Event Notification Report for July 30, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/29/1999 - 07/30/1999 ** EVENT NUMBERS ** 35889 35958 35971 35972 35973 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35889 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 07/02/1999| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 16:41[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 07/02/1999| +------------------------------------------------+EVENT TIME: 13:30[EDT]| | NRC NOTIFIED BY: HANK STRAHLEY |LAST UPDATE DATE: 07/29/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAWRENCE DOERFLEIN R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 15 Power Operation |15 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - RCIC SYSTEM DECLARED INOPERABLE - | | | | While performing Reactor Core Isolation Cooling (RCIC) System injection | | testing, the licensee declared the RCIC System inoperable due to problems | | with the system injection testable check valves. Valve #2ICS*AOV157 did not | | indicate open with full flow to the reactor vessel and valve #2ICS*AOV156 | | continued to indicate open following injection. The licensee declared these | | containment isolation valves inoperable and is taking actions to isolate the | | containment penetration. The RCIC System injected properly with the | | exception of the above noted problem. Otherwise, the RCIC System operated | | properly. Tech Spec 3.7.4 requires the licensee to restore the RCIC System | | to operable status within 14 days. The High Pressure Core Spray System is | | operable. The licensee will be troubleshooting these valves. | | | | The licensee informed the NRC Resident Inspector. | | | | * * * UPDATE AT 1028 ON 7/29/99, BY PITTS RECEIVED BY WEAVER * * * | | | | At 1330 on 7/2/99, report was made associated with the Reactor Core | | Isolation Cooling (RCIC) inoperability in accordance with | | 10CFR50.72(b)(2)(iii)(D). RCIC was declared inoperable due to problems with | | the injection testable check valves which are Primary Containment Isolation | | valves. 2ICS*AOV 156 continued to indicate open following injection and | | 2ICS*AOV 157 did not indicate open with full flow to the Reactor Vessel. | | These containment isolation valves were declared inoperable and actions were | | taken to isolate the containment penetration. RCIC injected properly when | | tested and injection capabilities were only effected by virtue of the | | necessity to comply with isolation requirements. | | | | RCIC testable check valves 21CS*AOV156 and 2ICS*AOV157 failing to properly | | close or indicate position are independent of the ability of RCIC to operate | | and perform its function. | | | | Based on the above, RCIC would have operated under all design conditions and | | was only incapacitated as a result of satisfying Primary Containment | | isolation functions. Therefore this is a retraction of notification made | | under 10CFR50.72(b)(2)(iii)(D) (See event notification # 35889). | | | | The licensee notified the NRC resident inspector and the Operations Center | | notified the R1DO (Kinneman). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35958 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 07/25/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 22:32[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 07/25/1999| +------------------------------------------------+EVENT TIME: 20:21[CDT]| | NRC NOTIFIED BY: WILLIAMS |LAST UPDATE DATE: 07/30/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |AUNA 50.72(b)(1)(ii)(A) UNANALYZED COND OP | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 87 Power Operation |87 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT ENTERED TECH SPEC 3.2.3 LCO ACTION STATEMENT | | | | AT 2021 CDT ON 07/25/99, THE "1B21-N500" PRESSURE TRANSMITTER INDICATION | | DROPPED FROM 1000 PSIG TO INDICATED 600 PSIG REACTOR PRESSURE. THIS | | TRANSMITTER IS THE PRIMARY PRESSURE TRANSMITTER TO THE ELECTROHYDRAULIC | | SYSTEM (EHC). DUE TO THIS CHANGE IN PRESSURE INDICATION, THE BACKUP | | TRANSMITTER TOOK CONTROL. IN THIS LINEUP (BACKUP TRANSMITTER IN CONTROL OF | | THE EHC), THERE IS NO OTHER BACKUP TRANSMITTER AVAILABLE AND PROCEDURE | | "LOA-EH-101" STATES THAT THIS CONDITION IS AN UNANALYZED CONDITION AND THE | | PLANT IS TO ENTER TS 3.2.3. TS 3.2.3 REQUIRES THE REACTOR TO BE <25% POWER | | WITHIN 4 HOURS. THIS CONDITION WAS NOT DETERMINED TO BE AN UNANALYZED | | CONDITION UNTIL 2045 CDT ON 07/25/99 UTILIZING THE ABOVE PROCEDURE AND THE | | UFSAR. THE PROBLEM WITH THE TRANSMITTER IS BEING INVESTIGATED TO DETERMINE | | WHY IT DOES NOT INDICATE 1000 PSIG. | | | | THE RESIDENT INSPECTOR WILL BE INFORMED. | | | | * * *RETRACTION 2253 7/29/99, FROM GRANWALD TAKEN BY STRANSKY * * * | | "It was subsequently determined from a detailed evaluation that was | | performed in May of 1999, which clearly shows that operation with a pressure | | regulator out of service at LaSalle is bounded by the thermal limits | | calculated for the slow closure of one or more turbine control valves | | (TCVs). The use of the thermal limits reported in the LaSalle Unit 1 Cycle | | 8 Core Operating Limits Report for the slow closure of one or more TCVs for | | operations with a pressure regulator out of service does not result in | | operation of the plant in an unanalyzed condition. The thermal limits were | | adjusted to be in line with the TCV slow closure analysis and plant thermal | | limits were declared OPERABLE and Tech Spec 3.2.3 exited within 4 hours. | | Therefore, LaSalle Unit 1 was not in an unanalyzed condition as reported in | | Event No.35958." | | | | The NRC resident inspector will be informed of this retraction by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 35971 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: VA COMMONWEALTH UNIVERSITY |NOTIFICATION DATE: 07/29/1999| |LICENSEE: VA COMMONWEALTH UNIVERSITY |NOTIFICATION TIME: 13:51[EDT]| | CITY: RICHMOND REGION: 2 |EVENT DATE: 07/23/1999| | COUNTY: STATE: VA |EVENT TIME: [EDT]| |LICENSE#: 45-00048-17 AGREEMENT: N |LAST UPDATE DATE: 07/29/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ROBERT HAAG R2 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: MARY BETH TAORMINAL | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION | | | | On 7/23/99, a medical misadministration occurred during a procedure | | involving a "Betacath" brachytherapy device with a strontium-90 source. Due | | to a problem with the catheter, a patient received only 2.26 Gy (226 rads) | | of the prescribed 14 Gy (1,400 rad) dose. The Betacath device is used during | | cardiac catherization to prevent restenosis of blood vessels. | | | | This event was reported to the licensee's radiation safety office on | | 7/29/99. The licensee has contacted the NRC Region II office regarding this | | event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35972 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PRAIRIE ISLAND REGION: 3 |NOTIFICATION DATE: 07/29/1999| | UNIT: [1] [2] [] STATE: MN |NOTIFICATION TIME: 17:59[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 07/29/1999| +------------------------------------------------+EVENT TIME: 16:40[CDT]| | NRC NOTIFIED BY: PAT RYAN |LAST UPDATE DATE: 07/29/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GEOFFREY WRIGHT R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTROL ROOM SPECIAL VENTILATION SYSTEM DECLARED INOPERABLE | | | | "At approximately 1640 on July 29, 1999, Plant Engineering discovered that a | | condition existed with door 158 (entry door to 122 Control Room Chiller | | Room) on 7/27/99 similar to a condition that existed on 6/25/99 that | | resulted in a LER. Further investigation concluded that the condition of | | door 158 on 7/27/99 was almost exactly the same as that on 6/25/99. Door 158 | | was identified as having a broken latch mechanism. The broken latch results | | in a breach of the Control Room Special Ventilation System, such that both | | trains are to be considered inoperable. | | | | "Interviews with duty people present during the 7/27/99 breach confirmed | | that the door latch was repaired well within an hour from its discovery and | | returned to service." | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | [HOO note: see related EN 35860] | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35973 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 07/30/1999| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 00:02[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 07/29/1999| +------------------------------------------------+EVENT TIME: 23:16[EDT]| | NRC NOTIFIED BY: ANTHONY PETRELLI |LAST UPDATE DATE: 07/30/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN KINNEMAN R1 | |10 CFR SECTION: | | |AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE CORE SPRAY INOPERABLE | | | | Check valve 2CSH*V16 on the High Pressure Core Spray pump suction from the | | suppression pool is not in the IST program plan for reverse flow testing. A | | preliminary review indicates that this check valve should be reverse flow | | tested. The HPCS was declared inoperable and the plant entered a 14 day | | LCO. Steps are being taken to retest the valve. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021