Event Notification Report for June 24, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/23/1999 - 06/24/1999 ** EVENT NUMBERS ** 35000 35849 35852 35853 35854 35855 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35000 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DAVIS BESSE REGION: 3 |NOTIFICATION DATE: 11/05/1998| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 11:57[EST]| | RXTYPE: [1] B&W-R-LP |EVENT DATE: 11/05/1998| +------------------------------------------------+EVENT TIME: 11:07[EST]| | NRC NOTIFIED BY: JOHN BALDWIN |LAST UPDATE DATE: 06/23/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF DESIGN OVERSTRESS CONDITION IN PRESSURIZER NOZZLES | | | | THE LICENSEE HAS DETERMINED (VIA ENGINEERING CALCULATION C-ME-064.085.01) | | THAT A DESIGN OVERSTRESS CONDITION EXISTED IN THE PRESSURIZER SAFETY VALVE | | NOZZLES DURING THE PERIOD FROM 7/22/87 (INSTALLATION OF PLANT MODIFICATION | | 87-1001, WHICH INCREASED RUPTURE DISC BURST PRESSURE) UNTIL 10/17/98 (PLANT | | MODIFICATION TM 98-0036, WHICH REMOVED THE RUPTURE DISCS). BASED UPON THE | | OVERSTRESS CONDITION, THESE PRESSURIZER NOZZLES WERE NOT FUNCTIONAL DURING | | THAT TIME. HOWEVER, WITH THE RUPTURE DISCS REMOVED, THE LICENSEE HAS | | DETERMINED THAT STRESS LEVELS REMAIN WITHIN USAR DEFINED ALLOWABLE VALUES | | FOR ALL LOAD COMBINATIONS. | | | | THE NRC RESIDENT INSPECTOR HAS BEEN INFORMED. | | | | *** UPDATE ON 6/23/99 @ 1326 BY MYERS TO GOULD *** RETRACTION | | | | UPON FURTHER ANALYSIS OF THIS EVENT, IT HAS BEEN DETERMINED THAT NO | | REPORTABLE CONDITION EXISTS. USING THE ACTUAL STEAM RELIEF CAPACITY OF THE | | PRESSURIZER SAFETY VALVES VERSUS THE RATED STEAM RELIEF CAPACITY, BOTH | | RUPTURE DISKS ON THE OUTLET PIPING TEE OF EACH SAFETY VALVE WOULD HAVE BURST | | FOR ALL EXPECTED SAFETY VALVE LIFTS. WITH BOTH RUPTURE DISKS BURST, THE | | POTENTIAL TO INDUCE EXCESSIVE ECCENTRIC LOADS ON THE VALVES OR PIPING IS | | ELIMINATED. THEREFORE THEY ARE RETRACTING THIS EVENT. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. THE REG 3 RDO (JORDAN) WAS NOTIFIED. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35849 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 06/21/1999| | UNIT: [] [2] [] STATE: AL |NOTIFICATION TIME: 18:53[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 06/21/1999| +------------------------------------------------+EVENT TIME: 16:57[CDT]| | NRC NOTIFIED BY: BOWEN |LAST UPDATE DATE: 06/23/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT ENTERED TS REQUIRED SHUT DOWN DUE TO LOSS OF TWO STEAM FLOW | | CHANNELS ON THE "A" STEAM GENERATOR. | | | | PRIOR TO THIS EVENT THERE WAS A BROKEN SENSING LINE ON THE "B" STEAM | | GENERATOR STEAM FLOW CHANNEL WHICH REQUIRED PUTTING THE CHANNEL 3 STEAM | | FLOWS ON ALL THREE STEAM GENERATORS IN TEST. TODAY @ 1657 CHANNEL 4 ON THE | | "A" STEAM GENERATOR FAILED. THERE ARE TWO STEAM FLOW CHANNELS PER STEAM | | GENERATOR AND TECHNICAL SPECIFICATIONS REQUIRE ONE OF THE TWO FLOW CHANNELS | | TO BE AVAILABLE. SINCE CHANNELS 3 AND 4 ON THE "A" STEAM GENERATOR ARE NOT | | AVAILABLE, THE PLANT ENTERED TS LCO 3.0.3 WHICH GIVES THEM 7 HRS. TO BE IN | | HOT STANDBY, 6 HOURS TO HOT SHUTDOWN AND THE FOLLOWING 24 HOURS TO COLD | | SHUTDOWN. THE FEED PUMP SPEED CONTROL AND THE "A" STEAM GENERATOR FLOW | | CONTROL VALVE WERE PLACED IN MANUAL AND LEVELS WERE STABILIZED. THEY CAN | | EXIT THE LCO ACTION STATEMENT IF THEY TAKE CHANNEL 3 OUT OF TEST ON "A" | | STEAM GENERATOR AND RETURN IT TO SERVICE. | | | | THE RESIDENT INSPECTOR WILL BE INFORMED. | | | | *** UPDATE ON 6/21/99 @ 2017 BY BOWEN TO GOULD *** | | | | THEY TOOK THE CHANNEL 3 STEAM FLOW OUT OF TEST AND RETURNED IT TO SERVICE AT | | 1807 AND EXITED THE LCO ACTION STATEMENT. | | | | THE RESIDENT WILL BE NOTIFIED. REG2 RDO (JULIAN) | | | | | | *** UPDATE ON 6/23/99 @ 1834 BY HUNTER TO GOULD *** RETRACTION | | | | SUBSEQUENT EVALUATION HAS DETERMINED THE FAILED COMPONENT HAD NO AFFECT ON | | THE PROTECTION FUNCTIONS PROVIDED BY THE STEAM FLOW CHANNELS. THE FAILURE | | AFFECTED THE MAIN CONTROL BOARD INDICATION AND FEEDWATER CONTROL ONLY. | | THEREFORE, THIS EVENT IS BEING RETRACTED. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED. THE REG 2 RDO (BELISLE) WAS | | NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35852 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 06/23/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 06:18[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 06/23/1999| +------------------------------------------------+EVENT TIME: 04:07[EDT]| | NRC NOTIFIED BY: TOM DOUGHERTY |LAST UPDATE DATE: 06/23/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GLENN MEYER R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI FAILED DURING A START TEST | | | | The High Pressure Coolant Injection (HPCI) system failed to start during | | surveillance testing. At the time of the failure, HPCI was inoperable for | | planned maintenance on the governor controller for the turbine control | | valve. The nature of the failure was the turbine control valve did not open | | in response to an initiation signal. The cause of this failure is under | | investigation, it is unknown at this time if the failure was due to the | | maintenance or existed prior to the maintenance. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35853 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: TURKEY POINT REGION: 2 |NOTIFICATION DATE: 06/23/1999| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 12:25[EDT]| | RXTYPE: [3] W-3-LP,[4] W-3-LP |EVENT DATE: 06/23/1999| +------------------------------------------------+EVENT TIME: 11:38[EDT]| | NRC NOTIFIED BY: FLYNN |LAST UPDATE DATE: 06/23/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE REACTOR WAS MANUALLY TRIPPED AFTER FOUR RODS FELL INTO THE CORE. | | | | SHUTDOWN BANK "B" GROUP 1 CONTROL RODS (4 RODS) FELL INTO THE CORE WITH THE | | CAUSE BEING UNKNOWN. THE REACTOR WAS MANUALLY TRIPPED AND ALL RODS FULLY | | INSERTED AND NO INJECTION OCCURRED. THEY DID HAVE TWO SECONDARY SIDE RELIEF | | VALVES TO LIFT AND RESEAT ON THE FEEDWATER HEATERS. THE CAUSE OF THIS | | INCIDENT IS BEING INVESTIGATED BY I&C TECHNICIANS. THEN UNIT IS BEING | | MAINTAINED IN MODE 3 AND NO ABNORMAL CONDITIONS WERE NOTED. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35854 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/23/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 19:37[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/23/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/23/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MIKE JORDAN R3 | | DOCKET: 0707002 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CRABTREE | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 4 HOUR 91-01 BULLETIN RESPONSE | | | | PLANT SHIFT SUPERINTENDENTS OFFICE WAS NOTIFIED BY THE NUCLEAR CRITICALITY | | SAFETY(NCS) STAFF THAT A NUCLEAR CRITICALITY SAFETY APPROVAL(NCSA) WAS NOT | | BEING MAINTAINED IN THE X-744H STORAGE WAREHOUSE. NCSA-PLANT048 COVERS | | CONTAMINATED METALS. VALVES AND THE OTHER CASCADE EQUIPMENT WERE BEING | | STORED WITH THE UNDERSTANDING THAT EACH PIECE OF EQUIPMENT HAD LESS THAN 15 | | GRAMS U-235, BECAUSE THE DESCRIPTION OF THE OPERATION WHICH STATES " IN | | THE CASE OF CONTAMINATED EQUIPMENT SENT TO PORTSMOUTH FROM PADUCAH, OR OAK | | RIDGE OR ANY OTHER FACILITY, NON- DESTRUCTIVE ANALYSIS INFORMATION VERIFYING | | THAT THERE IS LESS THAN 15GM U-235 IS REQUIRED PRIOR TO ACCEPTANCE." THUS | | THE VALVES WERE HANDLED UTILIZING 15 GRAMS U-235 PER PIECE FOR TRANSPORT AND | | BATCHING CONSIDERATIONS. | | | | ALL VALVES IN QUESTION HAD BEEN IN STORAGE FOR AN EXTENDED PERIOD OF | | TIME(YEARS), AND IT WAS ASSUMED THAT THE EQUIPMENT STORED IN X-744H MET THE | | ACCEPTANCE REQUIREMENTS. THE VALVES WERE ANALYZED USING NON-DESTRUCTIVE | | ANALYSIS MEASUREMENTS TO VERIFY THEY MET THE ACCEPTANCE CRITERIA FOR | | DECONTAMINATION IN THE DRY ICE BLASTER(REF. NCSA-PLANT081). MEASUREMENTS | | IDENTIFIED HIGHER U-235 ENRICHMENT AND MASS THAN WAS PREVIOUSLY IDENTIFIED | | WITH AVAILABLE HISTORICAL DATA. BY THE TIME THE DATA HAD BEEN INTERPRETED, | | SEVERAL COMPONENTS HAD BEEN TRANSFERRED OUT OF THE BUILDING AND STAGED FOR | | TRANSPORT. HOWEVER, IT SHOULD BE NOTED THAT THE VALVES HAD BEEN STAGED IN | | COMPLIANCE WITH NCSA-PLANT048, EVEN IN LIGHT OF THE HIGHER MASSES | | IDENTIFIED. IN RESPONDING TO THAT CONCERN, ADDITIONAL QUESTIONS REGARDING | | THE APPLICABILITY OF THE 15 GRAM U-235 PER PIECE OF EQUIPMENT CAME UP. IT | | WAS CONCLUDED THAT OPERATIONS IN X-744H WOULD BE HALTED PENDING FULL | | DETERMINATION OF COMPLIANCE WITH NCSA-PLANT048. | | | | HOWEVER, BASED ON A REVIEW OF AVAILABLE HISTORICAL DATA PERFORMED BY THE | | BUILDING MANAGEMENT, IT HAS BEEN DETERMINED THAT FULL COMPLIANCE WITH | | NCSA-PLANT048 CANNOT BE ESTABLISHED FOR A LARGE PORTION OF THE LEGACY | | EQUIPMENT STORED IN X-744H. IN ADDITION, NO PROCEDURE COULD BE IDENTIFIED | | WITH WHICH THE EQUIPMENT HAS BEEN HANDLED WHICH INCORPORATED THE | | REQUIREMENTS OF NCSA-PLANT048. | | | | THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED ALONG WITH THE DOE REPRESENTATIVE. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35855 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/24/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 05:18[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/23/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 20:50[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/24/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |MIKE JORDAN R3 | | DOCKET: 0707001 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MATT MAURER | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR REPORT - SAFETY SYSTEM ACTUATION | | | | "At 2050 CDT on 6/23/99, C-333A Autoclave Position 1 North received a High | | Autoclave Steam Pressure Alarm while in TSR mode 5. The Autoclave Steam | | Pressure Control System is required to be operable while in mode 5 per LCO | | 2.2,3.3. An Increase in autoclave steam pressure was observed by the | | Autoclave Steam Pressure Control System and the system isolated the steam | | from the autoclave as designed. The autoclave was placed in mode 2 and the | | cause of the safety system actuation is being investigated." | | | | The NRC Resident Inspector has been notified of this event. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021