Event Notification Report for September 3, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/02/1999 - 09/03/1999 ** EVENT NUMBERS ** 35964 36018 36113 36114 36115 36116 36117 36118 36119 36120 +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35964 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNITED STATES AIR FORCE |NOTIFICATION DATE: 07/27/1999| |LICENSEE: UNITED STATES AIR FORCE |NOTIFICATION TIME: 16:58[EDT]| | CITY: WASHINGTON DC REGION: 1 |EVENT DATE: 07/26/1999| | COUNTY: STATE: DC |EVENT TIME: 10:00[EDT]| |LICENSE#: 42-23539-01AF AGREEMENT: N |LAST UPDATE DATE: 09/02/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ROBERT HAAG R2 | | |BILL JONES R4 | +------------------------------------------------+CHARLEY HAUGHNEY NMSS | | NRC NOTIFIED BY: MAJOR HICKS | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAE1 20.2202(b)(1) PERS OVEREXPOSURE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | USAF PERSON INHALED DEPLETED URANIUM DUST | | | | THE USAF RADIOISOTOPE COMMITTEE, BOLLING AIR FORCE BASE, REPORTED THE | | FOLLOWING INCIDENT WHICH OCCURRED AT ROBINS AIR FORCE BASE, GEORGIA . | | | | AT 1000 ON 07/26/99, USAF PERSONNEL WERE PERFORMING MAINTENANCE ON A C-141 | | CARGO AIRCRAFT AILERON. A TECHNICIAN WAS FOUND USING A HAMMER AND CHISEL TO | | REMOVE INSTALLED DEPLETED URANIUM COUNTERWEIGHTS FROM THE AILERON. THIS | | PROCESS PRODUCED DUST AND DEBRIS WHICH WAS SCATTERED BY A NEARBY FAN. THE | | TECHNICIAN USING A HAMMER AND CHISEL ON THE DEPLETED URANIUM WAS IN | | VIOLATION OF SEVERAL RULES. | | | | UPON DISCOVERY OF THIS ACTIVITY, THE TECHNICIAN WAS TOLD TO IMMEDIATELY STOP | | WORK . THE AREA HAS BEEN SECURED AND DECONTAMINATION PROCEDURES INITIATED. | | HEALTH PHYSICS SUPPORT HAS BEEN REQUESTED FROM BROOKS AIR FORCE BASE, SAN | | ANTONIO, TEXAS. BIOASSAYS OF THE TECHNICIAN AND OTHER WORKERS IN THE AREA | | HAS BEEN INITIATED. | | | | CONTAMINATION LEVELS IN THE ROOM WHERE THE MAINTENANCE WAS BEING PERFORMED | | WERE FOUND TO BE ABOVE BACKGROUND (NUCLEAR RESEARCH CORPORATION MODEL | | ADM-300 DETECTOR WITH A PANCAKE PROBE WAS USED TO SURVEY THE AREA). THE | | AREA OF CONTAMINATION HAS BEEN CONFINED TO THE BUILDING 180 MAINTENANCE | | BAY. | | | | A FOLLOWUP REPORT BY THE USAF RADIOISOTOPE COMMITTEE WILL BE MADE TO NRC | | REGION 4 BY 08/27/99. | | | | *** UPDATE ON 9/2/99 FROM USAF (FAX) TO POERTNER *** | | | | An Interim Report was submitted to Region 4. A follow-up or final report | | will be submitted by 9/28/99. | | | | HOO notified R4DO (Cain), R2DO (Landis), and NMSS (Hickey). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36018 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/11/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:46[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/10/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/02/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |BRUCE BURGESS R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM McCLEERY | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF 13 HIGH PRESSURE FIRE WATER SPRINKLER SYSTEMS TO MEET SYSTEM | | OPERABILITY REQUIREMENTS (24-Hour Report) | | | | The following text is a portion of a facsimile received from Portsmouth: | | | | "On 08/10/99 at approximately 1600 hours, the Plant Shift Superintendent | | (PSS) was notified that 13 sprinkler systems associated with the High | | Pressure Fire Water (HPFW) system were not capable of meeting system | | operability requirements. This condition was discovered as a result of an | | engineering review of individual sprinkler heads that had previously been | | identified as exhibiting corrosion around the valve seat. The engineering | | review was conducted following the discovery that similar corrosion problems | | experienced at the Paducah Gaseous Diffusion Plant resulted in sprinkler | | heads being unable to actuate at normal pressure. An initial screening of | | PORTS sprinkler heads known to exhibit corrosion was conducted, and systems | | where the potential for two or more adjacent heads to be corroded were | | inspected. This identified 11 systems in the X-333 and 2 systems in the | | X-326 that did not meet the sprinkler system operability requirement that no | | two adjacent sprinkler heads be inoperable." | | | | "The PSS declared the affected sprinkler systems inoperable, and TSR | | required actions were completed. Further inspections of sprinkler systems | | are planned. This report will be updated if additional sprinkler systems | | are determined to be inoperable." | | | | "There was no loss of hazardous/radioactive material or | | radioactive/radiological contamination exposure as a result of this | | event." | | | | Portsmouth personnel notified the NRC resident inspector as well as the | | onsite Department of Energy representative. | | | | *** UPDATE ON 8/19/99 AT 2327 FROM HALCOMB TO POERTNER *** | | | | During continuing walkdowns, HPFW system #398 was discovered with two or | | more (3) adjacent sprinkler heads with mineral deposits. This HPFW | | sprinkler was declared inoperable at 1038 hours and was repaired at 1407 | | hours. | | | | Portsmouth personnel notified the NRC resident inspector. | | | | * * * UPDATE 1415 EDT ON 8/28/99 FROM JIM McCLEERY TO S. SANDIN * * * | | | | The following information was provided as an update to this report: | | | | "During continuing walk downs of the HPFW system, systems 194, 196, 197, | | 211, 212 were found with two or more adjacent sprinkler heads unable to meet | | system operability. Systems were made inoperable at 1452 on 8/27/99. All | | sprinklers were repaired and system operability made at 0550 8/26/99." | | | | Portsmouth personnel informed the NRC resident inspector. The NRC | | operations officer notified the R3DO (Leach) and NMSS EO (Piccone). | | | | * * * UPDATE 2337 ON 8/30/1999 FROM McCLEERY TAKEN BY STRANSKY * * * | | | | "During continuing walkdowns of the HPFW system, seven additional systems | | were found with two or more adjacent sprinkler heads unable to meet system | | operability. Six systems were in the X-333 and one in the X-330. These | | systems were made inoperable starting at 1100 8/30/99 and repairs are being | | performed at this time." | | | | Notified R3DO (Hills) and NMSS EO (Piccone). | | | | * * * UPDATE 2305 8/31/1999 FROM McCLEERY TAKEN BY STRANSKY * * * | | | | "Add seven HPFW systems from X-333 building." The NRC resident inspector has | | been informed of this update. | | | | Notified R3DO (Hills) and NMSS EO (Pierson). | | | | * * * UPDATE 0047 EDT on 9/2/1999 FROM JIM McCLEERY TO FANGIE JONES * * * | | | | "Add fourteen HPFW systems from X-333 building." The NRC resident inspector | | has been informed of this update. | | | | Notified R3DO (Hills) and NMSS EO (Pierson). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36113 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 09/02/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 12:50[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 09/02/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: [EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/02/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |DAVID HILLS R3 | | DOCKET: 0707002 |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KURT SISLER | | | HQ OPS OFFICER: WILLIAM POERTNER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MICROFILTRATION SYSTEM pH PROBES OUT OF TOLERANCE | | | | On 9/1/99 at 1300 hours, the plant shift superintendent was notified that a | | previously discovered X-705 Microfiltration System (MFS) pH probe out of | | tolerance condition likely existed during a time period when the MFS was in | | operation. The out of tolerance condition was in a non-conservative | | direction and previously documented during a routine weekly surveillance on | | 6/4/99. During the engineering evaluation, it was concluded at 1000 hours | | on 9/2/99, that the out of tolerance condition likely existed from | | approximately 5/28/99 to 6/4/99. | | | | The out of tolerance condition affected 2 of the 3 probes (2 out of 3 logic | | required to activate the safety system). The as found data for the 2 probes | | indicated they would actuate at 6.70 pH and 6.63 pH, which is below the 7 pH | | required setpoint. A review of MFS operational history indicated that the | | MFS pH was maintained above a 7 pH during the time the probes are suspected | | to have been out of tolerance. | | | | There was no loss of hazardous/radioactive material or | | radioactive/radiological contamination. | | | | The NRC resident inspector has been notified. | | | | * * * UPDATE 1452EDT ON 9/2/99 FROM KURT SISLER TO S. SANDIN * * * | | | | The following is a portion of information provided as an update to include | | classification of the event as a 24-hour 91-01 Bulletin report: | | | | "Upon further review of [the] X-705 Microfiltration System pH probe failure, | | it was determined to be reportable per NRC Bulletin 91-01 criteria. | | | | "Safety Significance: | | | | "Two out of three safety system pH probes used in the microfiltration system | | were found to be out of tolerance. The system relies on a two-out-of-three | | logic for system actuation. The probes read 7.30 and 7.37 for a buffer | | solution which had a pH of approximately 7.0 (depending on the temperature). | | NCSA-0705_015.A10 takes credit for these pH probes in satisfying the double | | contingency principle. Active engineered feature #5 states 'Microfiltration | | effluent pH shutdown system will automatically stop the flow of microfilter | | permeate to the T-105 tank if pH<7.0 (with an allowable test tolerance of | | -0.2), by closing both isolation valves automatically.' Since the probes | | were overestimating the pH, a pH of as low as approximately 6.70 could be | | present without an actuation of the system. | | | | "Contingency event B.4.2 credits the effluent pH shutdown system in | | preventing dissolved uranium past the microfilters (to an unsafe geometry | | tank downstream). Also credited is the unlikely event of solution with a | | low pH making it to the microfiltration modules due to the functioning of | | the pH adjustment system. Therefore, the out of tolerance condition in a | | non-conservative direction constitutes a loss of one criticality control in | | a double contingency system. | | | | "The discussion for B.4.2 includes the following, 'Based on chemical | | reactions and calculations in POEF-340-98-113, it would require an extremely | | low pH (in the range of approximately 4 to 5) before the resulting solution | | would pick up any appreciable amounts (i.e., milligrams per liter) of | | uranium. However, this level of uranium is well below the individually | | always safe concentration limit reported in GAT-225, Rev. 4, of 5000 ppm | | U-235 for 100% enriched solution.' Based on the as-found tolerances, a pH | | of 6.70 would have caused the system to actuate. Therefore, this event has a | | low safety significance. | | | | "Potential Criticality Pathways involved (Brief scenario(s) of how | | criticality could occur): | | | | "Event B.4.2.a credits the effluent pH shutdown system in preventing | | dissolved uranium past the microfilters (to an unsafe geometry tank | | downstream). Also credited is the unlikely event of solution with a low pH | | making it to the microfiltration modules due to the functioning of the pH | | adjustment system. Both a failure in the pH shutdown system and the unlikely | | event of a low pH following pH adjustment would have to occur for this | | scenario to take place. | | | | "Controlled parameters: | | | | "The prevention of acidic solutions from entering the microfiltration | | modules maintains the uranium in the filters in a favorable geometry, rather | | than picking up uranium in addition to the safe batch being processed. | | Therefore, geometry is controlled. | | | | "Estimated Amount, Enrichment, Form of Licensed Material (include process | | limit and % worst case of critical mass): | | | | "The operation is approved for 100% U-235; however, only USEC material | | (maximum 10% U-235 has been processed recently. The microfiltration process | | is controlled such that only a safe mass of U-235 is present in any | | unfavorable geometry. Operational information indicates that the pH was | | never less than 7.0 during the time the system was potentially out of | | calibration | | | | "Nuclear Criticality Safety Controls(s) or control system(s) and description | | of failures or deficiencies: | | | | "Two out of three safety system pH probes used in the microfiltration system | | were found to be out of tolerance. The system relies on a two-out-of-three | | logic for system actuation. The system is relied on to keep unmeasured | | quantities of uranium (from the microfilter modules) from entering an | | unfavorable geometry tank. | | | | "Therefore, the failure of the pH shutdown system (due to out of calibration | | probes or any reason) is an analyzed condition." | | | | The HOO notified R3DO (Hills) and NMSS (Piccone). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36114 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 09/02/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 13:21[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 09/02/1999| +------------------------------------------------+EVENT TIME: 10:36[CDT]| | NRC NOTIFIED BY: D. COVEYOU |LAST UPDATE DATE: 09/02/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 93 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RPS ACTUATION - REACTOR SCRAM | | | | At 1036 CDT on 9/2/99, Unit 1 received an RPS Automatic Actuation. The | | actuation occurred due to low water level (12.5 inches, Level 3) resulting | | from a feedwater transient. The lowest level noted was -10 inches on the | | wide range recorders. No ECCS actuations occurred or were required during | | the transient. All systems operated as designed except as described below: | | During the auxiliary power fast bus transfer the Unit 1 station air | | compressor surged and was subsequently restored, the 0C clean condensate | | pump tripped and the 0A clean condensate pump was started, the 1A and 1C | | circulating water pumps tripped, the 1B circulating water pump remained | | running, actions are being taken to restart the 1A circulating water pump | | and a delay is being encountered restoring the 345 KV ring bus due to | | difficulties in opening the main power transformer disconnects. | | | | All rods inserted and no safety relief valves lifted. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36115 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 09/02/1999| | UNIT: [1] [] [] STATE: VT |NOTIFICATION TIME: 13:44[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 09/02/1999| +------------------------------------------------+EVENT TIME: 11:43[EDT]| | NRC NOTIFIED BY: ANDREW WISNIEWSKI |LAST UPDATE DATE: 09/02/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WILLIAM COOK R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ESF ACTUATION - PRIMARY CONTAINMENT ISOLATION SYSTEM (PCIS) GROUP III | | ISOLATION | | | | At 1143, on 9/2/99, the control room received a PCIS Group III isolation. A | | Group III isolation isolates all drywell atmospheric valves and reactor | | building ventilation. Standby gas treatment started. The cause of the | | isolation was the west refuel floor radiation monitor failing upscale. The | | actuation is considered invalid. | | | | Local radiation readings were verified less than 1 mR/hr. New fuel | | inspections will be secured prior to resetting the Group III isolation to | | allow reestablishing drywell to torus differential pressure which had been | | broken for vacuum breaker testing prior to the isolation. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36116 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BYRON REGION: 3 |NOTIFICATION DATE: 09/02/1999| | UNIT: [1] [2] [] STATE: IL |NOTIFICATION TIME: 16:02[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/02/1999| +------------------------------------------------+EVENT TIME: 11:17[CDT]| | NRC NOTIFIED BY: STEVEN RAMSEY |LAST UPDATE DATE: 09/02/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: |TAD MARSH NRR | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION | | | | At 1158 CDT, 9/2/99, the National Earthquake Information Center, Golden | | Colorado, reported that an earthquake occurred at 1117 CDT with an epicenter | | approximately 30 miles from the site. It was reported the earthquake | | occurred approximately 10 miles SSE of Dixon, Illinois at a magnitude of 3.5 | | on the Richter scale. Some minor tremors were felt by site personnel. | | There was no impact on plant operations. Plant seismic instrumentation did | | not detect this event. The instrumentation was tested and verified | | operable. At approximately 1400 CDT a presentation was made to the local | | media to address questions they had. | | | | The NRC resident has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36117 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 09/02/1999| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 17:51[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/02/1999| +------------------------------------------------+EVENT TIME: 16:00[CDT]| | NRC NOTIFIED BY: GREG JANAK |LAST UPDATE DATE: 09/02/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR REPORT - CONTROL ROOM ENVELOPE VENTILATION SYSTEM MAKEUP UNIT TRAIN | | 'C' INOPERABLE | | | | South Texas Project made the following notification per NPF-076, Section | | 2G: | | | | Carbon samples obtained from control room envelope ventilation system makeup | | unit train 'C' failed laboratory tests. The Technical Specification | | 4.7.7.c.2 limit of 1% for methyl iodine penetration was exceeded. The as | | found methyl iodine penetration results were 2.87%. This results in the | | train 'C' control room envelope system being inoperable since the time that | | the carbon samples were obtained on August 23, 1999 at 0940 CDT. This | | results in the system being inoperable for greater than 7 days which is a | | violation of Technical Specification 3.7.7 action a. The sample results | | were obtained on September 1, 1999 at 0935 CDT. | | | | The charcoal adsorber banks for train 'C' control room envelope system have | | been replaced and testing is in progress to verify system operability. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36118 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 09/02/1999| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 19:13[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 09/02/1999| +------------------------------------------------+EVENT TIME: 15:00[CDT]| | NRC NOTIFIED BY: DANIEL BOWERS |LAST UPDATE DATE: 09/02/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ACCIDENT MITIGATION | | | | On 3/15/99 and 4/29/99, surveillance test STS AE-001, Main Feedwater | | Isolation Valve Accumulator Discharge Test, was performed using a digital | | temperature indicator that was subsequently found to be out of calibration. | | The surveillance test ensures the nitrogen precharge is sufficient to close | | the main feedwater isolation valves. With the out of calibration | | temperature indication the nitrogen precharge may not have been adequate to | | close the valves. The surveillance test is performed monthly and has | | subsequently been performed using calibrated instruments. The feedwater | | isolation valves are currently operable. | | | | The NRC resident inspector will be notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36119 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 09/02/1999| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 19:51[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/01/1999| +------------------------------------------------+EVENT TIME: 19:49[CDT]| | NRC NOTIFIED BY: JOHN MILLIFF |LAST UPDATE DATE: 09/02/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE 24 HOUR REPORT FOR VIOLATION OF OPERATING LICENSE NPF-80 (2G) | | Section 2.C(2) | | | | Steam generator level channel L-0549 failed on 9/1/99 at 1529 CDT placing | | the unit in a one hour Limiting Condition for Operation per Technical | | Specifications. Action 20 of TS 3.3.2.6.d was entered and the channel | | bistables were tripped. It was determined the cause of the level channel | | failure could be manifested in the solid state protection system. At 1949 | | CDT the bistables were untripped to verify the operability of the solid | | state protection system. Unit 2 entered Technical Specification 3.0.3 for | | this condition. The input relay to the 'S' logic train for steam generator | | level channel L-0549 was determined to be the cause of the failed channel. | | Action 9 of Technical Specification 3.3.1.21 and action 22 of Technical | | Specification 3.3.2.6.b were entered at 2017 CDT to replace the failed | | relay. The relay was replaced and steam generator level channel L-0549 was | | declared operable at 2055 CDT. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36120 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 09/02/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 22:02[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 09/02/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 12:57[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 09/02/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |DAVID HILLS R3 | | DOCKET: 0707001 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MIKE UNDERWOOD | | | HQ OPS OFFICER: WILLIAM POERTNER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | |OCBC 76.120(c)(2)(iii) REDUNDANT EQUIP INOP | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR REPORT - SAFETY EQUIPMENT FAILURE | | | | At 1257 CDT on 9/2/99, during performance of a proceduralized simulated | | power failure test, the main breaker to the Unit 2 battery room tripped. In | | addition, the transformer secondary breakers on all four auxiliary | | substations tripped due to undervoltage relay action. As a result of the | | loss of power to the four auxiliary substations, three plant air compressors | | on-line in the C-335 air plant were deenergized. The unplanned loss of the | | C-335 air compressors caused the on-line plant air compressor capacity to | | drop to 6500 SCFM which is below the 10,250 SCFM required to ensure plant | | Criticality Accident Alarm System (CAAS) audibility. CAAS detectability | | was not affected. CAAS TSR LCO actions for inaudibility were initiated for | | affected facilities C-310, C-331, C-333, C-333A, C-335, C-337, C-337A, | | C-360, C-400, and C-409. The plant air capacity was restored to above | | 10,250 SCFM at 1300 hours by placing standby air compressors in service. | | The CAAS was declared operable at 1312 hours and the LCOs were exited. | | | | The licensee is still investigating the cause of the event. | | | | This event is reportable under 10CFR76.120(c)(2) as a event in which | | equipment required by the TSR is disabled or fails to function as designed. | | | | The NRC resident inspector has been notified. | +------------------------------------------------------------------------------+
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