The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for June 24, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           06/23/1999 - 06/24/1999

                              ** EVENT NUMBERS **

35000  35849  35852  35853  35854  35855  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35000       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DAVIS BESSE              REGION:  3  |NOTIFICATION DATE: 11/05/1998|
|    UNIT:  [1] [] []                 STATE:  OH |NOTIFICATION TIME: 11:57[EST]|
|   RXTYPE: [1] B&W-R-LP                         |EVENT DATE:        11/05/1998|
+------------------------------------------------+EVENT TIME:        11:07[EST]|
| NRC NOTIFIED BY:  JOHN BALDWIN                 |LAST UPDATE DATE:  06/23/1999|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |RONALD GARDNER       R3      |
|10 CFR SECTION:                                 |                             |
|AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| DISCOVERY OF DESIGN OVERSTRESS CONDITION IN PRESSURIZER NOZZLES              |
|                                                                              |
| THE LICENSEE HAS DETERMINED  (VIA ENGINEERING CALCULATION C-ME-064.085.01)   |
| THAT A DESIGN OVERSTRESS CONDITION EXISTED IN THE PRESSURIZER SAFETY VALVE   |
| NOZZLES DURING THE PERIOD FROM 7/22/87 (INSTALLATION OF PLANT MODIFICATION   |
| 87-1001, WHICH INCREASED RUPTURE DISC BURST PRESSURE) UNTIL 10/17/98 (PLANT  |
| MODIFICATION TM 98-0036, WHICH REMOVED THE RUPTURE DISCS).  BASED UPON THE   |
| OVERSTRESS CONDITION, THESE PRESSURIZER NOZZLES WERE NOT FUNCTIONAL DURING   |
| THAT TIME. HOWEVER, WITH THE RUPTURE DISCS REMOVED, THE LICENSEE HAS         |
| DETERMINED THAT STRESS LEVELS REMAIN WITHIN USAR DEFINED ALLOWABLE VALUES    |
| FOR ALL LOAD COMBINATIONS.                                                   |
|                                                                              |
| THE NRC RESIDENT INSPECTOR HAS BEEN INFORMED.                                |
|                                                                              |
| *** UPDATE ON 6/23/99 @ 1326 BY MYERS TO GOULD ***       RETRACTION          |
|                                                                              |
| UPON FURTHER ANALYSIS OF THIS EVENT, IT HAS BEEN DETERMINED THAT NO          |
| REPORTABLE CONDITION EXISTS.  USING THE ACTUAL STEAM RELIEF CAPACITY OF THE  |
| PRESSURIZER SAFETY VALVES VERSUS THE RATED STEAM RELIEF CAPACITY, BOTH       |
| RUPTURE DISKS ON THE OUTLET PIPING TEE OF EACH SAFETY VALVE WOULD HAVE BURST |
| FOR ALL EXPECTED SAFETY VALVE LIFTS.  WITH BOTH RUPTURE DISKS BURST, THE     |
| POTENTIAL TO INDUCE EXCESSIVE ECCENTRIC LOADS ON THE VALVES OR PIPING IS     |
| ELIMINATED.  THEREFORE THEY ARE RETRACTING THIS EVENT.                       |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED.   THE REG 3 RDO (JORDAN) WAS NOTIFIED.  |
+------------------------------------------------------------------------------+

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35849       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FARLEY                   REGION:  2  |NOTIFICATION DATE: 06/21/1999|
|    UNIT:  [] [2] []                 STATE:  AL |NOTIFICATION TIME: 18:53[EDT]|
|   RXTYPE: [1] W-3-LP,[2] W-3-LP                |EVENT DATE:        06/21/1999|
+------------------------------------------------+EVENT TIME:        16:57[CDT]|
| NRC NOTIFIED BY:  BOWEN                        |LAST UPDATE DATE:  06/23/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CAUDLE JULIAN        R2      |
|10 CFR SECTION:                                 |                             |
|ASHU 50.72(b)(1)(i)(A)   PLANT S/D REQD BY TS   |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE PLANT ENTERED TS REQUIRED SHUT DOWN DUE TO LOSS OF TWO STEAM FLOW        |
| CHANNELS ON THE "A" STEAM GENERATOR.                                         |
|                                                                              |
| PRIOR TO THIS EVENT THERE WAS A BROKEN SENSING LINE ON THE  "B" STEAM        |
| GENERATOR STEAM FLOW CHANNEL WHICH REQUIRED PUTTING THE CHANNEL 3 STEAM      |
| FLOWS ON ALL THREE STEAM GENERATORS IN TEST.   TODAY @ 1657 CHANNEL 4 ON THE |
| "A" STEAM GENERATOR FAILED.  THERE ARE TWO STEAM FLOW CHANNELS PER STEAM     |
| GENERATOR AND TECHNICAL SPECIFICATIONS REQUIRE ONE OF THE TWO FLOW CHANNELS  |
| TO BE AVAILABLE.  SINCE  CHANNELS 3 AND 4 ON THE "A" STEAM GENERATOR ARE NOT |
| AVAILABLE, THE PLANT ENTERED TS LCO 3.0.3 WHICH GIVES THEM 7 HRS. TO BE IN   |
| HOT STANDBY, 6 HOURS TO HOT SHUTDOWN AND THE FOLLOWING 24 HOURS TO COLD      |
| SHUTDOWN.  THE FEED PUMP SPEED CONTROL AND THE "A" STEAM GENERATOR FLOW      |
| CONTROL VALVE WERE PLACED IN MANUAL AND LEVELS WERE STABILIZED.  THEY CAN    |
| EXIT THE LCO ACTION STATEMENT IF THEY  TAKE CHANNEL 3 OUT OF TEST ON "A"     |
| STEAM GENERATOR AND RETURN IT TO SERVICE.                                    |
|                                                                              |
| THE RESIDENT INSPECTOR WILL BE INFORMED.                                     |
|                                                                              |
| *** UPDATE ON 6/21/99 @ 2017 BY BOWEN TO GOULD ***                           |
|                                                                              |
| THEY TOOK THE CHANNEL 3 STEAM FLOW OUT OF TEST AND RETURNED IT TO SERVICE AT |
| 1807 AND EXITED THE LCO ACTION STATEMENT.                                    |
|                                                                              |
| THE RESIDENT WILL BE NOTIFIED.  REG2 RDO (JULIAN)                            |
|                                                                              |
|                                                                              |
| *** UPDATE ON 6/23/99 @ 1834 BY HUNTER TO GOULD ***   RETRACTION             |
|                                                                              |
| SUBSEQUENT EVALUATION HAS DETERMINED THE FAILED COMPONENT HAD NO AFFECT ON   |
| THE PROTECTION FUNCTIONS PROVIDED BY THE STEAM FLOW CHANNELS.  THE FAILURE   |
| AFFECTED THE MAIN CONTROL BOARD INDICATION AND FEEDWATER CONTROL ONLY.       |
| THEREFORE, THIS EVENT IS BEING RETRACTED.                                    |
|                                                                              |
| THE RESIDENT INSPECTOR WILL BE NOTIFIED.  THE REG 2 RDO (BELISLE) WAS        |
| NOTIFIED.                                                                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35852       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LIMERICK                 REGION:  1  |NOTIFICATION DATE: 06/23/1999|
|    UNIT:  [1] [] []                 STATE:  PA |NOTIFICATION TIME: 06:18[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        06/23/1999|
+------------------------------------------------+EVENT TIME:        04:07[EDT]|
| NRC NOTIFIED BY:  TOM DOUGHERTY                |LAST UPDATE DATE:  06/23/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |GLENN MEYER          R1      |
|10 CFR SECTION:                                 |                             |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| HPCI FAILED DURING A START TEST                                              |
|                                                                              |
| The High Pressure Coolant Injection (HPCI) system failed to start during     |
| surveillance testing.  At the time of the  failure, HPCI was inoperable for  |
| planned maintenance on the governor controller for the turbine control       |
| valve.  The nature of the failure was the turbine control valve did not open |
| in response to an initiation signal.  The cause of this failure is under     |
| investigation, it is unknown at this time if the failure was due to the      |
| maintenance or existed prior to the maintenance.                             |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35853       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: TURKEY POINT             REGION:  2  |NOTIFICATION DATE: 06/23/1999|
|    UNIT:  [3] [] []                 STATE:  FL |NOTIFICATION TIME: 12:25[EDT]|
|   RXTYPE: [3] W-3-LP,[4] W-3-LP                |EVENT DATE:        06/23/1999|
+------------------------------------------------+EVENT TIME:        11:38[EDT]|
| NRC NOTIFIED BY:  FLYNN                        |LAST UPDATE DATE:  06/23/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |AL BELISLE           R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|3     M/R        Y       100      Power Operation  |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE REACTOR WAS MANUALLY TRIPPED AFTER FOUR RODS FELL INTO THE CORE.         |
|                                                                              |
| SHUTDOWN BANK "B" GROUP 1 CONTROL RODS (4 RODS) FELL INTO THE CORE WITH THE  |
| CAUSE BEING UNKNOWN.  THE REACTOR WAS MANUALLY TRIPPED AND ALL RODS FULLY    |
| INSERTED AND NO INJECTION OCCURRED.  THEY DID HAVE TWO SECONDARY SIDE RELIEF |
| VALVES TO LIFT AND RESEAT ON THE FEEDWATER HEATERS.  THE CAUSE OF THIS       |
| INCIDENT IS BEING INVESTIGATED BY I&C TECHNICIANS.  THEN UNIT IS BEING       |
| MAINTAINED IN MODE 3 AND NO ABNORMAL CONDITIONS WERE NOTED.                  |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED.                                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35854       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 06/23/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 19:37[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        06/23/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        16:00[EDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  06/23/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |MIKE JORDAN          R3      |
|  DOCKET:  0707002                              |ROBERT PIERSON       NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  CRABTREE                     |                             |
|  HQ OPS OFFICER:  CHAUNCEY GOULD               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 4 HOUR 91-01 BULLETIN RESPONSE                                               |
|                                                                              |
| PLANT SHIFT SUPERINTENDENTS OFFICE WAS NOTIFIED BY THE NUCLEAR CRITICALITY   |
| SAFETY(NCS) STAFF THAT A NUCLEAR CRITICALITY SAFETY APPROVAL(NCSA) WAS NOT   |
| BEING MAINTAINED IN THE X-744H STORAGE WAREHOUSE.  NCSA-PLANT048 COVERS      |
| CONTAMINATED METALS.  VALVES AND THE OTHER CASCADE EQUIPMENT WERE BEING      |
| STORED WITH THE UNDERSTANDING THAT EACH PIECE OF EQUIPMENT HAD LESS THAN 15  |
| GRAMS U-235, BECAUSE THE DESCRIPTION OF THE OPERATION WHICH  STATES  " IN    |
| THE CASE OF CONTAMINATED EQUIPMENT SENT TO PORTSMOUTH FROM PADUCAH, OR OAK   |
| RIDGE OR ANY OTHER FACILITY, NON- DESTRUCTIVE ANALYSIS INFORMATION VERIFYING |
| THAT THERE IS LESS THAN 15GM U-235 IS REQUIRED PRIOR TO ACCEPTANCE."  THUS   |
| THE VALVES WERE HANDLED UTILIZING 15 GRAMS U-235 PER PIECE FOR TRANSPORT AND |
| BATCHING CONSIDERATIONS.                                                     |
|                                                                              |
| ALL VALVES IN QUESTION HAD BEEN IN STORAGE FOR AN EXTENDED PERIOD OF         |
| TIME(YEARS), AND IT WAS ASSUMED THAT THE EQUIPMENT STORED IN X-744H MET THE  |
| ACCEPTANCE REQUIREMENTS.  THE VALVES WERE ANALYZED USING NON-DESTRUCTIVE     |
| ANALYSIS MEASUREMENTS TO VERIFY THEY MET THE ACCEPTANCE CRITERIA FOR         |
| DECONTAMINATION IN THE DRY ICE BLASTER(REF. NCSA-PLANT081).  MEASUREMENTS    |
| IDENTIFIED HIGHER U-235 ENRICHMENT AND MASS THAN WAS PREVIOUSLY IDENTIFIED   |
| WITH AVAILABLE HISTORICAL DATA.  BY THE TIME THE DATA HAD BEEN INTERPRETED,  |
| SEVERAL COMPONENTS HAD BEEN TRANSFERRED OUT OF THE BUILDING AND STAGED FOR   |
| TRANSPORT.  HOWEVER, IT SHOULD BE NOTED THAT THE VALVES HAD BEEN STAGED IN   |
| COMPLIANCE WITH NCSA-PLANT048, EVEN IN LIGHT OF THE HIGHER MASSES            |
| IDENTIFIED.  IN RESPONDING TO THAT CONCERN, ADDITIONAL QUESTIONS REGARDING   |
| THE APPLICABILITY OF THE 15 GRAM U-235 PER PIECE OF EQUIPMENT CAME UP.  IT   |
| WAS CONCLUDED THAT OPERATIONS IN X-744H WOULD BE HALTED PENDING FULL         |
| DETERMINATION OF COMPLIANCE WITH NCSA-PLANT048.                              |
|                                                                              |
| HOWEVER, BASED ON A REVIEW OF AVAILABLE HISTORICAL DATA PERFORMED BY THE     |
| BUILDING MANAGEMENT, IT HAS BEEN DETERMINED THAT FULL COMPLIANCE WITH        |
| NCSA-PLANT048 CANNOT BE ESTABLISHED FOR A LARGE PORTION OF THE LEGACY        |
| EQUIPMENT STORED IN X-744H.  IN ADDITION, NO PROCEDURE COULD BE IDENTIFIED   |
| WITH WHICH THE EQUIPMENT HAS BEEN HANDLED WHICH INCORPORATED THE             |
| REQUIREMENTS OF NCSA-PLANT048.                                               |
|                                                                              |
| THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR                       |
| RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT.   |
|                                                                              |
| THE NRC RESIDENT INSPECTOR WAS NOTIFIED ALONG WITH THE DOE REPRESENTATIVE.   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35855       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 06/24/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 05:18[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        06/23/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        20:50[CDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  06/24/1999|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |MIKE JORDAN          R3      |
|  DOCKET:  0707001                              |ROBERT PIERSON       NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  MATT MAURER                  |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NLTR                     LICENSEE 24 HR REPORT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 24 HOUR REPORT - SAFETY SYSTEM ACTUATION                                     |
|                                                                              |
| "At 2050 CDT on 6/23/99, C-333A Autoclave Position 1 North received a High   |
| Autoclave Steam Pressure Alarm while in TSR mode 5.  The Autoclave Steam     |
| Pressure Control System is required to be operable while in mode 5 per LCO   |
| 2.2,3.3.  An Increase in autoclave steam pressure was observed by the        |
| Autoclave Steam Pressure Control System and the system isolated the steam    |
| from the autoclave as designed.  The autoclave was placed in mode 2 and the  |
| cause of the safety system actuation is being investigated."                 |
|                                                                              |
| The NRC Resident Inspector has been notified of this event.                  |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021