AIR FORCE BASE, REPORTED THE        |
| FOLLOWING INCIDENT WHICH OCCURRED AT ROBINS AIR FORCE BASE, GEORGIA .        |
|                                                                              |
| AT 1000 ON 07/26/99, USAF PERSONNEL WERE PERFORMING MAINTENANCE ON A C-141   |
| CARGO AIRCRAFT AILERON.  A TECHNICIAN WAS FOUND USING A HAMMER AND CHISEL TO |
| REMOVE INSTALLED DEPLETED URANIUM COUNTERWEIGHTS FROM THE AILERON.  THIS     |
| PROCESS PRODUCED DUST AND DEBRIS WHICH WAS SCATTERED BY A NEARBY FAN.  THE   |
| TECHNICIAN USING A HAMMER AND CHISEL ON THE DEPLETED URANIUM WAS IN          |
| VIOLATION OF SEVERAL RULES.                                                  |
|                                                                              |
| UPON DISCOVERY OF THIS ACTIVITY, THE TECHNICIAN WAS TOLD TO IMMEDIATELY STOP |
| WORK . THE AREA HAS BEEN SECURED AND DECONTAMINATION PROCEDURES INITIATED.   |
| HEALTH PHYSICS SUPPORT HAS BEEN REQUESTED FROM BROOKS AIR FORCE BASE, SAN    |
| ANTONIO, TEXAS.  BIOASSAYS OF THE TECHNICIAN AND OTHER WORKERS IN THE AREA   |
| HAS BEEN INITIATED.                                                          |
|                                                                              |
| CONTAMINATION LEVELS IN THE ROOM WHERE THE MAINTENANCE WAS BEING PERFORMED   |
| WERE FOUND TO BE ABOVE BACKGROUND (NUCLEAR RESEARCH CORPORATION MODEL        |
| ADM-300 DETECTOR WITH A PANCAKE PROBE WAS USED TO SURVEY THE AREA).  THE     |
| AREA OF CONTAMINATION HAS BEEN CONFINED TO THE BUILDING 180 MAINTENANCE      |
| BAY.                                                                         |
|                                                                              |
| A FOLLOWUP REPORT BY THE USAF RADIOISOTOPE COMMITTEE WILL BE MADE TO NRC     |
| REGION 4 BY 08/27/99.                                                        |
|                                                                              |
| *** UPDATE ON 9/2/99 FROM USAF (FAX) TO POERTNER ***                         |
|                                                                              |
| An Interim Report was submitted to Region 4.  A  follow-up or final report   |
| will be submitted by 9/28/99.                                                |
|                                                                              |
| HOO notified R4DO (Cain), R2DO (Landis), and NMSS (Hickey).                  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36018       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 08/11/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 14:46[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        08/10/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        16:00[EDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  09/02/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |BRUCE BURGESS        R3      |
|  DOCKET:  0707002                              |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  JIM McCLEERY                 |                             |
|  HQ OPS OFFICER:  LEIGH TROCINE                |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBB 76.120(c)(2)(ii)    EQUIP DISABLED/FAILS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| FAILURE OF 13 HIGH PRESSURE FIRE WATER SPRINKLER SYSTEMS TO MEET SYSTEM      |
| OPERABILITY REQUIREMENTS  (24-Hour Report)                                   |
|                                                                              |
| The following text is a portion of a facsimile received from Portsmouth:     |
|                                                                              |
| "On 08/10/99 at approximately 1600 hours, the Plant Shift Superintendent     |
| (PSS) was notified that 13 sprinkler systems associated with the High        |
| Pressure Fire Water (HPFW) system were not capable of meeting system         |
| operability requirements.  This condition was discovered as a result of an   |
| engineering review of individual sprinkler heads that had previously been    |
| identified as exhibiting corrosion around the valve seat.  The engineering   |
| review was conducted following the discovery that similar corrosion problems |
| experienced at the Paducah Gaseous Diffusion Plant resulted in sprinkler     |
| heads being unable to actuate at normal pressure.  An initial screening of   |
| PORTS sprinkler heads known to exhibit corrosion was conducted, and systems  |
| where the potential for two or more adjacent heads to be corroded were       |
| inspected.  This identified 11 systems in the X-333 and 2 systems in the     |
| X-326 that did not meet the sprinkler system operability requirement that no |
| two adjacent sprinkler heads be inoperable."                                 |
|                                                                              |
| "The PSS declared the affected sprinkler systems inoperable, and TSR         |
| required actions were completed.  Further inspections of sprinkler systems   |
| are planned.  This report will be updated if additional sprinkler systems    |
| are determined to be inoperable."                                            |
|                                                                              |
| "There was no loss of hazardous/radioactive material or                      |
| radioactive/radiological contamination  exposure as a result of this         |
| event."                                                                      |
|                                                                              |
| Portsmouth personnel notified the NRC resident inspector as well as the      |
| onsite Department of Energy representative.                                  |
|                                                                              |
| *** UPDATE ON 8/19/99 AT 2327 FROM HALCOMB TO POERTNER ***                   |
|                                                                              |
| During continuing walkdowns, HPFW system #398 was discovered with two or     |
| more (3) adjacent sprinkler heads with mineral deposits.  This HPFW          |
| sprinkler was declared inoperable at 1038 hours and was repaired at 1407     |
| hours.                                                                       |
|                                                                              |
| Portsmouth personnel notified the NRC resident inspector.                    |
|                                                                              |
| * * * UPDATE 1415 EDT ON 8/28/99 FROM JIM McCLEERY TO S. SANDIN * * *        |
|                                                                              |
| The following information was provided as an update to this report:          |
|                                                                              |
| "During continuing walk downs of the HPFW system, systems 194, 196, 197,     |
| 211, 212 were found with two or more adjacent sprinkler heads unable to meet |
| system operability.  Systems were made inoperable at 1452 on 8/27/99.  All   |
| sprinklers were repaired and system operability made at 0550 8/26/99."       |
|                                                                              |
| Portsmouth personnel informed the NRC resident inspector.  The NRC           |
| operations officer notified the R3DO (Leach) and NMSS EO (Piccone).          |
|                                                                              |
| * * * UPDATE 2337 ON 8/30/1999 FROM McCLEERY TAKEN BY STRANSKY * * *         |
|                                                                              |
| "During continuing walkdowns of the HPFW system, seven additional systems    |
| were found with two or more adjacent sprinkler heads unable to meet system   |
| operability. Six systems were in the X-333 and one in the X-330. These       |
| systems were made inoperable starting at 1100 8/30/99 and repairs are being  |
| performed at this time."                                                     |
|                                                                              |
| Notified R3DO (Hills) and NMSS EO (Piccone).                                 |
|                                                                              |
| * * * UPDATE 2305 8/31/1999 FROM McCLEERY TAKEN BY STRANSKY * * *            |
|                                                                              |
| "Add seven HPFW systems from X-333 building." The NRC resident inspector has |
| been informed of this update.                                                |
|                                                                              |
| Notified R3DO (Hills) and NMSS EO (Pierson).                                 |
|                                                                              |
| * * * UPDATE 0047 EDT on  9/2/1999 FROM JIM McCLEERY  TO FANGIE JONES * * *  |
|                                                                              |
| "Add fourteen HPFW systems from X-333 building." The NRC resident inspector  |
| has been informed of this update.                                            |
|                                                                              |
| Notified R3DO (Hills) and NMSS EO (Pierson).                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36113       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 09/02/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 12:50[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        09/02/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:             [EDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  09/02/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |DAVID HILLS          R3      |
|  DOCKET:  0707002                              |JOHN HICKEY          NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  KURT SISLER                  |                             |
|  HQ OPS OFFICER:  WILLIAM POERTNER             |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBB 76.120(c)(2)(ii)    EQUIP DISABLED/FAILS   |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MICROFILTRATION SYSTEM pH PROBES OUT OF TOLERANCE                            |
|                                                                              |
| On 9/1/99 at 1300 hours, the plant shift superintendent was notified that a  |
| previously discovered X-705 Microfiltration System (MFS) pH probe out of     |
| tolerance condition likely existed during a time period when the MFS was in  |
| operation.  The out of tolerance condition was in a non-conservative         |
| direction and previously documented during a routine weekly surveillance on  |
| 6/4/99.  During the engineering evaluation, it was concluded at 1000 hours   |
| on 9/2/99, that the out of tolerance condition likely existed from           |
| approximately 5/28/99 to 6/4/99.                                             |
|                                                                              |
| The out of tolerance condition affected 2 of the 3 probes (2 out of 3 logic  |
| required to activate the safety system).  The as found data for the 2 probes |
| indicated they would actuate at 6.70 pH and 6.63 pH, which is below the 7 pH |
| required setpoint.  A review of MFS operational history indicated that the   |
| MFS pH was maintained above a 7 pH during the time the probes are suspected  |
| to have been out of tolerance.                                               |
|                                                                              |
| There was no loss of hazardous/radioactive material or                       |
| radioactive/radiological contamination.                                      |
|                                                                              |
| The NRC resident inspector has been notified.                                |
|                                                                              |
| * * * UPDATE 1452EDT ON 9/2/99 FROM KURT SISLER TO S. SANDIN * * *           |
|                                                                              |
| The following is a portion of information provided as an update to include   |
| classification of the event as a 24-hour 91-01 Bulletin report:              |
|                                                                              |
| "Upon further review of [the] X-705 Microfiltration System pH probe failure, |
| it was determined to be reportable per NRC Bulletin 91-01 criteria.          |
|                                                                              |
| "Safety Significance:                                                        |
|                                                                              |
| "Two out of three safety system pH probes used in the microfiltration system |
| were found to be out of tolerance. The system relies on a two-out-of-three   |
| logic for system actuation. The probes read 7.30 and 7.37 for a buffer       |
| solution which had a pH of approximately 7.0 (depending on the temperature). |
| NCSA-0705_015.A10 takes credit for these pH probes in satisfying the double  |
| contingency principle.  Active engineered feature #5 states 'Microfiltration |
| effluent pH shutdown system will automatically stop the flow of microfilter  |
| permeate to the T-105 tank if pH<7.0 (with an allowable test tolerance of    |
| -0.2), by closing both isolation valves automatically.'  Since the probes    |
| were overestimating the pH, a pH of as low as approximately 6.70 could be    |
| present without an actuation of the system.                                  |
|                                                                              |
| "Contingency event B.4.2 credits the effluent pH shutdown system in          |
| preventing dissolved uranium past the microfilters (to an unsafe geometry    |
| tank downstream).  Also credited is the unlikely event of solution with a    |
| low pH making it to the microfiltration modules due to the functioning of    |
| the pH adjustment system. Therefore, the out of tolerance condition in a     |
| non-conservative direction constitutes a loss of one criticality control in  |
| a double contingency system.                                                 |
|                                                                              |
| "The discussion for B.4.2 includes the following,  'Based on chemical        |
| reactions and calculations in POEF-340-98-113, it would require an extremely |
| low pH (in the range of approximately 4 to 5) before the resulting solution  |
| would pick up any appreciable amounts (i.e., milligrams per liter) of        |
| uranium. However, this level of uranium is well below the individually       |
| always safe concentration limit reported in GAT-225, Rev. 4, of 5000 ppm     |
| U-235 for 100% enriched solution.'  Based on the as-found tolerances, a pH   |
| of 6.70 would have caused the system to actuate. Therefore, this event has a |
| low safety significance.                                                     |
|                                                                              |
| "Potential Criticality Pathways involved (Brief scenario(s) of how           |
| criticality could occur):                                                    |
|                                                                              |
| "Event B.4.2.a credits the effluent pH shutdown system in preventing         |
| dissolved uranium past the microfilters (to an unsafe geometry tank          |
| downstream). Also credited is the unlikely event of solution with a low pH   |
| making it to the microfiltration modules due to the functioning of the pH    |
| adjustment system. Both a failure in the pH shutdown system and the unlikely |
| event of a low pH following pH adjustment would have to occur for this       |
| scenario to take place.                                                      |
|                                                                              |
| "Controlled parameters:                                                      |
|                                                                              |
| "The prevention of acidic solutions from entering the microfiltration        |
| modules maintains the uranium in the filters in a favorable geometry, rather |
| than picking up uranium in addition to the safe batch being processed.       |
| Therefore, geometry is controlled.                                           |
|                                                                              |
| "Estimated Amount, Enrichment, Form of Licensed Material (include process    |
| limit and % worst case of critical mass):                                    |
|                                                                              |
| "The operation is approved for 100% U-235; however, only USEC material       |
| (maximum 10% U-235 has been processed recently. The microfiltration process  |
| is controlled such that only a safe mass of U-235 is present in any          |
| unfavorable geometry. Operational information indicates that the pH was      |
| never less than 7.0 during the time the system was potentially out of        |
| calibration                                                                  |
|                                                                              |
| "Nuclear Criticality Safety Controls(s) or control system(s) and description |
| of failures or deficiencies:                                                 |
|                                                                              |
| "Two out of three safety system pH probes used in the microfiltration system |
| were found to be out of tolerance. The system relies on a two-out-of-three   |
| logic for system actuation. The system is relied on to keep unmeasured       |
| quantities of uranium (from the microfilter modules) from entering an        |
| unfavorable geometry tank.                                                   |
|                                                                              |
| "Therefore, the failure of the pH shutdown system (due to out of calibration |
| probes or any reason) is an analyzed condition."                             |
|                                                                              |
| The HOO notified R3DO (Hills) and NMSS (Piccone).                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36114       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LASALLE                  REGION:  3  |NOTIFICATION DATE: 09/02/1999|
|    UNIT:  [1] [] []                 STATE:  IL |NOTIFICATION TIME: 13:21[EDT]|
|   RXTYPE: [1] GE-5,[2] GE-5                    |EVENT DATE:        09/02/1999|
+------------------------------------------------+EVENT TIME:        10:36[CDT]|
| NRC NOTIFIED BY:  D. COVEYOU                   |LAST UPDATE DATE:  09/02/1999|
|  HQ OPS OFFICER:  WILLIAM POERTNER             +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |DAVID HILLS          R3      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       93       Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| RPS ACTUATION - REACTOR SCRAM                                                |
|                                                                              |
| At 1036 CDT on 9/2/99, Unit 1 received an RPS Automatic Actuation.  The      |
| actuation occurred due to low water level (12.5 inches, Level 3) resulting   |
| from a feedwater transient.  The lowest level noted was -10 inches on the    |
| wide range recorders.  No ECCS actuations occurred or were required during   |
| the transient.  All systems operated as designed except as described below:  |
| During the auxiliary power fast bus transfer the Unit 1 station air          |
| compressor surged and was subsequently restored, the 0C clean condensate     |
| pump tripped and the 0A clean condensate pump was started, the 1A and 1C     |
| circulating water pumps tripped, the 1B circulating water pump remained      |
| running, actions are being taken to restart the 1A circulating water pump    |
| and a delay is being encountered restoring the 345 KV ring bus due to        |
| difficulties in opening the main power transformer disconnects.              |
|                                                                              |
| All rods inserted and no safety relief valves lifted.                        |
|                                                                              |
| The NRC resident inspector has been notified.                                |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36115       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: VERMONT YANKEE           REGION:  1  |NOTIFICATION DATE: 09/02/1999|
|    UNIT:  [1] [] []                 STATE:  VT |NOTIFICATION TIME: 13:44[EDT]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        09/02/1999|
+------------------------------------------------+EVENT TIME:        11:43[EDT]|
| NRC NOTIFIED BY:  ANDREW WISNIEWSKI            |LAST UPDATE DATE:  09/02/1999|
|  HQ OPS OFFICER:  WILLIAM POERTNER             +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |WILLIAM COOK         R1      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| ESF ACTUATION - PRIMARY CONTAINMENT ISOLATION SYSTEM (PCIS) GROUP III        |
| ISOLATION                                                                    |
|                                                                              |
| At 1143, on 9/2/99, the control room received a PCIS Group III isolation.  A |
| Group III isolation isolates all drywell atmospheric valves and reactor      |
| building ventilation.  Standby gas treatment started.  The cause of the      |
| isolation was the west refuel floor radiation monitor failing upscale.  The  |
| actuation is considered invalid.                                             |
|                                                                              |
| Local radiation readings were verified less than 1 mR/hr.  New fuel          |
| inspections will be secured prior to resetting the Group III isolation to    |
| allow reestablishing drywell to torus differential pressure which had been   |
| broken for vacuum breaker testing prior to the isolation.                    |
|                                                                              |
| The NRC resident inspector has been notified.                                |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36116       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BYRON                    REGION:  3  |NOTIFICATION DATE: 09/02/1999|
|    UNIT:  [1] [2] []                STATE:  IL |NOTIFICATION TIME: 16:02[EDT]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        09/02/1999|
+------------------------------------------------+EVENT TIME:        11:17[CDT]|
| NRC NOTIFIED BY:  STEVEN RAMSEY                |LAST UPDATE DATE:  09/02/1999|
|  HQ OPS OFFICER:  WILLIAM POERTNER             +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |DAVID HILLS          R3      |
|10 CFR SECTION:                                 |TAD MARSH            NRR     |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION                                                         |
|                                                                              |
| At 1158 CDT, 9/2/99, the National Earthquake Information Center, Golden      |
| Colorado, reported that an earthquake occurred at 1117 CDT with an epicenter |
| approximately 30 miles from the site.  It was reported the earthquake        |
| occurred approximately 10 miles SSE of Dixon, Illinois at a magnitude of 3.5 |
| on the Richter scale.  Some minor tremors were felt by site personnel.       |
| There was no impact on plant operations.  Plant seismic instrumentation did  |
| not detect this event.  The instrumentation was tested and verified          |
| operable.  At approximately 1400 CDT a presentation was made to the local    |
| media to address questions they had.                                         |
|                                                                              |
| The NRC resident has been notified.                                          |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36117       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS              REGION:  4  |NOTIFICATION DATE: 09/02/1999|
|    UNIT:  [1] [] []                 STATE:  TX |NOTIFICATION TIME: 17:51[EDT]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        09/02/1999|
+------------------------------------------------+EVENT TIME:        16:00[CDT]|
| NRC NOTIFIED BY:  GREG JANAK                   |LAST UPDATE DATE:  09/02/1999|
|  HQ OPS OFFICER:  WILLIAM POERTNER             +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES CAIN         R4      |
|10 CFR SECTION:                                 |                             |
|NLTR                     LICENSEE 24 HR REPORT  |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24 HOUR REPORT - CONTROL ROOM ENVELOPE VENTILATION SYSTEM MAKEUP UNIT TRAIN  |
| 'C' INOPERABLE                                                               |
|                                                                              |
| South Texas Project made the following notification per NPF-076, Section     |
| 2G:                                                                          |
|                                                                              |
| Carbon samples obtained from control room envelope ventilation system makeup |
| unit train 'C' failed laboratory tests.  The Technical Specification         |
| 4.7.7.c.2 limit of 1% for methyl iodine penetration was exceeded.  The as    |
| found  methyl iodine penetration results were 2.87%.  This results in the    |
| train 'C'  control room envelope system being inoperable since the time that |
| the carbon samples were obtained on August 23, 1999 at 0940 CDT.  This       |
| results in the system being inoperable for greater than 7 days which is a    |
| violation of Technical Specification 3.7.7 action a.  The sample results     |
| were obtained on September 1, 1999 at 0935 CDT.                              |
|                                                                              |
| The charcoal adsorber banks for train 'C' control room envelope system have  |
| been replaced and testing is in progress to verify system operability.       |
|                                                                              |
| The NRC resident inspector has been notified.                                |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36118       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: WOLF CREEK               REGION:  4  |NOTIFICATION DATE: 09/02/1999|
|    UNIT:  [1] [] []                 STATE:  KS |NOTIFICATION TIME: 19:13[EDT]|
|   RXTYPE: [1] W-4-LP                           |EVENT DATE:        09/02/1999|
+------------------------------------------------+EVENT TIME:        15:00[CDT]|
| NRC NOTIFIED BY:  DANIEL BOWERS                |LAST UPDATE DATE:  09/02/1999|
|  HQ OPS OFFICER:  WILLIAM POERTNER             +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES CAIN         R4      |
|10 CFR SECTION:                                 |                             |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| ACCIDENT MITIGATION                                                          |
|                                                                              |
| On 3/15/99 and 4/29/99, surveillance test STS AE-001, Main Feedwater         |
| Isolation Valve Accumulator Discharge Test, was performed using a digital    |
| temperature indicator that was subsequently found to be out of calibration.  |
| The surveillance test ensures the nitrogen precharge is sufficient to close  |
| the main feedwater isolation valves.  With the out of calibration            |
| temperature indication the nitrogen precharge may not have been adequate to  |
| close the valves.  The surveillance test is performed monthly and has        |
| subsequently been performed using calibrated instruments.  The feedwater     |
| isolation valves are currently operable.                                     |
|                                                                              |
| The NRC resident inspector will be notified.                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   36119       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS              REGION:  4  |NOTIFICATION DATE: 09/02/1999|
|    UNIT:  [] [2] []                 STATE:  TX |NOTIFICATION TIME: 19:51[EDT]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        09/01/1999|
+------------------------------------------------+EVENT TIME:        19:49[CDT]|
| NRC NOTIFIED BY:  JOHN MILLIFF                 |LAST UPDATE DATE:  09/02/1999|
|  HQ OPS OFFICER:  WILLIAM POERTNER             +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES CAIN         R4      |
|10 CFR SECTION:                                 |                             |
|NLTR                     LICENSEE 24 HR REPORT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LICENSEE 24 HOUR REPORT FOR VIOLATION OF OPERATING LICENSE NPF-80 (2G)       |
| Section 2.C(2)                                                               |
|                                                                              |
| Steam generator level channel L-0549 failed on 9/1/99 at 1529 CDT placing    |
| the unit in a one hour Limiting Condition for Operation per Technical        |
| Specifications.  Action 20 of TS 3.3.2.6.d was entered and the channel       |
| bistables were tripped.  It was determined the cause of the level channel    |
| failure could be manifested in the solid state protection system.  At 1949   |
| CDT the bistables were untripped to verify the operability of the solid      |
| state protection system.  Unit 2 entered Technical Specification 3.0.3 for   |
| this condition.  The input relay to the 'S' logic train for steam generator  |
| level channel L-0549 was determined to be the cause of the failed channel.   |
| Action 9 of Technical Specification 3.3.1.21 and action 22 of Technical      |
| Specification 3.3.2.6.b were entered at 2017 CDT to replace the failed       |
| relay.  The relay was replaced and steam generator level channel L-0549 was  |
| declared operable at 2055 CDT.                                               |
|                                                                              |
| The NRC resident inspector has been notified.                                |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   36120       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 09/02/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 22:02[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        09/02/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        12:57[CDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  09/02/1999|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |DAVID HILLS          R3      |
|  DOCKET:  0707001                              |ROBERT PIERSON       NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  MIKE UNDERWOOD               |                             |
|  HQ OPS OFFICER:  WILLIAM POERTNER             |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBA 76.120(c)(2)(i)     ACCID MT EQUIP FAILS   |                             |
|OCBB 76.120(c)(2)(ii)    EQUIP DISABLED/FAILS   |                             |
|OCBC 76.120(c)(2)(iii)   REDUNDANT EQUIP INOP   |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24 HOUR REPORT - SAFETY EQUIPMENT FAILURE                                    |
|                                                                              |
| At 1257 CDT on 9/2/99, during performance of a proceduralized simulated      |
| power failure test, the main breaker to the Unit 2 battery room tripped.  In |
| addition, the transformer secondary breakers on all four auxiliary           |
| substations tripped due to undervoltage relay action.  As a result of the    |
| loss of power to the four auxiliary substations, three plant air compressors |
| on-line in the C-335 air plant were deenergized.  The unplanned loss of the  |
| C-335 air compressors caused the on-line plant air compressor capacity to    |
| drop to 6500 SCFM which is below the 10,250 SCFM required to ensure plant    |
| Criticality Accident Alarm  System (CAAS) audibility.  CAAS detectability    |
| was not affected.  CAAS TSR LCO actions for inaudibility were initiated for  |
| affected facilities C-310, C-331, C-333, C-333A, C-335, C-337, C-337A,       |
| C-360, C-400, and C-409.  The plant air capacity was restored to above       |
| 10,250 SCFM at 1300 hours by placing standby air compressors in service.     |
| The CAAS was declared operable at 1312 hours and the LCOs were exited.       |
|                                                                              |
| The licensee is still investigating the cause of the event.                  |
|                                                                              |
| This event is reportable under 10CFR76.120(c)(2) as a event in which         |
| equipment required by the TSR is disabled or fails to function as designed.  |
|                                                                              |
| The NRC resident inspector has been notified.                                |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Wednesday, March 24, 2021