Event Notification Report for July 7, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/06/1999 - 07/07/1999 ** EVENT NUMBERS ** 35897 35898 35899 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35897 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SURRY REGION: 2 |NOTIFICATION DATE: 07/06/1999| | UNIT: [] [2] [] STATE: VA |NOTIFICATION TIME: 02:44[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 07/06/1999| +------------------------------------------------+EVENT TIME: 02:04[EDT]| | NRC NOTIFIED BY: LISA HILBERT-SEMMES |LAST UPDATE DATE: 07/06/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PAUL FREDRICKSON R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Hot Shutdown |0 Intermediate Shut| | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MODE CHANGE INITIATED AS PART OF A TECHNICAL SPECIFICATION REQUIRED | | SHUTDOWN | | | | "At 1810 hours on 7-5-99, with Surry Power Station Unit 2 at Hot Shutdown | | (HSD) following a reactor trip, the 'A' Cold Leg Loop Stop Valve (Mark | | number 2-RC-MOV-2591) was removed from it's backseat in accordance with | | station procedure 2-GOP-2.4. Upon reopening the valve, full open indication | | was not received. In accordance with Technical Specification 3.17.1 and | | 3.0.1, a 30 hour clock to Cold Shutdown (CSD) LCO was started. The valve was | | de-energized by opening it's breaker. A cooldown to CSD was initiated at | | 2050 on 7-5-99. At 0204 on 7-6-99, a review of Station procedures and | | 10CFR50.72 determined that a one hour report was required for commencing the | | RCS cooldown in accordance with the Technical Specification LCO. | | | | "There were no radiation releases due to this event, nor were there any | | personnel injuries or contamination events. | | | | "Unit 2 is currently at Intermediate Shutdown with RCS cooldown in progress | | in accordance with station procedures. | | | | "Unit 1 was not affected by this event and remains stable at 100% power and | | 824 MWe. | | | | "This event is being reported in accordance with 10CFR50.72(b)(1)(i)(A)." | | | | The Licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35898 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 07/06/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 14:37[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 07/06/1999| +------------------------------------------------+EVENT TIME: 13:30[EDT]| | NRC NOTIFIED BY: DON ROLAND |LAST UPDATE DATE: 07/06/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JIM TRAPP R1 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DEGRADED/UNANALYZED CONDITION | | | | During a Unit 1 forced outage, the licensee determined that the 'C' outboard | | Main Steam Isolation Valve (MSIV) was unable to fully close. Based on the | | as-found valve configuration, it is believed that the MSIV volume would not | | reach required test pressure, therefore actual leak rate testing was not | | performed. This report documents exceeding overall MSIV maximum pathway | | acceptance criteria of 300 scfh. | | | | The licensee determined that the valve disc had separated from the stem. | | | | See Event 35884 for further information. | | | | The licensee has notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35899 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 07/07/1999| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 02:41[EDT]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 07/07/1999| +------------------------------------------------+EVENT TIME: 01:10[EDT]| | NRC NOTIFIED BY: MICHAEL DUNTON |LAST UPDATE DATE: 07/07/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK LESSER R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 15 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR TRIP DUE TO LOSS OF MAIN FEEDWATER | | | | The unit automatically tripped due to the loss of all main feedwater flow | | after the main feedwater pump tripped on low suction pressure. All control | | rods inserted following the trip. Emergency feedwater actuated as | | expected. | | | | The licensee reported that two main steam relief valves remained open | | following the trip, but reclosed after steam generator pressure was reduced | | to 920 psig. The unit is currently stable in Hot Standby, with steam | | generator levels being maintained by the motor driven emergency feedwater | | pumps, and decay heat being relieved to the main condenser via the turbine | | bypass valves. | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021