Event Notification Report for June 16, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/15/1999 - 06/16/1999 ** EVENT NUMBERS ** 35752 35823 35824 35825 35826 35827 35828 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35752 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 05/21/1999| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 15:02[EDT]| | RXTYPE: [2] GE-4 |EVENT DATE: 05/21/1999| +------------------------------------------------+EVENT TIME: 10:14[EDT]| | NRC NOTIFIED BY: STEVE MAREK |LAST UPDATE DATE: 06/15/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRENT CLAYTON R3 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 15 Power Operation |15 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 hour License Condition 2.C.(9) report concerning non-compliance with the | | approved fire protection program. | | | | During a design calculation review, plant engineering department personnel | | discovered that cable routing for safety/relief valve (SRV) 'G' is not in | | compliance with Appendix R design assumptions for cable separation. The SRV | | is used in the dedicated shutdown procedure to control reactor pressure and | | to depressurize the plant so that a cold shutdown condition can be achieved | | within 10 hours after plant shutdown (UFSAR commitment). An hourly fire | | watch has been established in the affected zone, pending an evaluation by | | engineering department personnel. | | | | The NRC Resident Inspector has been notified of this event notification by | | the licensee. | | | | * * * RETRACTED AT 1454 EDT ON 6/15/99 BY PATRICK FALLON TO WILLIAM POERTNER | | * * * | | | | "Further review determined that the previously reported cable routing of | | associated circuits for SRV 'G' being different than the Appendix R design | | assumptions, would not have affected the ability of SRV 'G' to function as | | assumed in the Dedicated Shutdown Procedure. Although the associated | | circuits were routed through fire zones where use of the Dedicated Shutdown | | Procedure was required, the fuses for the associated circuits were | | appropriately coordinated such that fire induced multiple high impedance | | faults would not have prevented operation of SRV 'G' as assumed in the | | procedure. Therefore, the existing configuration is in compliance with the | | approved Fermi 2 fire protection program as required by License Condition | | 2.C.(9). Accordingly, the previous notification made in accordance with | | License Condition 2.F is withdrawn." | | | | The licensee notified the NRC resident inspector. HOO notified R3DO (JOHN | | MADERA). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35823 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/15/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 04:02[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/14/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 17:56[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/16/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |JOHN MADERA R3 | | DOCKET: 0707002 |FRED COMBS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC 91-01 BULLETIN REPORT INVOLVING NCSA VIOLATION | | | | "On 6/14/99 at 1756, the Plant Shift Superintendent's office was notified by | | operations personnel that a Nuclear Criticality Safety Approval (NCSA) was | | not being maintained in the X-333 process building. Operations personnel | | discovered that a converter classified as UH (uncomplicated handling) being | | stored on the cell floor had a cover missing from an opening. The NCSA for | | this operation, PLANT062.A00, has a requirement which states in part, | | 'Openings/penetrations shall be covered to minimize the potential for | | moderator collection and moist air exposure.' | | | | "The Nuclear Criticality Safety (NCS) staff determined that this incident | | caused a loss of control such that only one double contingency control | | remained in place." | | | | Operations personnel will inform the DOE Site Representative and has | | informed the NRC Resident Inspector. | | | | * * * UPDATE AT 0402 BY SPAETH, TAKEN BY WEAVER * * * | | | | On 6/15/99, at 1123 while continuing an NCS walkdown, an additional NCSA | | non-compliance was discovered. A Recycle Cooler stored on the cell floor | | had a cover missing from an opening. The Recycle Cooler is classified as UH. | | Compliance was restored within four hours. | | | | The licensee notified the NRC resident inspector. The HOO notified the RDO | | (Madera); NMSS EO (Piccone). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35824 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 06/15/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 07:45[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 06/15/1999| +------------------------------------------------+EVENT TIME: 03:56[EDT]| | NRC NOTIFIED BY: ANTHONY ROGENSKI |LAST UPDATE DATE: 06/15/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JIMI YEROKUN R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VALID RADIATION ALARM IN AUXILIARY BUILDING CAUSED BY MAINTENANCE ACTIVITY. | | | | | | "WHILE DRAINING CHEMICAL AND VOLUME CONTROL SYSTEM (CVCS) HOLDUP TANK (HUT) | | 'A' WHICH WAS ISOLATED, THE LICENSEE NOTICED THE AUXILIARY BUILDING | | PARTICULATE AND GAS MONITORS INCREASING. OPERATORS CLOSED THE DRAIN VALVE | | AND THE RADIATION MONITORS CONTINUED TO INCREASE. THE GAS MONITOR TRIPPED | | AND GAVE AN AUXILIARY BUILDING VENTILATION ISOLATION." | | | | THE CVCS HUT IS NORMALLY MAINTAINED CLOSED WITH A NITROGEN OVERPRESSURE. | | RADIATION MONITORS R13 AND R14 INSTALLED ON THE AUXILIARY BUILDING | | VENTILATION EXHAUST BOTH SHOWED INCREASING COUNTS. THE R14 MONITOR | | INCREASED TO 2755 CORRECTED COUNTS PER MIN (CCPM) EXCEEDING THE ALARM | | SETPOINT OF 2250 RESULTING IN THE AUXILIARY BUILDING VENTILATION ISOLATION. | | THE R13 INCREASED TO 1283 CCPM WELL BELOW THE ALARM SETPOINT OF 3000. THE | | LICENSEE SUBSEQUENTLY RESTORED VENTILATION AND RESET THE ISOLATION SIGNAL. | | THERE WAS NO RADIATION RELEASE OFFSITE. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35825 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 06/15/1999| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 20:13[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/15/1999| +------------------------------------------------+EVENT TIME: 17:00[EDT]| | NRC NOTIFIED BY: ROBERT MAGLAJANG |LAST UPDATE DATE: 06/15/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN MADERA R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH FLUX AT SHUTDOWN ALARM NOT TESTED DURING CHANNEL FUNCTIONAL TEST. | | | | The following is a portion of a facsimile received from the licensee: | | | | "The function of the Source Range Channels is to provide detection and | | indication of source range neutron flux during shutdown, refueling and | | startup modes. The source range channels N31/N32 provide a 'High Flux at | | Shutdown' alarm in the control room and containment in case of unexpected | | reactivity excursions during shutdown and refueling operations. This alarm | | is credited in the Cook licensing basis for detection and mitigation of a | | boron dilution event as analyzed in UFSAR. This function is required to be | | available during modes 3, 4, 5 and 6. | | | | "Technical Specifications defines a Channel Functional Test as an injection | | of a simulated signal into the channel as close to the primary sensor as | | practicable to verify OPERABILITY including alarm and/or trip functions. | | Contrary to this the 'High Flux at Shutdown' alarm is not tested or verified | | during the Source Range Channel Functional Test. The function of the Source | | Range Channels cannot be credited as operable under the Technical | | Specifications unless it has been tested in conjunction with these Tech Spec | | requirements. | | | | "Technical Specification compensatory actions have begun which include | | verifying the Shutdown Margin requirements are met within one hour and at | | least once per 12 hours thereafter. | | | | "It should be noted that there is a great degree of confidence in the | | physical functionality of this alarm based on drawing review and the fact | | that the alarm came in on a channel spike on 2/4/99. The inoperability is | | based entirely on missed surveillance requirements." | | | | The licensee is revising procedures to test the high flux at shutdown | | alarm. | | | | The licensee plans to contact the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35826 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 06/15/1999| | UNIT: [1] [2] [] STATE: GA |NOTIFICATION TIME: 23:51[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 06/15/1999| +------------------------------------------------+EVENT TIME: 21:24[EDT]| | NRC NOTIFIED BY: BARRY COLEMAN |LAST UPDATE DATE: 06/16/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |NLCO TECH SPEC LCO A/S | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 M/R Y 41 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR SCRAM FROM 41% POWER. | | | | Operators manually scrammed the reactor from 41% power because of lowering | | vacuum in the main condenser. Operators first noticed lowering vacuum at | | around 2000 and worked unsuccessfully to fix the problem until the reactor | | was eventually scrammed at 2124. The cause of the loss of vacuum was a | | faulty steam jet air ejector. The turbine was manually tripped after the | | scram. Reactor water level lowered to -20 inches during the transient and | | caused an automatic group II isolation. | | | | Several complications arose during the plant response to this transient. | | The 4160 Volt electrical buses 2C and 2D did not switch to their alternate | | power supply as expected. This caused the loss of the recirculation pump | | oil pumps and the resultant loss of the recirculation pumps. These buses | | have been restored and recirculation pumps restarted. Restoring one of the | | recirculation pumps resulted in a transient on Unit 1 as described in the | | update below. | | | | The outboard MSIVs were manually closed because of low condenser vacuum and | | loss of the condensate system. The inboard 2B MSIV did not auto close as | | expected when vacuum reached 10 inches. This valve could not be shut | | manually (remotely) either and still indicates open. A drywell entry is | | planned to ascertain the exact status of this valve. | | | | Reactor Core Isolation Cooling (RCIC) has been manually started and is being | | used in conjunction with Safety Relief Valves (SRVs) to maintain reactor | | pressure, temperature and water level. Suppression pool cooling is | | operating, although pool temperature has risen to 112� F. Tech specs | | require the plant to be placed in cold shutdown within 36 hours when pool | | temperature exceeds 110� F. Operators are currently preparing to place High | | Pressure Coolant Injection (HPCI) online which is expected to reduce the | | heat load on the suppression pool and allow its temperature to lower. | | Efforts are also in progress to restore the secondary plant to aid in plant | | cooldown if necessary. | | | | The licensee notified the NRC resident inspector. | | | | | | * * * UPDATE AT 0041 ON 6/16/99 BY COLEMAN TAKEN BY WEAVER * * * | | | | Just prior to this event a hard ground was coming and going on the 600 Volt | | bus 1D. The licensee believes that the ground was caused by the cycling of | | the "B" recirculation pump discharge MOV on Unit 2. The 600 Volt bus 1D is | | the normal power supply to 2R24-SO18B which feeds the "B" recirculation pump | | discharge valve 2B31-FO31B. | | | | The "B" RPS MG set tripped causing a half scram, a half group II isolation | | (the outboard valves closed), a half group V isolation (F004 closed & RWCU | | pump tripped), reactor building & refueling floor ventilation isolated | | (outboard dampers closed), all four Standby Gas Treatment fans auto started, | | the main control room ventilation went into pressurization mode, and the | | fission product monitors isolated (outboard valves). | | | | The licensee notified the NRC resident inspector and the Operations Officer | | informed the R2DO (Julian). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35827 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 06/16/1999| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 02:58[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 06/16/1999| +------------------------------------------------+EVENT TIME: 02:10[EDT]| | NRC NOTIFIED BY: PHIL SANTINI |LAST UPDATE DATE: 06/16/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JIMI YEROKUN R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 99 Power Operation |95 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF ROD POSITION INDICATION RESULTS IN A RUNBACK | | | | "At 0210, Motor Control Center (MCC) 24 deenergized. This resulted in a | | loss of power to rod position indication. This in turn caused a dropped rod | | automatic runback to 95% power. Axial power tilt remained within the band. | | Loss of rod position indication placed the plant in a condition which was | | outside the limitations of Technical Specification 3.10.6. Rod position | | indication was subsequently recovered at 0225 when this load was | | reenergized. All automatic functions associated with the loss of MCC 24 | | and the runback occurred as expected." | | | | The licensee is investigating whether or not the runback should have reduced | | power to 85% vs 95% as well as the initial cause for the loss of power to | | MCC 24. | | | | The licensee will inform the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35828 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/16/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 03:53[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/15/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 09:30[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/16/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |JOHN MADERA R3 | | DOCKET: 0707002 |JOSEPHINE PICCONE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BULLETIN 91-01 24 HOUR REPORT | | | | On 6/15/99, at 0930 the Plant Shift Superintendent's office was notified by | | operations personnel that a Nuclear Criticality Safety Approval (NCSA) was | | not being maintained In the X-705 decontamination building. While | | performing operator rounds, Operations personnel discovered that a general | | purpose small diameter container in a transport cart, was incorrectly spaced | | from a 1-inch line containing fissile solution. | | | | The NCSA for this operation. NCSA-0705.004. has a requirement which states | | in part, "when moving uranium bearing containers, a minimum 2 feet | | edge-to--edge spacing shall be maintained between other uranium bearing | | materials and the container being moved." | | | | The Nuclear Criticality Safety staff determined that this incident caused a | | loss of control such that only one double contingency control remained in | | place. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
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