Event Notification Report for July 26, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/23/1999 - 07/26/1999 ** EVENT NUMBERS ** 31161 35867 35897 35948 35949 35950 35951 35952 35953 35954 35955 35956 35957 35958 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 31161 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CAP ENGINEERING CONSULTANTS |NOTIFICATION DATE: 10/16/1996| |LICENSEE: CAP ENGINEERING CONSULTANTS |NOTIFICATION TIME: 15:14[EDT]| | CITY: CORAL GABLES REGION: 2 |EVENT DATE: 10/15/1996| | COUNTY: POLK STATE: FL |EVENT TIME: 00:00[EDT]| |LICENSE#: FL-2611-1 AGREEMENT: Y |LAST UPDATE DATE: 07/23/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CAUDLE JULIAN RDO | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: REGION 2 (WOODRUFF) | | | HQ OPS OFFICER: RUDY KARSCH | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CAP ENGINEERING CONSULTANTS, CORAL GABLES, FL. | | | | A TROXLER MODEL 3440 MOISTURE DENSITY GAGE WAS STOLEN FROM THE BACK OF A | | PICKUP TRUCK. THE GAGE CONTAINED 9 mCi OF CESIUM-137 AND 44 mCi OF Am-Be. | | THE LICENSEE HOLDS A FLORIDA LICENSE AND REPORTED THE INCIDENT TO FLORIDA ON | | 10/15/96. REGION 2 (WOODRUFF) REPORTED THE EVENT TO THE OPERATIONS CENTER. | | REGION 2 IS ISSUING PN-072. | | | | * * * UPDATE AT 1405 ON 07/23/99 FROM EAKINS TO CHAUNCEY GOULD * * * | | | | THE STATE OF FLORIDA BUREAU OF RADIATION CONTROL WAS INFORMED ON 07/23/99 | | THAT THE STOLEN TROXLER MOISTURE DENSITY GAGE HAD BEEN RECOVERED IN WEBSTER, | | FL. SEE EVENT #35949 FOR ADDITIONAL DETAILS. THE NRC OPERATIONS OFFICER | | NOTIFIED R2DO (ED McALPINE) AND NMSS EO (DON COOL). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35867 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 06/26/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 05:28[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 06/26/1999| +------------------------------------------------+EVENT TIME: 04:03[EDT]| | NRC NOTIFIED BY: DOUGLAS AMTSFIELD |LAST UPDATE DATE: 07/23/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GLENN MEYER R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM INOPERABLE | | | | On 6-26-99 at 0403, the Unit 2 HPCI System was declared inoperable following | | performance of a routine test on the HPCI drain pot orifice. The purpose of | | the test is to verify flow through the HPCI turbine exhaust drain pot | | discharge line flow orifice. At the time of the failure the HPCI System was | | operable. The HPCI System was conservatively declared inoperable due to the | | potential for the exhaust line to fill. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE AT 1449 EDT ON 07/23/99 FROM STANLEY GAMBLE TO S. SANDIN * * * | | | | The licensee is retracting this report based on the following: | | | | The HPCI System was conservatively declared inoperable due to the potential | | for water to be present in the turbine as a result of a plugged flow orifice | | on the turbine exhaust drain pot drain line. The plugged orifice was | | discovered during performance of a test specifically designed to ensure that | | exhaust drain pot drain line flow path is operable. Testing is routinely | | scheduled the day following normal HPCI System surveillance testing since | | operation of the HPCI System is the initiator for plugging of the flow | | orifice. | | | | The basis for this retraction is that a minimal amount, less than one | | gallon, of condensate was drained from the exhaust drain pot when the flow | | orifice piping was disassembled. The amount of condensate was much less | | than the amount required to adversely impact HPCI System operability. It | | would require in excess of 40 gallons of condensate to fill the exhaust | | drain pot to a level that would result in condensate entering the turbine or | | exhaust line. Therefore, the HPCI System was operable and capable of | | performing its safety function until it was removed from service to clear | | the flow orifice. | | | | The licensee informed the NRC Resident Inspector. | | | | The NRC Operations Officer notified R1DO (Jim Noggle). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35897 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SURRY REGION: 2 |NOTIFICATION DATE: 07/06/1999| | UNIT: [] [2] [] STATE: VA |NOTIFICATION TIME: 02:44[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 07/06/1999| +------------------------------------------------+EVENT TIME: 02:04[EDT]| | NRC NOTIFIED BY: LISA HILBERT-SEMMES |LAST UPDATE DATE: 07/23/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PAUL FREDRICKSON R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Hot Shutdown |0 Intermediate Shut| | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MODE CHANGE INITIATED AS PART OF A TECHNICAL SPECIFICATION REQUIRED | | SHUTDOWN | | | | "At 1810 hours on 7-5-99, with Surry Power Station Unit 2 at Hot Shutdown | | (HSD) following a reactor trip, the 'A' Cold Leg Loop Stop Valve (Mark | | number 2-RC-MOV-2591) was removed from it's backseat in accordance with | | station procedure 2-GOP-2.4. Upon reopening the valve, full open indication | | was not received. In accordance with Technical Specification 3.17.1 and | | 3.0.1, a 30 hour clock to Cold Shutdown (CSD) LCO was started. The valve | | was de-energized by opening it's breaker. A cooldown to CSD was initiated | | at 2050 on 7-5-99. At 0204 on 7-6-99, a review of Station procedures and | | 10CFR50.72 determined that a one hour report was required for commencing the | | RCS cooldown in accordance with the Technical Specification LCO. | | | | "There were no radiation releases due to this event, nor were there any | | personnel injuries or contamination events. | | | | "Unit 2 is currently in Intermediate Shutdown with RCS cooldown in progress | | in accordance with station procedures. | | | | "Unit 1 was not affected by this event and remains stable at 100% power and | | 824 MWe. | | | | "This event is being reported in accordance with 10CFR50.72(b)(1)(i)(A)." | | | | The Licensee informed the NRC Resident Inspector. | | | | * * * UPDATE AT 0940 ON 07/23/99 FROM RAWLEIGH DILLARD TO JOLLIFFE * * * | | | | A review of NUREG 1022 with respect to 10CFR50.72(b)(1)(i)(A) provides the | | following clarification: "the phrase 'initiation of any nuclear plant | | shutdown' includes action to start reducing reactor power, i.e., adding | | negative reactivity to achieve a nuclear plant shutdown required by | | Technical Specifications. The 'initiation of any nuclear plant shutdown' | | does not include mode changes required by Technical Specifications if | | initiated after the plant is already in a shutdown condition." | | | | Unit 2 achieved Hot Shutdown Mode at 1122 on 07/05/99 after a reactor trip. | | Based on the information given above in NUREG 1022, a one hour report was | | not required for commencing the cooldown to Cold Shutdown Mode as this was a | | mode change after Unit 2 was already in a shutdown condition. The actions | | taken by the Licensee were prudent and represented a conservative decision | | by the Licensee. | | | | Thus, the Licensee desires to retract the above report based on the above | | discussion. | | | | The Licensee informed the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R2DO Ed McAlpine. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35948 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: OR DEPT OF HEALTH RAD PROTECTION |NOTIFICATION DATE: 07/23/1999| |LICENSEE: EUGENE SAND AND GRAVEL COMPANY |NOTIFICATION TIME: 12:06[EDT]| | CITY: EUGENE REGION: 4 |EVENT DATE: 07/22/1999| | COUNTY: STATE: OR |EVENT TIME: 16:26[PDT]| |LICENSE#: ORE-90643 AGREEMENT: Y |LAST UPDATE DATE: 07/23/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ELMO COLLINS R4 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WRIGHT | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TROXLER MOISTURE DENSITY GAUGE DAMAGED AT A FLORENCE, OR. JOBSITE | | | | A TROXLER MOISTURE DENSITY GAUGE SERIES 3400 CONTAINING 9 MILLICURIES OF | | CESIUM-137 AND 44 MILLICURIES OF AMERICIUM-241-BERYLLIUM WAS RUN OVER BY A | | PICKUP TRUCK. THE SOURCE ROD WAS IN THE STORAGE POSITION WHEN THE DEVICE | | WAS RUN OVER. THE ONLY DAMAGE APPEARS TO BE TO THE ELECTRONICS PORTION OF | | THE DEVICE. A PRELIMINARY SWIPE WAS TAKEN AND NO CONTAMINATION WAS | | DETERMINED. THE DEVICE IS BEING STORED AT THE LICENSEE'S FACILITY IN | | EUGENE, OREGON AWAITING TO BE SENT BACK TO THE MANUFACTURER. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35949 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA STATE WARNING POINT |NOTIFICATION DATE: 07/23/1999| |LICENSEE: CAP ENGINEERING CONSULTANTS |NOTIFICATION TIME: 12:46[EDT]| | CITY: WEBSTER REGION: 2 |EVENT DATE: 07/23/1999| | COUNTY: SUMTER STATE: FL |EVENT TIME: 12:00[EDT]| |LICENSE#: FL-2611-1 AGREEMENT: Y |LAST UPDATE DATE: 07/23/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |EDWARD MCALPINE R2 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: FLETCHER | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TROXLER MOISTURE DENSITY GAUGE FOUND IN WEBSTER, FL | | | | MELISSA SYLVEST, FL STATE WARNING POINT, REPORTED TO THE NATIONAL RESPONSE | | CENTER THAT A TROXLER MOISTURE DENSITY GAUGE, SERIAL #26065, WAS FOUND BY | | THE ROAD SIDE IN WEBSTER, FL. THE DEVICE DOES NOT APPEAR TO BE DAMAGED AND | | IS BEING HELD BY THE WEBSTER POLICE DEPARTMENT. THE LICENSEE FOR THE DEVICE | | IS CAP ENGINEERING CONSULTANTS. | | | | NATIONAL RESPONSE CENTER INCIDENT REPORT #492446. | | | | SEE EVENT #31161 FOR ADDITIONAL INFORMATION. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35950 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 07/23/1999| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 12:51[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 07/23/1999| +------------------------------------------------+EVENT TIME: 11:30[EDT]| | NRC NOTIFIED BY: T. McKEE |LAST UPDATE DATE: 07/23/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION OF A MINOR SEWAGE SPILL | | | | The licensee notified the New York State Department of Environmental | | Conservation of a 2-5 gallon sewage spill from the warehouse sewage pit to a | | storm drain. | | | | The licensee will inform the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35951 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NEW YORK CITY DEPT OF HEALTH |NOTIFICATION DATE: 07/23/1999| |LICENSEE: NEW YORK PRESBYTERIAN HOSPITAL |NOTIFICATION TIME: 13:20[EDT]| | CITY: NEW YORK REGION: 1 |EVENT DATE: 07/22/1999| | COUNTY: STATE: NY |EVENT TIME: 13:20[EDT]| |LICENSE#: 52-2960-11 AGREEMENT: Y |LAST UPDATE DATE: 07/23/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JAMES NOGGLE R1 | | |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: BORRI | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING SHIPMENT OF 10 MILLICURIES OF IODINE-131 | | | | NEW YORK PRESBYTERIAN HOSPITAL, NEW YORK CITY, RECEIVED A SHIPMENT OF 10 | | MILLICURIES OF IODINE -131 ON 07/20/99 FROM MDS NORDIAN, CANADA. THE SOURCE | | APPEARS TO BE MISSING AS OF 07/22/99. HOSPITAL PERSONNEL ARE SEARCHING FOR | | THE SHIPMENT AT THE HOSPITAL. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35952 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 07/23/1999| | UNIT: [1] [2] [] STATE: VA |NOTIFICATION TIME: 13:26[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 07/19/1999| +------------------------------------------------+EVENT TIME: 09:45[EDT]| | NRC NOTIFIED BY: MIKE WHALEN |LAST UPDATE DATE: 07/23/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |EDWARD MCALPINE R2 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A LICENSEE VOLUNTARY 24 HOUR NOTIFICATION IS BEING MADE TO REPORT AN INITIAL | | LACK OF INDEPENDENT ANALYSIS OF BORON CONCENTRATION SAMPLES. | | | | Dissolved boron concentration of the spent fuel pool and of the water added | | to the cavity of a sealed source storage cask is required to be within | | limits specified in ISFSI Technical Specification Section 3.2.1, Table 3-1 | | within 4 hours prior to commencing loading operations. The boron | | concentration is determined using chemical analysis of two samples analyzed | | by different individuals to reduce the risk that a single error could lead | | to not meeting the LCO. | | | | By procedure, Sample 1 is obtained from the spent fuel pool and from the | | cask pit by one technician. Sample 2 is then obtained from the spent fuel | | pool and from the cask pit by a different technician. Sample 1 is to be | | analyzed by the technician who obtained Sample 2 and vice versa. | | | | On 07/19/99, boron concentration sampling was performed prior to loading a | | spent fuel cask. Technician 1 obtained both cask pit samples and Technician | | 2 obtained both spent fuel pool samples. Technician 1 then analyzed both | | cask pit samples and Technician 2 analyzed both spent fuel pool samples. | | This is contrary to ISFSI Technical Specification Section 3.2.1. Upon | | realizing the lack of independence in analyzing the samples, Technician 1 | | analyzed the samples Technician 2 obtained and vice versa. Results of the | | analysis indicated acceptable dissolved boron concentrations. | | | | The Licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35953 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: OR DEPT OF HEALTH RAD PROTECTION |NOTIFICATION DATE: 07/23/1999| |LICENSEE: SMURFIT NEWSPRINT COMPANY |NOTIFICATION TIME: 14:52[EDT]| | CITY: OREGON CITY REGION: 4 |EVENT DATE: 07/07/1999| | COUNTY: STATE: OR |EVENT TIME: 10:49[PDT]| |LICENSE#: ORE-90296 AGREEMENT: Y |LAST UPDATE DATE: 07/23/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ELMO COLLINS R4 | | |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: WRIGHT | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STUCK SHUTTER ON A K-RAY LEVEL DETECTOR | | | | ON 07/16/99, A SMURFIT NEWSPRINT COMPANY REPRESENTATIVE NOTIFIED THE OREGON | | DEPARTMENT OF HEALTH RADIATION PROTECTION THAT THE SHUTTER ON A MODEL 7062B | | K-RAY LEVEL DETECTOR AT THE SMURFIT NEWSPRINT COMPANY FACILITY IN OREGON | | CITY, OREGON STUCK OPEN FOR UNKNOWN REASONS. THE DETECTOR IS LOCATED IN THE | | #5 TMP STEAMING TUBE/TANK WHICH IS USED FOR PROCESSING PAPER. A TN | | TECHNOLOGIES REPRESENTATIVE WILL GO TO THE PLANT TO REPLACE THE DETECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35954 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 07/23/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 17:04[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 07/23/1999| +------------------------------------------------+EVENT TIME: 15:58[EDT]| | NRC NOTIFIED BY: SIENCZAK |LAST UPDATE DATE: 07/23/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTO REACTOR SCRAM FROM 100% POWER DUE TO A HIGH FLUX SIGNAL | | | | DURING POST MAINTENANCE TESTING OF THE MECHANICAL PRESSURE REGULATOR, | | REACTOR PRESSURE OSCILLATIONS WERE EXPERIENCED AND AN AUTOMATIC REACTOR | | SCRAM OCCURRED FROM 100% POWER DUE TO A HIGH FLUX SIGNAL. ALL CONTROL RODS | | FULLY INSERTED AND NO SAFETY/RELIEF VALVES LIFTED. THE HIGH PRESSURE | | COOLANT INJECTION SYSTEM STARTED AS EXPECTED AND INJECTED FOR APPROXIMATELY | | 52 SECONDS BEFORE BEING SECURED. UNIT 1 IS STABLE IN HOT SHUTDOWN CONDITION | | AND COOLDOWN IS IN PROGRESS. ALL SYSTEMS APPEARED TO FUNCTION, AS | | DESIGNED. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35955 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 07/23/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 22:06[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 07/23/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 03:20[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 07/23/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |PATRICK HILAND R3 | | DOCKET: 0707002 |LARRY CAMPER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM McCLEERY | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC SHUTDOWN OF AUTOCLAVE #2 STEAM SYSTEM DUE TO HIGH CONDENSATE | | LEVEL | | | | AT 0320 ON 07/23/99, AUTOCLAVE #2, OPERATING IN MODE 2 (HEATING), | | EXPERIENCED A SAFETY SYSTEM SHUTDOWN WHEN BOTH CONDENSATE HIGH LEVEL PROBES | | ALARMED SHUTTING DOWN THE STEAM SYSTEM 20 MINUTES INTO THE HEATING CYCLE. | | THIS ACTUATION PLACED THE AUTOCLAVE INTO MODE 7 (SHUTDOWN) AND WAS DECLARED | | INOPERABLE BY THE PLANT SHIFT SUPERINTENDENT AT 0331. OPERATIONS PERSONNEL | | FOLLOWED ESTABLISHED ALARM RESPONSE PROCEDURES AND VERIFIED THE HIGH LEVEL | | ALARM ACTUATION AT 0430. AN ENGINEERING EVALUATION IS IN PROGRESS. | | | | THERE WAS NO LOSS OF HAZARDOUS OR RADIOACTIVE MATERIAL NOR RADIOACTIVE OR | | RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. | | | | THE NRC RESIDENT INSPECTOR AND THE DOE SITE REPRESENTATIVE HAVE BEEN | | NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35956 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 07/24/1999| | UNIT: [] [2] [3] STATE: IL |NOTIFICATION TIME: 13:34[EDT]| | RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 07/24/1999| +------------------------------------------------+EVENT TIME: 09:20[CDT]| | NRC NOTIFIED BY: GADBOIS |LAST UPDATE DATE: 07/24/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 57 Power Operation |57 Power Operation | |3 N Y 68 Power Operation |68 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO ILLINOIS EPA | | | | THE LICENSEE NOTIFIED THE ILLINOIS EPA AS REQUIRED BY NPDES PERMIT STANDARD | | CONDITION NO. 12(e)(1) OF AN UNANTICIPATED BYPASS OF THE DRESDEN STATION | | COOLING POND. THIS OCCURRED DUE TO A LIGHTNING STRIKE THAT CAUSED THE LOSS | | OF THE COOLING POND LIFT STATION. THE COOLING POND WAS PLACED ON BYPASS AT | | 2241 CDT ON 07/23/99. LIFT STATION OPERATION WAS RESTORED AND THE COOLING | | POND PLACED BACK ON INDIRECT OPEN CYCLE AT 0626 CDT ON 07/24/99. BOTH UNITS | | WERE PREVIOUSLY DERATED DUE TO THERMAL DISCHARGE LIMITATIONS. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35957 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 07/24/1999| | UNIT: [1] [] [] STATE: MD |NOTIFICATION TIME: 15:16[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 07/24/1999| +------------------------------------------------+EVENT TIME: 14:38[EDT]| | NRC NOTIFIED BY: PACE |LAST UPDATE DATE: 07/24/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES NOGGLE R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTO REACTOR TRIP FROM 100% POWER FOLLOWING A TURBINE TRIP. | | | | AN AUTO REACTOR TRIP OCCURRED FROM 100% POWER FOLLOWING A TURBINE TRIP WHICH | | OCCURRED FOLLOWING LOSS OF UNIT TRANSFORMER U25,000-12. IT APPEARS THAT THE | | TRANSFORMER FAULT PROTECTION ACTUATED DUE TO A POSSIBLE LIGHTNING STRIKE TO | | THE TRANSFORMER. THE FIRE DELUGE SYSTEM FOR THE TRANSFORMER ACTUATED, BUT | | THERE WAS NO EVIDENCE OF ANY FIRE, WITH THE EXCEPTION OF A SCORCHED PHASE | | BUSHING WHICH MAY HAVE BEEN THE RESULT OF A LIGHTNING STRIKE. THERE IS NO | | ESTIMATE OF THE EXTENT OF DAMAGE TO THE TRANSFORMER. ALL CONTROL RODS FULLY | | INSERTED, NO ECCS INJECTION OCCURRED AND NO SAFETY/RELIEF VALVES APPEARED TO | | HAVE LIFTED. THE CURRENT HEAT SINK IS THE MAIN CONDENSER. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35958 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 07/25/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 22:32[EDT]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 07/25/1999| +------------------------------------------------+EVENT TIME: 20:21[CDT]| | NRC NOTIFIED BY: WILLIAMS |LAST UPDATE DATE: 07/25/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PATRICK HILAND R3 | |10 CFR SECTION: | | |AUNA 50.72(b)(1)(ii)(A) UNANALYZED COND OP | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 87 Power Operation |87 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT ENTERED TECH SPEC 3.2.3 LCO ACTION STATEMENT | | | | AT 2021 CDT ON 07/25/99, THE "1B21-N500" PRESSURE TRANSMITTER INDICATION | | DROPPED FROM 1000 PSIG TO INDICATED 600 PSIG REACTOR PRESSURE. THIS | | TRANSMITTER IS THE PRIMARY PRESSURE TRANSMITTER TO THE ELECTROHYDRAULIC | | SYSTEM (EHC). DUE TO THIS CHANGE IN PRESSURE INDICATION, THE BACKUP | | TRANSMITTER TOOK CONTROL. IN THIS LINEUP (BACKUP TRANSMITTER IN CONTROL OF | | THE EHC), THERE IS NO OTHER BACKUP TRANSMITTER AVAILABLE AND PROCEDURE | | "LOA-EH-101" STATES THAT THIS CONDITION IS AN UNANALYZED CONDITION AND THE | | PLANT IS TO ENTER TS 3.2.3. TS 3.2.3 REQUIRES THE REACTOR TO BE <25% POWER | | WITHIN 4 HOURS. THIS CONDITION WAS NOT DETERMINED TO BE AN UNANALYZED | | CONDITION UNTIL 2045 CDT ON 07/25/99 UTILIZING THE ABOVE PROCEDURE AND THE | | UFSAR. THE PROBLEM WITH THE TRANSMITTER IS BEING INVESTIGATED TO DETERMINE | | WHY IT DOES NOT INDICATE 1000 PSIG. | | | | THE RESIDENT INSPECTOR WILL BE INFORMED. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021