Event Notification Report for June 9, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/08/1999 - 06/09/1999 ** EVENT NUMBERS ** 35806 35807 35808 35809 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35806 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 06/08/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 14:54[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 06/08/1999| +------------------------------------------------+EVENT TIME: 12:06[EDT]| | NRC NOTIFIED BY: R. M. PEAL |LAST UPDATE DATE: 06/08/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN CARUSO R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR SCRAM DUE TO MAIN TRANSFORMER LOCKOUT | | | | The following text is a portion of a facsimile received from the licensee. | | | | "On June 8, 1999, Susquehanna Unit 2 was operating at 100% power. The unit | | experienced a unit primary lockout associated with [the] 'A' main | | transformer resulting in a main turbine trip and a reactor scram on turbine | | control valve fast closure. [All rods fully inserted.] Reactor water level | | dropped to approximately 0.4 inches on wide range instrumentation, [and] | | level was restored to 35 inches using feedwater. Reactor pressure peaked at | | approximately 1,114 psig which is higher than the reactor scram setpoint of | | 1,087 psig. Two [safety relief valves] cycled once during the initial | | event, and [the] turbine bypass valves are now open controlling at [the] | | pressure setpoint. There were no [emergency core cooling system] | | initiations or diesel generator starts. There were no challenges to | | containment." | | | | "This event is an unplanned actuation of an engineered safety feature and, | | therefore, requires a 4-hour ENS notification under 10 CFR | | 50.72(b)(2)(ii)." | | | | The licensee stated that the lockout was caused by a sudden pressure relay | | and that oil was initially spraying from the transformer. The fire brigade | | responded and has since been secured. A fire watch is currently in place. | | The licensee plans to place the unit in Cold Shutdown. | | | | The licensee notified the NRC resident inspector and plans to issue a press | | release. | | | | ******************** UPDATE AT 1850 ON 06/08/99 FROM MIKE PEAL TO LEIGH | | TROCINE ******************** | | | | The licensee notified the Pennsylvania Department of Environmental | | Protection of the oil spill from the 'A' main transformer. The licensee | | stated that the state notification was not required and was made as a | | courtesy. The transformer leaked for more than 1 hour, and the licensee | | drained the transformer from the bottom to stop the leak. This oil was | | placed into the pit so that it was contained. The quantity of oil that | | sprayed from the transformer and landed on the ground outside the | | transformer's berm was not known, but it covered only a small area. None of | | the oil entered the storm drains, and there was no run off. | | | | The licensee notified the NRC resident inspector of this update. The NRC | | operations officer notified the R1DO (Caruso). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35807 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FT CALHOUN REGION: 4 |NOTIFICATION DATE: 06/08/1999| | UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 15:39[EDT]| | RXTYPE: [1] CE |EVENT DATE: 09/10/1998| +------------------------------------------------+EVENT TIME: 15:44[CDT]| | NRC NOTIFIED BY: ERICK MATZKE |LAST UPDATE DATE: 06/08/1999| | HQ OPS OFFICER: WILLIAM POERTNER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GAIL GOOD R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNPLANNED INITIATION OF THE VENTILATION ISOLATION ACTUATION SYSTEM (VIAS) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "A condition report on 09/10/98 documented the actuation of the VIAS | | circuitry due to the operation of the KEY switch on RM-062. Due to the | | questioning attitude of system engineering personnel, the control room log | | for 09/10/98 was reviewed to determine the events surrounding the VIAS | | actuation. A containment pressure reduction (CPR) had been initiated prior | | to the VIAS actuation. The control room logs indicate that the CPR was | | terminated by the VIAS. In addition, the isolation valves for containment | | radiation monitoring (RM-050 and 051) were also actuated. The isolation of | | the monitors and the CPR are documented in the control room logs for | | 09/10/98. 10 CFR 50.72(b)(2)(ii) and 10 CFR 50.73(a)(2)(iv) require | | reporting actuations of engineered safety feature (ESF) equipment except | | when: | | (A) The actuation resulted from and was part of a pre-planned sequence | | during testing or reactor operation; | | (B) The actuation was invalid and: | | (1) Occurred while the system was properly removed from service; | | (2) Occurred after the safety function had already completed; or | | (3) Involved only the following specific ESFs or their equivalent systems; | | (i) Reactor water clean-up system; | | (ii) Control room emergency ventilation system; | | (iii) Reactor building ventilation system; | | (iv) Fuel building ventilation system; or | | (v) Auxiliary building ventilation system." | | | | "This actuation was not preplanned, and although the actuation was invalid | | it affected containment equipment which is not excluded by subparagraph | | (B)(3). This event should have been reported as a 4-hour verbal to the NRC | | and a 30-day written report to the NRC." | | | | The NRC resident inspector has been notified by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35808 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 06/08/1999| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 21:35[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 06/08/1999| +------------------------------------------------+EVENT TIME: 17:40[EDT]| | NRC NOTIFIED BY: DAVID NOYES |LAST UPDATE DATE: 06/08/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN CARUSO R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNEXPECTED LOW PRESSURE COOLANT INJECTION SYSTEM LOOP SELECT LOGIC ACTUATION | | DURING LOGIC SYSTEM TESTING | | | | At 1740 EDT on 06/08/99, with the unit in the Refueling mode, moderator | | temperature of 105�F, reactor water level of 40 inches in the normal band, | | and the 'A' loop of shutdown cooling in service; the low pressure coolant | | injection (LPCI) loop select logic caused the 'A' loop injection valve to | | travel from the throttled position to fully open. At the time, the 'B' loop | | was removed from service for maintenance, and the 'B' loop injection valve | | went fully closed. The effect on the plant was that shutdown cooling flow | | increased from 9,600 gpm to 11,200 gpm. After 5 minutes, control was | | restored to the 'A' loop injection valve, and flow was reduced to 9,600 gpm. | | There was no noticeable change on level because LPCI takes a suction from | | the vessel and returns water to the vessel. | | | | The initiation occurred during a Recirculation Motor-Generator Set Lockout | | Relay and 4,160-V Drive Motor Trip Control Test. Investigation into the | | cause of the event is ongoing. Logic system testing has been suspended | | until the cause has been determined and until a verification that all | | initiations occurred as designed has been completed. | | | | The licensee notified the NRC resident inspector and plans to notify the | | Massachusetts Civil Defense tomorrow morning. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35809 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 06/09/1999| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 00:26[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/09/1999| +------------------------------------------------+EVENT TIME: 00:20[EDT]| | NRC NOTIFIED BY: MIKE FERGUSON |LAST UPDATE DATE: 06/09/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRIAN BONSER R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECH SPEC REQUIRED SHUTDOWN - BOTH CHEMICAL & VOLUME CONTROL PUMPS | | INOPERABLE | | | | The licensee commenced a Tech Spec required shutdown at 0020 on 6/9/99. | | The shutdown was terminated at 0029 when the 1A Chemical and Volume Control | | (CVC) charging pump was returned to an operable status. Reactor power had | | been reduced to 99%. | | | | On 6/7/99, at 1500 the 1A CVC charging pump was declared inoperable because | | the "A" Service water pump was inoperable. At 2320 on 6/8/99, the 1B CVC | | charging pump was also declared inoperable because of abnormal flow. The | | licensee entered Tech Spec 3.0.3 at that time, and since the condition had | | not been repaired by 0020 on 6/9/99, a shutdown was commenced. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021