Event Notification Report for June 28, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/25/1999 - 06/28/1999 ** EVENT NUMBERS ** 35790 35856 35860 35861 35862 35863 35864 35865 35866 35867 35868 35869 35870 35871 35872 35873 35874 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35790 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/03/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:44[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/02/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:30[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/25/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |DAVID HILLS R3 | | DOCKET: 0707001 |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: THOMAS WHITE | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THREE SPRINKLER SYSTEMS DECLARED INOPERABLE DUE TO CORRODED HEADS (24-hour | | report) | | | | The following text is a portion of a facsimile received from Paducah: | | | | "On 06/02/99 at 1630 CDT, the Plant Shift Superintendent (PSS) was notified | | that numerous sprinkler heads were corroded, affecting 16 sprinkler systems | | in C-337 and one system in C-333, such that the ability of the sprinklers to | | flow sufficient water was called into question. Subsequently, these | | sprinkler systems were declared inoperable, and TSR-required actions | | establishing roving fire patrols were initiated. This deficiency was | | detected during scheduled system inspections conducted by Fire Protection | | personnel. Currently, functionality of the sprinkler heads has not been | | fully evaluated by Fire Protection personnel, and the remaining cascade | | buildings are currently being inspected, and if necessary, this report will | | be updated to identify any additional areas. | | | | "It has been determined that this event is reportable under | | 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to | | function as designed." | | | | The NRC resident inspector has been notified of this event. | | | | ******************** UPDATE RECEIVED AT 1022 EDT ON 06/04/99 FROM CAGE TO | | TROCINE ******************* | | | | The following text is a portion of a facsimile received from Paducah: | | | | "Two sprinkle heads on system D-1 in C-337 and two sprinkler heads on system | | 27 in C-335 were identified to also be corroded. These were identified to | | the PSS on 06/03/99 at 1600 CDT and 1601 CDT, respectively, and determined | | to require an update to this report by the PSS. | | | | "It has been determined that this event is reportable under | | 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to | | function as designed." | | | | Paducah personnel notified the NRC resident inspector of this update. The | | NRC operations officer notified the R3DO (Hills) and NMSS EO (Combs). | | | | *********** UPDATE RECEIVED AT 2152 EDT ON 06/17/99 FROM WALKER TO POERTNER | | *********** | | | | The following text is a portion of a facsimile received from Paducah: | | | | "Three sprinkler heads on system C-15 and five sprinkler heads on system B-8 | | in C-333 were identified to also be corroded. The PSS was notified of this | | condition at 1300 CDT on 06/17/99 and determined that an update to this | | report was required." | | | | "It has been determined that this event is reportable under | | 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to | | function as designed." | | | | Paducah personnel notified the NRC resident inspector of this update. The | | NRC operations officer notified the R3DO (Madera). | | | | * * * UPDATE AT 1440 ON 06/18/99 FROM UNDERWOOD TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on system C-15 and one sprinkler head on system B-8 in | | C-333 were identified to have corrosion. The PSS was notified of this | | condition at 1350 CDT on 06/18/99. The area of the fire patrol for system | | C-15 was expanded to include the two heads identified as corroded. The one | | head on system B-8 was in the area already being patrolled. The PSS | | determined that an update to this report was required." | | | | The NRC resident inspector has been informed of this update. The NRC | | operations officer notified R3DO (Madera). | | | | * * * UPDATE 1315 6/25/1999 FROM WALKER TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on system D-8 and three sprinkler heads on system D-7 | | in C-337 were identified to have corrosion. The PSS was notified of the | | condition on system D-8 at 0125 on 6/25/99 and at 1019 on 6/25/99 for system | | D-7. Both systems were immediately declared inoperable and LCO fire patrol | | actions were implemented. It was determined that an update to this report | | was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Jordan). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 35856 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: U.S. VETERANS ADMINISTRATION |NOTIFICATION DATE: 06/24/1999| |LICENSEE: DURHAM VA HOSPITAL |NOTIFICATION TIME: 15:00[EDT]| | CITY: DURHAM REGION: 2 |EVENT DATE: 05/28/1999| | COUNTY: STATE: NC |EVENT TIME: 12:00[EDT]| |LICENSE#: 32-01134-01 AGREEMENT: Y |LAST UPDATE DATE: 06/25/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |AL BELISLE R2 | | |FRED COMBS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: LYNN McGUIRE | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF IODINE-125 SEEDS INTO SANITARY SEWER | | | | "On May 28, 1999, two I-125 sources, with a combined activity of 0.584 mCi, | | were lost from the Medical Center. The seeds had been implanted into a | | patient's prostate earlier in the day. The patient had been instructed to | | save his urine so that any seeds passed in the urine could be recovered. An | | instruction sheet was posted on the door, directing that all urine, trash | | and linen be saved, and nurses had been trained for the procedure. A nurse | | called nuclear medicine to report that two seeds were in the urine | | container. When nuclear medicine personnel arrived to recover the seeds, | | the urine had been flushed into the sanitary sewer by another staff member | | on the floor. | | | | "The toilet and urine container were surveyed with a portable low-energy | | gamma detector, and no residual activity was detected. The sources are | | presumed to have gone into the sewer, and assuming the seeds remain covered | | by water, no significant exposure is expected to any individual member of | | the public. On June 1, 1999, the loss of the sources was reported by phone | | to the VA National Health Physics Program. | | | | "In order to prevent recurrence of this type of incident, the nurses on ward | | 7A have been retrained in the proper procedures. In the future, implant | | patient rooms will be posted with larger signs saying 'hold urine, trash, | | linen'." | | | | * * * UPDATE AT 0950 EDT ON 6/25/99 BY KELLY MAYO TO FANGIE JONES * * * | | | | Corrected reporting criteria from 10 CFR 20.2201(a)(1)(i) to 10 CFR | | 20.2201(a)(1)(ii) as the activity was more than 10 times the limit, but less | | than 1000 times the limit. Notified the R2DO (Al Belisle) and NMSS (Larry | | Camper).. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35860 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PRAIRIE ISLAND REGION: 3 |NOTIFICATION DATE: 06/25/1999| | UNIT: [1] [2] [] STATE: MN |NOTIFICATION TIME: 14:32[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 06/25/1999| +------------------------------------------------+EVENT TIME: 10:23[CDT]| | NRC NOTIFIED BY: RICK PEARSON |LAST UPDATE DATE: 06/25/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE JORDAN R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - CONTROL ROOM VENTILATION SYSTEM INOPERABLE DUE TO A BROKEN DOOR LATCH | | MECHANISM - | | | | AT 1023 CDT ON 06/25/99, WITH BOTH UNITS AT 100% POWER, THE LICENSEE | | DISCOVERED THAT PERSONNEL ENTRY DOOR #158 TO CONTROL ROOM CHILLER ROOM #122 | | HAD A BROKEN LATCH MECHANISM ON IT. THIS CONSTITUTES A BREACH OF THE | | CONTROL ROOM SPECIAL VENTILATION SYSTEM AND THUS, BOTH TRAINS OF THE CONTROL | | ROOM SPECIAL VENTILATION SYSTEM ARE INOPERABLE (TECH SPEC 3.13.A.1). | | | | AT 1121 CDT ON 06/25/99, PLANT TECHNICIANS REPAIRED THE BROKEN DOOR LATCH | | MECHANISM AND DECLARED THE VENTILATION SYSTEM OPERABLE. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35861 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 06/25/1999| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 15:23[EDT]| | RXTYPE: [2] GE-4 |EVENT DATE: 06/25/1999| +------------------------------------------------+EVENT TIME: 14:30[EDT]| | NRC NOTIFIED BY: STEVE MAREK |LAST UPDATE DATE: 06/25/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |MIKE JORDAN R3 | |10 CFR SECTION: |ROBERT DENNIG NRR | |AAEC 50.72 (a) (1) (I) EMERGENCY DECLARED |JOSEPH GIITTER IRO | |AENS 50.72(b)(1)(v) ENS INOPERABLE |CANUPP FEMA | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 97 Power Operation |97 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO LOSS OF TELEPHONE SERVICE | | | | "At 1430, Fermi 2 determined that the Emergency Notification System (ENS) | | phones were not available. The local telephone company notified Fermi 2 that | | an offsite fiber optic cable was cut. Additionally, local phone service to | | Monroe County, including the Monroe County Sheriffs Department is | | unavailable. Security radio communication to the Monroe County Sheriff is | | available and has been verified. RERP phone service to locations outside | | Monroe County is available. | | | | "This report is being made in accordance with 10CFR50.72(b)(1)(v), as an | | event that results in a major loss of emergency response assessment | | capability, or communications capability. | | | | "At 1508, an Unusual Event was declared due to notification that the | | Emergency Call Out System (ECOS) may also be impaired, due to the loss of | | local phones." | | | | The NRC resident inspector has been informed of this notification. | | | | * * * UPDATE 1844 6/25/99 FROM MAREK TAKEN BY STRANSKY * * * | | | | The Unusual Event was terminated at 1838 after the ENS and offsite telephone | | service were restored. The licensee will inform the NRC resident inspector | | of this update. Notified R3DO(Jordan), NRR EO (Hannon), FEMA (Sullivan). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35862 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: ABB COMBUSTION ENGINEERING |NOTIFICATION DATE: 06/25/1999| |LICENSEE: ABB COMBUSTION ENGINEERING |NOTIFICATION TIME: 16:34[EDT]| | CITY: WINDSOR REGION: 1 |EVENT DATE: 06/25/1999| | COUNTY: STATE: CT |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 06/25/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GLENN MEYER R1 | | |VERN HODGE (via fax) NRR | +------------------------------------------------+ | | NRC NOTIFIED BY: IAN RICKARD | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 10 CFR PART 21 REPORT REGARDING ABB 4kV CIRCUIT BREAKERS | | | | The following text is excerpted from a facsimile received in the Operations | | Center: | | | | "The defect concerns ABB 1200A 4KV Vacuum Breakers delivered to Baltimore | | Gas and Electric Company's Calvert Cliffs Nuclear Power Plant. Specifically, | | the defect concerns the breaker performing a trip free operation when a | | close signal is received by the breaker. This defect results in the breaker | | failing to remain in the closed position. The defect could lead to | | non-conservative failure of not starting certain plant equipment upon demand | | such as an Emergency Core Cooling Pump." | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35863 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 06/25/1999| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 18:52[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 06/25/1999| +------------------------------------------------+EVENT TIME: 09:30[CDT]| | NRC NOTIFIED BY: RICK HUBBARD |LAST UPDATE DATE: 06/27/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOSEPH TAPIA R4 | |10 CFR SECTION: | | |BAE1 20.2202(b)(1) PERS OVEREXPOSURE | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PERSONNEL OVEREXPOSURE | | | | A worker received internal contamination resulting in an estimated total | | effective dose equivalent (TEDE) of 14.5 rem (145 mSv). The individual had | | been involved in decontamination activities on the 1974' elevation of the | | auxiliary building, in the valve gallery of the Boron Thermal Regeneration | | System room. Upon exiting the area, significant contamination was detected | | on the individual's face (up to 80,000 dpm on the right side of the face). | | The individual was decontaminated and a whole body count was performed. The | | whole body count indicated the presence of cobalt-58 contamination in the | | individual's gastrointestinal tract. Whole body counts were given to other | | individuals who had been working in the same area, but no additional | | internal contamination was discovered. | | | | The licensee has issued a stop work order for all work areas with | | contamination levels in excess of 50,000 dpm, except those with specific | | approval from the Radiation Protection Manager. The licensee is also | | forming an Incident Investigation Team to determine the root cause of this | | event. The NRC resident inspector has been informed of this event by the | | licensee. | | | | | | * * * UPDATE AT 0920 ON 6/26/99, BY HUBBARD TAKEN BY WEAVER * * * | | The licensee has notified the State of this event and also issued a press | | release. HOO notified R4DO (Tapia). | | | | * * * COMMISSIONERS ASSISTANTS BRIEFING 2000 6/26/99 * * * | | | | A Commissioners Assistants briefing was held regarding this event. | | Participants: NRR (Donahue, Richards, Zwolinski), Region IV (Brockman, | | Brush, Hackney, Good, Ricketson, Henderson, Graves-briefer), NMSS (Cool), | | OCA (Madden), OPA (Gilliland), OSP (Sollenberger), EDO (Knapp, Lange), IRO | | (Giitter), Chm Jackson (Johnson), Comm Merrifield (McCabe), Comm Dicus | | (Lubenau), Comm McGaffigan (Crockett), Comm Diaz (Castleman). | | | | * * * RETRACTED AT 1751 EDT ON 6/27/99 BY RICK HUBBARD TO FANGIE JONES * * | | * | | | | Further reviews of this event identified a significant error in the | | original dose calculations which were the basis of the report. The error | | was in the use of a software generated activity rather than actual activity, | | a matter of using the wrong column's information in the calculations. Using | | the correct value, the internal exposure is estimated to be 2 mRem. The | | external exposure received by the individual on that work activity was 5 | | mRem. The assigned total effective dose equivalent (TEDE) is a combination | | of the internal and external exposures. Therefore, when corrected, the | | TEDE is estimated to be approximately 7 mRem versus the 14.5 Rem reported on | | June 25, 1999. | | | | The exposure of the individual involved in the June 25 decontamination | | evolution was well below regulatory limits and, therefore, does not meet the | | reporting requirements. Therefore, Event Notification # 35863 is being | | retracted. | | | | The licensee notified the NRC Resident Inspector for the Wolf Creek | | Generating Station and will also notify the State of Kansas and the media. | | The Headquarters Operations Officer notified the R4DO (Joseph Tapia). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35864 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 06/25/1999| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 18:57[EDT]| | RXTYPE: [3] CE |EVENT DATE: 06/25/1999| +------------------------------------------------+EVENT TIME: 17:45[CDT]| | NRC NOTIFIED BY: ARTHUR WEMETT |LAST UPDATE DATE: 06/25/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOSEPH TAPIA R4 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF LICENSEE TO SUBMIT CHANGES TO LICENSING BASIS FOR NRC REVIEW | | | | On 6/25/99, the NRC notified the licensee that the use of equipment failure | | probabilities (TORMIS) in the assessment of tornado and missile effects on | | the emergency feedwater (EFW) system constitutes a change to the licensing | | and design bases of the system. Such changes to the licensing and design | | bases constitute an Unreviewed Safety Question (USQ) and require formal NRC | | review and approval in accordance with 10 CFR 50.90. The licensee has | | decided not to contest the conclusion by the NRC. | | | | An engineering evaluation had previously been performed to postulate the | | effects of tornado winds and missiles on the EFW pump turbine steam supply | | piping and steam exhaust stack. The evaluation concluded that the results | | were acceptable, based on criteria provided in NRC Regulatory Guide 1.117. | | Based upon this evaluation, the licensee has concluded that the EFW system | | is operable with respect to its design basis functions, including the | | effects of tornado winds and missiles. | | | | The licensee plans to submit a formal license amendment request in | | accordance with 10 CFR 50.90 to incorporate the use of TORMIS. The NRC | | resident inspector has been informed of this notification by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35865 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 06/25/1999| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 22:30[EDT]| | RXTYPE: [2] GE-4 |EVENT DATE: 06/25/1999| +------------------------------------------------+EVENT TIME: 19:28[EDT]| | NRC NOTIFIED BY: R. PIZARRO |LAST UPDATE DATE: 06/25/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE JORDAN R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 97 Power Operation |97 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI SYSTEM DECLARED INOPERABLE | | | | The licensee declared the high pressure coolant injection (HPCI) system | | inoperable after the manual/automatic flow controller (E41-R614) was found | | to be indicating full downscale. The cause of the problem is currently | | under investigation. The licensee entered Technical Specification 3.5.1.c, | | and verified that all other emergency core cooling systems are operable. | | Although the HPCI flow controller would be unable to automatically control | | system flow, the licensee believes that operators would be able to control | | system flow manually, if needed. | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35866 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 06/25/1999| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 23:08[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/25/1999| +------------------------------------------------+EVENT TIME: 20:30[EDT]| | NRC NOTIFIED BY: DAN ETHERIDGE |LAST UPDATE DATE: 06/25/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE JORDAN R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY DIESEL GENERATOR DECLARED INOPERABLE | | | | "The Diesel Generator Fuel Oil System is designed to provide the required | | amount of diesel fuel to operate the EDGs on each unit for a minimum of | | seven days at the full load capacity of the generators. Two fuel oil | | transfer pumps are provided for each EDG to transfer diesel fuel from the | | storage tank to the fuel oil day tank. From each day tank, the fuel oil | | flows by gravity into the suction of the engine-driven fuel pump. The pump | | provides nine gpm at 35 psig and discharges through a duplex fuel oil filter | | into the two fuel oil supply manifolds. | | | | "Some of the fuel oil which flows from the supply manifold into the | | injection pump is not delivered to the spray nozzle. This excess fuel oil | | circulates through the injection pump, cooling the injection pump, and | | providing lubrication for the fuel oil side of the pump. The fuel oil then | | flows to the return manifold. To maintain a fixed pressure in the supply | | manifold, a relief valve at the end of each supply manifold (SV-200 set at | | 25 psig) bypasses fuel oil to the return manifold. | | | | "On 6/25/99, during routine inspection of the fuel oil lines, it was | | discovered that SV-200 on one of the Unit 1 EDGs was installed backwards, | | effectively blocking the safety valve from relieving excess pressure on the | | supply manifold. This configuration may have existed since initial | | construction. The EDG has been operated successfully many times with this | | condition, but uncertainty about the ability to operate for 7 days, | | especially at low loads, has caused the EDG to be declared inoperable and | | prompted this 4 hour NRC notification. The EDG remains available and will be | | repaired at the earliest opportunity." | | | | The licensee will inform the NRC resident inspector of this notification. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35867 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 06/26/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 05:28[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 06/26/1999| +------------------------------------------------+EVENT TIME: 04:03[EDT]| | NRC NOTIFIED BY: DOUGLAS AMTSFIELD |LAST UPDATE DATE: 06/26/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GLENN MEYER R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI INOPERABLE | | | | On 6-26-99, at 0403 the unit 2 HPCI System was declared inoperable following | | performance of a routine test on the HPCI drain pot orifice. The purpose of | | the test is to verify flow through the HPCI turbine exhaust drain pot | | discharge line flow orifice. At the time of the failure HPCI was operable. | | The HPCI system was conservatively declared inoperable due to the potential | | for the exhaust line to fill. The licensee notified the NRC resident | | inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35868 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/26/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 10:44[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/26/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 08:30[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/26/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MIKE JORDAN R3 | | DOCKET: 0707002 | | +------------------------------------------------+ | | NRC NOTIFIED BY: KURT SISLER | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NOTIFICATION OF ANOTHER FEDERAL AGENCY | | | | The licensee notified the DOE of an event in the X-705 building annex | | cylinder cleaning area. While attempting to clean an empty 8" cylinder it | | was discovered that the cylinder would not fit into the cadmium shield. It | | was later discovered that the NCSA had been based on a cylinder design which | | was slightly smaller than the older cylinder which caused the problem. A | | new NCSA will be performed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35869 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: THREE MILE ISLAND REGION: 1 |NOTIFICATION DATE: 06/26/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 13:18[EDT]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP |EVENT DATE: 06/26/1999| +------------------------------------------------+EVENT TIME: 10:08[EDT]| | NRC NOTIFIED BY: BLAIR |LAST UPDATE DATE: 06/26/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KURT COWGILL R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EDG STARTED AND LOADED DUE TO LOSS OF AUXILIARY TRANSFORMER | | | | At 1008, the '1B' 230 kV auxiliary transformer failed for unknown reasons. | | The '1A' emergency diesel generator (EDG) automatically started and loaded | | to its associated 4kV emergency bus. The unit is currently stable at 100% | | power. The licensee stated that EDG will remain loaded to its emergency bus | | until the auxiliary transformer can be restored to service. The NRC | | resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35870 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/26/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 18:49[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/25/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 20:30[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/26/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MIKE JORDAN R3 | | DOCKET: 0707002 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KURT SISLER | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01 REPORT | | | | "ON 6/25/99 PLANT PERSONNEL PERFORMING A WALKDOWN OF X-744L (STOREROOM) TO | | ENSURE COMPLIANCE WITH NCSA-PLANT046 'CONTAMINATED METAL' DISCOVERED PALLETS | | OF VACUUM PUMPS (3-4 pumps) STACKED FOUR TO A PALLET ON STORAGE RACKS WITHIN | | A CONTAMINATION STORAGE AREA. THE PUMPS ARE CONTAMINATED BUT THERE IS NO | | DOCUMENTATION IMMEDIATELY AVAILABLE IDENTIFYING THE URANIUM CONCENTRATION IN | | THESE PUMPS. THIS BUILDING HAS PREVIOUSLY BEEN SCANNED BY THE APPLIED | | NUCLEAR TECHNOLOGY GROUP FOR NDT ANALYSIS OF THE MATERIAL. WITHOUT THIS | | DOCUMENTATION READILY AVAILABLE THE NCSA REQUIRES THE MATERIAL TO BE SPACED | | AT A MINIMUM TWO FOOT EDGE-TO-EDGE SPACING. THIS IS A VIOLATION OF ONE | | CONTROL (SPACING) OF THE DOUBLE CONTINGENCY MATRIX. THE OTHER CONTROL VOLUME | | WAS MAINTAINED." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35871 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/26/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 19:04[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/26/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 05:33[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/26/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MIKE JORDAN R3 | | DOCKET: 0707002 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DALE NOEL | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MOTOR STOP BUTTON FAILED TO FUNCTION AS DESIGNED | | | | "ON 6/26/99 AT 0533 HOURS, THE X-333 PROCESS BUILDING AREA CONTROL ROOM | | (ACR) #1 MOTOR STOP BUTTON FAILED TO FUNCTION AS DESIGNED WHEN CALLED UPON | | TO SHUTDOWN MOTORS ON CELL 33-5-10 (CASCADE OPERATIONAL MODE Ill). THIS | | REPRESENTS THE FAILURE OF TECHNICAL SAFETY REQUIREMENT (TSR) SURVEILLANCE | | 2.2.3.14.3 FOR CASCADE D.C. CONTROL POWER WHICH STATES: 'UTILIZE THE ACR | | MOTOR STOP BUTTON FOR EACH SCHEDULED CELL TRIP. MONITOR EXPECTED CELL BLOCK | | VALVE CLOSURE AND ANY RECYCLE VALVE ACTUATION.' OPERATIONS PERSONNEL | | IMMEDIATELY UTILIZED AN ALTERNATE MEANS LOCATED AT THE CELLS LOCAL CONTROL | | CENTER (LCC) TO TRIP CELL 33-5-10 MOTORS. | | | | "THIS EVENT IS REPORTABLE DUE TO A SAFETY SYSTEM COMPONENT (SSC) REQUIRED BY | | THE TSR NOT BEING AVAILABLE OR OPERABLE AND NO REDUNDANT EQUIPMENT WAS | | AVAILABLE TO PERFORM THE REQUIRED SAFETY FUNCTION. | | | | "THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35872 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 06/27/1999| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 14:00[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/27/1999| +------------------------------------------------+EVENT TIME: 11:00[CDT]| | NRC NOTIFIED BY: ROBERT BRINKLEY |LAST UPDATE DATE: 06/27/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOSEPH TAPIA R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR PROTECTION SYSTEM ACTUATION RESULTING IN REACTOR TRIP | | | | The unit had a reactor trip from OTDeltaT, all control rods fully inserted. | | Auxiliary Feedwater, an Engineered Safety Features (ESF) system, | | automatically started on low steam generator level and feedwater isolation, | | as expected. The pressurizer power operated relief valves lifted on the | | reactor trip and then reseated. Also, some steam generator safeties lifted | | momentarily and reseated, the steam dumps to the condenser are operating to | | remove excess energy. The plant is stable in Hot Standby. | | | | All systems functioned as required, the only unexpected action was the trip | | of both main feedwater pumps on overspeed during the transient. The cause | | of the reactor trip is being investigation, a turbine trip is suspected. | | The trip of the feed pumps is also under review. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35873 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 06/27/1999| | UNIT: [1] [2] [] STATE: AL |NOTIFICATION TIME: 18:21[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 06/27/1999| +------------------------------------------------+EVENT TIME: 16:55[CDT]| | NRC NOTIFIED BY: VAUDY HOLLEY |LAST UPDATE DATE: 06/27/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF OFFSITE COMMUNICATION SYSTEM - TONE ALERT RADIO | | | | After thunderstorms moved through the area of the plant, the licensee | | discovered that communications with the meteorological tower had been lost | | and the tone alert radio system was unavailable for greater than 15 minutes, | | part of the public communication (warning) system. | | | | Workers have been called in to investigate and repair the systems that have | | been lost. | | | | The licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35874 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 06/28/1999| | UNIT: [] [2] [] STATE: GA |NOTIFICATION TIME: 03:55[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 06/28/1999| +------------------------------------------------+EVENT TIME: 03:00[EDT]| | NRC NOTIFIED BY: FRANK GORLEY |LAST UPDATE DATE: 06/28/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM ON LOW REACTOR WATER LEVEL | | | | The reactor automatically scrammed on low reactor vessel water level because | | of maintenance activities on the 'B' level keep fill system. Operators | | venting the keep fill system unintentionally vented the 'B' reference leg | | because the isolation valve between the two system is apparently leaking. | | This venting caused level instruments using the 'B' reference leg to | | indicate high. The mismatch on level indicators caused the feed system to | | switch to the 'B' leg (which happened to be the failed system). This | | resulted in a decrease in feed flow and an actual decrease in reactor vessel | | water level. | | | | The decrease in reactor water level caused a reactor scram and High Pressure | | Coolant Injection (HPCI) initiation. Reactor Core Isolation Cooling (RCIC) | | did not initiate because it uses the 'B' reference leg as an input. | | All control rods fully inserted. The plant is stable in mode 3. Water | | level has been restored to the normal band and is being maintained by the | | feed system. The recirculating pumps are operating and no safety relief | | valves lifted. The lowest indicated level was -45". | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021