The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for June 7, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           06/04/1999 - 06/07/1999

                              ** EVENT NUMBERS **

35686  35687  35790  35791  35792  35793  35794  35795  35796  35797  35798  35799 
35800  35801  35802  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35686       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MILLSTONE                REGION:  1  |NOTIFICATION DATE: 05/06/1999|
|    UNIT:  [] [] [3]                 STATE:  CT |NOTIFICATION TIME: 18:44[EDT]|
|   RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP           |EVENT DATE:        05/06/1999|
+------------------------------------------------+EVENT TIME:        18:00[EDT]|
| NRC NOTIFIED BY:  MARTIN                       |LAST UPDATE DATE:  06/04/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JAMES LINVILLE       R1      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|                                                   |                          |
|3     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| VALVE FAILED LOCAL LEAK RATE TEST (LLRT).                                    |
|                                                                              |
| VALVE 3QSS*V4 IS A CHECK VALVE IN THE QUENCH SPRAY SYSTEM, AND THE CAUSE OF  |
| THE LLRT FAILURE IS UNKNOWN AND BEING INVESTIGATED, BUT MOST LIKELY MAY BE   |
| DUE TO VALVE DEGRADATION.  WHEN THE RESULTS OF ITS LLRT WERE ADDED TO THE    |
| OTHER CATEGORY "C" VALVES' RESULTS, THE TOTAL LEAKAGE EXCEEDED TECHNICAL     |
| SPECIFICATION ALLOWABLE LIMITS OF 43 SCFH (TOTAL MEASURED CATEGORY "C" WAS   |
| 335 SCFH); HOWEVER, THE TOTAL LEAKAGE OF EVERYTHING STILL DID NOT EXCEED THE |
| 0.6 La VALUE.  CORRECTIVE ACTION WILL BE TO REPAIR THE VALVE PRIOR TO        |
| STARTUP.                                                                     |
|                                                                              |
| THE NRC RESIDENT INSPECTOR WAS NOTIFIED ALONG WITH STATE, LOCAL AND OTHER    |
| GOVERNMENT AGENCIES.                                                         |
|                                                                              |
| * * * UPDATE 1134 5/13/99 FROM STEVE LAWHEAD TAKEN BY STRANSKY * * *         |
|                                                                              |
| Local leak rate testing of valve SIL*V6 (RHS Loop 1 Cold Leg Check Valve)    |
| found the leakage to be excessive.  This leakage, when combined with the     |
| other known leakage, caused TS LCO 3.6.1.2.b to be exceeded.  The TS         |
| requires a combined leakage rate of less than 0.6 La for all penetrations    |
| and valves subject to Type B and C tests, when pressurized to Pa.  The NRC   |
| resident inspector has been informed of this update.  Notified R1DO          |
| (Cowgill).                                                                   |
|                                                                              |
| * * * RETRACTION 1633 EDT ON 6/4/99 BY DALE BRODSKY TO FANGIE JONES * * *    |
|                                                                              |
| These conditions were conservatively reported as conditions outside the      |
| unit's design basis.                                                         |
|                                                                              |
| "A review has determined that the Combined Type B and C Leakage limit of     |
| 0.60 La and the Enclosure Building (Secondary Containment) Bypass Leakage    |
| limit of 0.042 La, (based upon ANSI/ANS 56.8-1994 and NUREG 1022, Rev. 1)    |
| should be based upon the As-Found limit measured on a Minimum Pathway        |
| Leakage Rate basis. Using this basis the measured total as-found leakage     |
| does not exceed either limit.                                                |
|                                                                              |
| "These conditions are not reportable pursuant to 10 CFR 50.72(b)(1)(ii)(B)   |
| as conditions outside the design basis, or pursuant to 10 CFR 50.72(b)(2)(i) |
| as events or conditions that may have resulted in an unanalyzed conditions   |
| and therefore, the Immediate Notification for these conditions is            |
| retracted."                                                                  |
|                                                                              |
| The licensee notified the NRC Resident Inspector.  The Headquarters          |
| Operations Officer notified the R1DO (Ronald Bellamy).                       |
+------------------------------------------------------------------------------+

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35687       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BROWNS FERRY             REGION:  2  |NOTIFICATION DATE: 05/06/1999|
|    UNIT:  [] [2] []                 STATE:  AL |NOTIFICATION TIME: 20:33[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4           |EVENT DATE:        05/06/1999|
+------------------------------------------------+EVENT TIME:        16:14[CDT]|
| NRC NOTIFIED BY:  NACOSTE                      |LAST UPDATE DATE:  06/04/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHRIS CHRISTENSEN    R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     M/R        Y       23       Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE REACTOR WAS MANUALLY SCRAMMED FROM 23.5% POWER.                          |
|                                                                              |
| DURING STARTUP FOLLOWING A REFUELING OUTAGE, THE UNIT EXPERIENCED A STEAM    |
| LEAK ON THE INLET SIDE OF THE OFFGAS PREHEATER  (ASME CLASS 2 PIPING).       |
| TECHNICAL REQUIREMENTS MANUAL (TMR) SECTION  3.4.3 REQUIRES THAT THE         |
| AFFECTED COMPONENT BE ISOLATED IMMEDIATELY, REQUIRING THAT THE MAIN STEAM    |
| ISOLATION VALVES (MSIVs) BE CLOSED.  THE MAIN TURBINE WAS TRIPPED FROM 23.5  |
| % POWER IN ANTICIPATION OF THE INSERTION OF A MANUAL SCRAM WHICH OCCURRED AT |
| 1614 CST.  THE MANUAL SCRAM CAUSED REACTOR VESSEL WATER LEVEL TO GO BELOW    |
| THE LOW SETPOINT LEVEL, WHICH GENERATED A REDUNDANT SCRAM SIGNAL AND         |
| INITIATED THE PCIS ISOLATIONS OF GROUPS 2 (PRIMARY CONTAINMENT), 3 (RWCU), 6 |
| (SECONDARY CONTAINMENT), AND 8 (TIP SYSTEM).  ALL RODS FULLY INSERTED, NO    |
| ECCS INJECTION OCCURRED, AND NO RELIEF VALVES LIFTED.  THE MSIVs WERE CLOSED |
| AT 1632.                                                                     |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED OF THIS EVENT.                           |
|                                                                              |
| * * * RETRACTED AT 1434 EDT ON 6/4/99 BY CHRIS VAUGHN TO FANGIE JONES * * *  |
|                                                                              |
| This event is retracted after review and determination that as a planned     |
| manual reactor trip, it was not reportable under 10CFR50.72.2.ii per NUREG   |
| 1022.                                                                        |
|                                                                              |
| The licensee notified the NRC Resident Inspector.  The Headquarters          |
| Operations Officer notified the R2DO (Kenneth Barr).                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35790       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 06/03/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 14:44[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        06/02/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        16:30[CDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  06/04/1999|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |DAVID HILLS          R3      |
|  DOCKET:  0707001                              |DON COOL             NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  THOMAS WHITE                 |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBA 76.120(c)(2)(i)     ACCID MT EQUIP FAILS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THREE SPRINKLER SYSTEMS DECLARED INOPERABLE DUE TO CORRODED HEADS (24-hour   |
| report)                                                                      |
|                                                                              |
| The following text is a portion of a facsimile received from Paducah:        |
|                                                                              |
| "On 06/02/99 at 1630 CDT, the Plant Shift Superintendent (PSS) was notified  |
| that numerous sprinkler heads were corroded, affecting 16 sprinkler systems  |
| in C-337 and 1 system in C-333, such that the ability of the sprinklers to   |
| flow sufficient water was called into question.  Subsequently, these         |
| sprinkler systems were declared inoperable, and TSR-required actions         |
| establishing roving fire patrols were initiated.  This deficiency was        |
| detected during scheduled system inspections conducted by Fire Protection    |
| personnel.  Currently, functionality of the sprinkler heads has not been     |
| fully evaluated by Fire Protection personnel, and the remaining cascade      |
| buildings are currently being inspected, and if necessary, this report will  |
| be updated to identify any additional areas.                                 |
|                                                                              |
| "It has been determined that this event is reportable under                  |
| 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to     |
| function as designed."                                                       |
|                                                                              |
| The NRC resident inspector has been notified of this event.                  |
|                                                                              |
| ******************** UPDATE RECEIVED AT 1022 EDT ON 06/04/99 FROM CAGE TO    |
| TROCINE *******************                                                  |
|                                                                              |
| The following text is a portion of a facsimile received from Paducah:        |
|                                                                              |
| "Two sprinkle heads on system D-1 in C-337 and two sprinkler heads on system |
| 27 in C-335 were identified to also be corroded.  These were identified to   |
| the PSS on 06/03/99 at 1600 CDT and 1601 CDT, respectively, and determined   |
| to require an update to this report by the PSS.                              |
|                                                                              |
| "It has been determined that this event is reportable under                  |
| 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to     |
| function as designed."                                                       |
|                                                                              |
| Paducah personnel notified the NRC resident inspector of this update.  The   |
| NRC operations officer notified the R3DO (Hills) and NMSS EO (Combs).        |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35791       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE              REGION:  2  |NOTIFICATION DATE: 06/04/1999|
|    UNIT:  [] [2] []                 STATE:  FL |NOTIFICATION TIME: 05:48[EDT]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        06/04/1999|
+------------------------------------------------+EVENT TIME:        03:13[EDT]|
| NRC NOTIFIED BY:  JACK BREEN                   |LAST UPDATE DATE:  06/04/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |KENNETH BARR         R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     M/R        Y       48       Power Operation  |0        Hot Standby      |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - MANUAL REACTOR TRIP FROM 48% POWER DUE TO 4 CONTROL RODS DROPPING INTO THE |
| CORE -                                                                       |
|                                                                              |
| AT 0313 ON 06/04/99, WHILE PERFORMING TROUBLESHOOTING ACTIVITIES ON UNIT 2   |
| CONTROL ELEMENT DRIVE SYSTEM FOLLOWING A CONTROL ROD DROPPING INTO THE       |
| REACTOR CORE ON 06/02/99 (REFER TO EVENT #35785), FOUR CONTROL ELEMENT       |
| ASSEMBLIES (SHUTDOWN GROUP 'B' - SUBGROUP 21) FELL INTO THE REACTOR CORE FOR |
| UNKNOWN REASONS.  CONTROL ROOM OPERATORS MANUALLY TRIPPED UNIT 2 FROM 48%    |
| POWER.  ALL CONTROL RODS INSERTED INTO THE CORE COMPLETELY.  STEAM IS BEING  |
| DUMPED INTO THE MAIN CONDENSER.  UNIT 2 IS STABLE IN MODE 3 (HOT STANDBY).   |
|                                                                              |
| THE LICENSEE IS CONTINUING TO INVESTIGATE THE CAUSE(S) OF THE DROPPED        |
| CONTROL RODS.                                                                |
|                                                                              |
| THIS EVENT HAD NO EFFECT ON UNIT 1 WHICH IS OPERATING  AT 100% POWER.        |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Other Nuclear Material                           |Event Number:   35792       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  U.S. AIR FORCE                       |NOTIFICATION DATE: 06/04/1999|
|LICENSEE:  U.S. AIR FORCE                       |NOTIFICATION TIME: 09:34[EDT]|
|    CITY:  Washington D.C.          REGION:  1  |EVENT DATE:        06/04/1999|
|  COUNTY:                            STATE:  DC |EVENT TIME:        06:30[EDT]|
|LICENSE#:  42-23539-01AF         AGREEMENT:  N  |LAST UPDATE DATE:  06/04/1999|
|  DOCKET:  03028641                             |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |RONALD BELLAMY       R1      |
|                                                |KENNETH BARR         R2      |
+------------------------------------------------+LINDA HOWELL         R4      |
| NRC NOTIFIED BY:  MAJOR MITCH HICKS            |FRED COMBS           NMSS    |
|  HQ OPS OFFICER:  LEIGH TROCINE                |CHARLES MILLER       IRO     |
+------------------------------------------------+FRANK CONGEL         IRO     |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|IBDB 30.50(b)(4)(ii)     DAMAGED LNM/CONTAINER  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LOSS OF TWO 500- �Ci STRONTIUM-90 SOURCES DUE TO A HELICOPTER CRASH IN       |
| FAYETTEVILLE, NORTH CAROLINA (24-HOUR REPORT)                                |
|                                                                              |
| A representative from Bolling Air Force Base (located in Washington D.C.)    |
| reported that a helicopter from Hurlburt Field (located in Mary Esther,      |
| Florida) crashed at 2300 on 06/02/99 while performing a night training       |
| exercise at Pope Air Force Base (located in Fayetteville, North Carolina).   |
| Each helicopter blade contained an in-flight blade inspection system (IBIS)  |
| source with 500 �Ci of Strontium-90, and it is currently believed that the   |
| helicopter had four blades.  Two of the four IBIS sources have been          |
| identified and recovered by the pope Air Force Base Accident Response Team.  |
| These devices have been bagged and will be checked for contamination.        |
| Pending the completion of the crash investigation, the licensee plans to     |
| search for the remaining IBIS sources with survey equipment.                 |
|                                                                              |
| This event was reported to Bolling Air Force Base at 0630 on 06/04/99.       |
|                                                                              |
| Five individuals survived the crash, and there was one fatality.             |
|                                                                              |
| The limit referenced in 10 CFR Part 20, Appendix C, for Strontium-90 is 0.1  |
| �Ci.                                                                         |
|                                                                              |
| The licensee plans to notify the NRC Region 4 Office.  (Call the NRC         |
| Operations Center for a licensee contact telephone number.)                  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35793       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: VERMONT YANKEE           REGION:  1  |NOTIFICATION DATE: 06/04/1999|
|    UNIT:  [1] [] []                 STATE:  VT |NOTIFICATION TIME: 12:35[EDT]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        06/04/1999|
+------------------------------------------------+EVENT TIME:        09:50[EDT]|
| NRC NOTIFIED BY:  MITCH McCLUSKIE              |LAST UPDATE DATE:  06/04/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |RONALD BELLAMY       R1      |
|10 CFR SECTION:                                 |                             |
|AINB 50.72(b)(2)(iii)(B) POT RHR INOP           |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| ALTERNATE COOLING SYSTEM DECLARED INOPERABLE                                 |
|                                                                              |
| "Following a question raised by an NRC Resident Inspector at VY, an Event    |
| Report was submitted due to a lack of sufficient analysis to determine if    |
| procedural guidance was adequate for operation of the Alternate Cooling      |
| System (ACS).  VY declared the ACS inoperable at 2110 on 6/3/99 and entered  |
| a 7 day LCO [3.5.d.3] per the plant Technical Specifications.  Based on      |
| further evaluation, Operations and Engineering Personnel concluded that      |
| current VY procedures may not provide the specific information necessary to  |
| ensure that ACS Design Bases 1 & 2 above, would have been met.  Engineering  |
| and Licensing evaluations of ACS design and performance requirements         |
| continue.                                                                    |
|                                                                              |
| "VY is currently developing procedural enhancements that will ensure that    |
| the operating crews are provided with the guidance necessary to ensure that  |
| ACS would be operated in the manner necessary to achieve its safety design   |
| bases.  It is expected that the necessary procedural guidance will be        |
| developed and issued prior to the                                            |
| expiration of the cited 7 day LCO."                                          |
|                                                                              |
| The licensee notified the NRC Resident Inspector and the State of Vermont.   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   35794       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  ARKANSAS DEPT OF HEALTH RAD CONTROL  |NOTIFICATION DATE: 06/04/1999|
|LICENSEE:  AQUATERRA, INC.                      |NOTIFICATION TIME: 12:51[EDT]|
|    CITY:  El DORADO                REGION:  4  |EVENT DATE:        06/02/1999|
|  COUNTY:                            STATE:  AR |EVENT TIME:        18:00[CDT]|
|LICENSE#:  LA-5382-L01           AGREEMENT:  Y  |LAST UPDATE DATE:  06/04/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |LINDA HOWELL         R4      |
|                                                |FRED COMBS           NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  DAVID SNELLINGS              |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT                                                       |
|                                                                              |
| "Abstract:  A Troxler gauge Model 3411 B (Serial # 9816) was run over and    |
| damaged by a bulldozer at a construction site near El Dorado, Arkansas.  The |
| gauge contained approximately 9 millicuries of Cesium-137 and 44 millicuries |
| of Americium-241: beryllium.  The outer case of the gauge was damaged and    |
| the source rod was bent.  The licensee was working under reciprocity with a  |
| Louisiana Radioactive Material License (LA-5382-L01).  The licensee was able |
| to retrieve the gauge, assess the damage and return the gauge to the storage |
| location.  A leak test was performed and Troxler Labs was notified.  A       |
| health physicist from the Arkansas Dept. of Health investigated the incident |
| on June 3, 1999.  It was noted during investigation that the shutter was     |
| partially opened resulting in doserate of 50 mR/hour at contact.  Further    |
| investigation is on going.                                                   |
|                                                                              |
| "Arkansas License No:  ARK-REC-232; Reciprocity Licensee: AQUATERRA, INC.,   |
| LA-5382L01, of PORT ALLEN, LA"                                               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Hospital                                         |Event Number:   35795       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  NORTH COUNTRY HOSPITAL               |NOTIFICATION DATE: 06/04/1999|
|LICENSEE:  NORTH COUNTRY HOSPITAL               |NOTIFICATION TIME: 14:25[EDT]|
|    CITY:  Newport                  REGION:  1  |EVENT DATE:        02/04/1999|
|  COUNTY:  Orleans                   STATE:  VT |EVENT TIME:             [EDT]|
|LICENSE#:                        AGREEMENT:  N  |LAST UPDATE DATE:  06/04/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |RONALD BELLAMY       R1      |
|                                                |FRED COMBS           NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  LARRY LABOR                  |                             |
|  HQ OPS OFFICER:  LEIGH TROCINE                |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|LADM 35.33(a)            MED MISADMINISTRATION  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MEDICAL MISADMINISTRATION AT NORTH COUNTRY HOSPITAL LOCATED IN NEWPORT,      |
| VERMONT                                                                      |
|                                                                              |
| On 02/04/99, a medical misadministration occurred at North Country Hospital  |
| located in Newport, Vermont.  The physician prescribed a diagnostic test     |
| involving 10 �Ci of Iodine-131, and a 305-�Ci dose of Iodine-131 was         |
| administered.  Subsequent review of the dose by a radiologist determined     |
| that the literature search showed support for the dose received, and the     |
| licensee stated that there were no anticipated adverse health affects.  The  |
| patient subsequently went to a tertiary medical center and received an       |
| ablation therapy, and the 305-�Ci dose of Iodine-131 that was administered   |
| on 02/04/99 at North Country Hospital was subtracted from the ablation dose  |
| administered at the tertiary medical center.   At this time, the licensee    |
| does not plan to notify the patient.                                         |
|                                                                              |
| A Region 1 inspector (Thompson) was informed by the licensee on 06/03/99.    |
| (Call the NRC Operations Center for a licensee contact telephone number.)    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35796       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUMMER                   REGION:  2  |NOTIFICATION DATE: 06/04/1999|
|    UNIT:  [1] [] []                 STATE:  SC |NOTIFICATION TIME: 16:03[EDT]|
|   RXTYPE: [1] W-3-LP                           |EVENT DATE:        06/04/1999|
+------------------------------------------------+EVENT TIME:        13:58[EDT]|
| NRC NOTIFIED BY:  JIM PROPER                   |LAST UPDATE DATE:  06/04/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |KENNETH BARR         R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       100      Power Operation  |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| REACTOR TRIP DUE TO SPURIOUS SIGNAL DURING POWER RANGE CALIBRATION           |
|                                                                              |
| During the performance of power range calibration of N42, with a trip signal |
| in, a spurious signal from N43 was received which completed the 2 of 4       |
| coincidence for a reactor trip on high flux.  The reactor tripped, all rods  |
| inserted and all systems functioned as required.                             |
|                                                                              |
| This event is being investigated and the plant will remain in Hot Standby    |
| until the cause is determined and corrected.  The plant is presently stable  |
| with auxiliary feedwater supplying water to the steam generators and the     |
| steam dumps exhausting to the main condenser.                                |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35797       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: WOLF CREEK               REGION:  4  |NOTIFICATION DATE: 06/04/1999|
|    UNIT:  [1] [] []                 STATE:  KS |NOTIFICATION TIME: 17:04[EDT]|
|   RXTYPE: [1] W-4-LP                           |EVENT DATE:        06/04/1999|
+------------------------------------------------+EVENT TIME:        15:05[CDT]|
| NRC NOTIFIED BY:  DAVE DEES                    |LAST UPDATE DATE:  06/04/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA HOWELL         R4      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION DUE TO EXCESSIVE CHLORINE IN DISCHARGE                  |
|                                                                              |
| The licensee notified the Kansas Department of Health and Environment due to |
| exceeding the residual limit of 0.2 ppm chlorine in the Circulating Water    |
| discharge.  The highest observed reading was 1.6 ppm.  A mechanical failure  |
| in the sodium hypochlorite feed pump is suspected.  An investigation is in   |
| progress and the system is isolated until corrected.                         |
|                                                                              |
| The licensee notified the NRC Resident Inspector as well as the State of     |
| Kansas and local county authorities.                                         |
|                                                                              |
| * * * UPDATE AT 2243 EDT ON 6/4/99 BY STEVE HEDGES TO FANGIE JONES * * *     |
|                                                                              |
| After subsequent evaluation of sodium hypochlorite release volumes, the      |
| licensee determined that the release limits of 40 CFR 302 of 100 pounds was  |
| exceeded.  The calculated release was 1694 pounds.  The licensee notified    |
| the National Response Center (report # 486-281).                             |
|                                                                              |
| The licensee notified the NRC Resident Inspector.  The Headquarters          |
| Operations Officer notified the R4DO (Linda Howell).                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35798       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: THREE MILE ISLAND        REGION:  1  |NOTIFICATION DATE: 06/04/1999|
|    UNIT:  [1] [] []                 STATE:  PA |NOTIFICATION TIME: 18:02[EDT]|
|   RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP            |EVENT DATE:        06/04/1999|
+------------------------------------------------+EVENT TIME:        17:17[EDT]|
| NRC NOTIFIED BY:  JOHN SCHORK                  |LAST UPDATE DATE:  06/04/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |RONALD BELLAMY       R1      |
|10 CFR SECTION:                                 |                             |
|AOUT 50.72(b)(1)(ii)(B)  OUTSIDE DESIGN BASIS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| REACTOR BUILDING EMERGENCY COOLING SYSTEM OPERABLE BUT DEGRADED              |
|                                                                              |
| "At 1717 hours on June 4, 1999, GPU Nuclear determined that a condition that |
| is outside the plant design basis may exist at TMI-1 due to potential        |
| degraded performance of the Reactor Building [RB] Emergency Cooling System.  |
| Measurements of indirect system performance parameters for the TMI-1 Reactor |
| Building Emergency Cooling System indicate that the air flow through the     |
| system may be less than that assumed in the plant design basis.              |
|                                                                              |
| "Specifically, air flow in the RB Normal Cooling system, that utilizes duct  |
| work and a flow damper common to both the RB Normal cooling system and the   |
| RB Emergency Cooling System, has been found to be below previous air flow    |
| measurements. The air flow reduction may be indicative of a reduced air flow |
| that would occur in the RB Emergency Cooling system if it was called upon to |
| function in the event of a design basis accident. The design basis flow for  |
| the RB Emergency Cooling System is 25,000 CFM with the RB cooling fans in    |
| slow speed. Engineering judgement is that the current flow rate may be below |
| 25,000 CFM if the system was called upon to function, hence the              |
| identification of a condition outside the plant design basis.                |
|                                                                              |
| "Engineering judgement is that: the Reactor Building Emergency Cooling       |
| System remains operable but may be degraded. The judgement that the system   |
| is operable with degraded air flow is based on the difference between        |
| conservative assumptions in environmental temperatures in the plant design   |
| basis analysis and current environmental conditions and in view of the fact  |
| that the environmental conditions within the Reactor Building in the design  |
| basis accident should enhance the current potential degraded system air      |
| flow. A formal internal justification of continued operation (JCO) will be   |
| prepared to document the basis for the engineering judgement and will be     |
| provided to the site NRC resident inspectors office.                         |
|                                                                              |
| "Because GPU Nuclear has classified this condition as being potentially      |
| outside the design basis of the plant, GPU Nuclear is notifying the NRC      |
| Operations Center in accordance with 10 CFR 50.72(b)(1)(ii)(b). This         |
| notification will be followed with a 30 day LER in accordance with 10 CFR    |
| 50.73.                                                                       |
|                                                                              |
| "GPU Nuclear will document this condition in its 10 CFR 50 Appendix B        |
| corrective action program and this potential non-conformance is being        |
| addressed in accordance with the guidance provided in NRC Generic Letter     |
| 91-18, Rev 1."                                                               |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35799       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 06/04/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 19:05[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        06/04/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        07:25[EDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  06/04/1999|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |DAVID HILLS          R3      |
|  DOCKET:  0707002                              |WAYNE HODGES         NMSS    |
+------------------------------------------------+CHARLES MILLER       IRO     |
| NRC NOTIFIED BY:  RICK LARSON                  |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| NRC BULLETIN 91-01 24 HOUR REPORT                                            |
|                                                                              |
| "ON 6/4/99 AT 0725 HRS. OPERATIONS PERSONNEL DISCOVERED THAT REQUIREMENT #5  |
| OF NUCLEAR CRITICALITY SAFETY ANALYSIS (NCSA) PLANT_003.A01 WAS NOT BEING    |
| MET.  THE REQUIREMENT, MONITORING SURGE DRUM PRESSURE ONCE EACH SHIFT WAS    |
| BEING PERFORMED WITH THE INSTALLED PRESSURE INDICATOR WHICH WAS ISOLATED ON  |
| 5/20/99 TO ALLOW MAINTENANCE TO CALIBRATE.  WHEN THE INDICATOR COULD NOT BE  |
| CALIBRATED IT WAS LEFT ISOLATED AND OPERATIONS WAS NOT MADE AWARE THAT OF    |
| THIS CONDITION.  SINCE THE LINE WAS VALVED OFF THE DRUM PRESSURE WAS NOT     |
| MEASURED AS REQUIRED, THIS IS A LOSS OF A SINGLE CONTROL (CONCENTRATION) OF  |
| THE DOUBLE CONTINGENCY PROGRAM.  THE SECOND CONTROL (MODERATION) WAS         |
| MAINTAINED THROUGHOUT THE EVENT.  THE PRESSURE INDICATOR WAS VALVED IN AT    |
| 0905 HRS. ON 6/4/99.  PREVIOUS MAINTENANCE IN THE CASCADE REGARDING SURGE    |
| DRUM CALIBRATION MAY HAVE RESULTED IN A SIMILAR SITUATION.                   |
|                                                                              |
| "THE 'X'  BANK SURGE DRUM WAS EVACUATED AND TAGGED OUT OF SERVICE FOR        |
| MAINTENANCE.                                                                 |
| THEREFORE, THE SURGE DRUM IS CONSIDERED EMPTY.  ON 5/20/99 MAINTENANCE       |
| VALVED OFF THE DRUM TO DO WORK ON THE PRESSURE SENSOR.  THE DRUM REMAINED    |
| VALVED OFF UNTIL 6/4/99.  WHEN THE DRUM WAS VALVED BACK IN THE DRUM WAS      |
| STILL EVACUATED.  THIS INDICATED THAT THE NCSA PRESSURE LIMIT WAS NEVER      |
| EXCEEDED (i.e., WET AIR IN-LEAKAGE DID NOT OCCUR), THEREFORE, THE SAFETY     |
| SIGNIFICANCE OF THIS EVENT IS LOW AND A CRITICALITY WAS NOT POSSIBLE.        |
|                                                                              |
| "FOR CRITICALITY TO OCCUR THE SURGE DRUM WOULD HAVE TO HAVE MATERIAL IN IT   |
| AND THE MATERIAL WOULD NAVE TO BE MODERATED BY WET AIR IN-LEAKAGE.  THIS WAS |
| EXPECTED TO OCCUR IN THIS CASE BECAUSE THE DRUM WAS HOLDING ITS PRESSURE     |
| BEFORE MAINTENANCE CALIBRATED THE PRESSURE SENSOR, AND THE FACT THAT OTHER   |
| SURGE DRUMS IN THE SAME ROOM WERE OPERATING AND THE ROOM TEMPERATURE WAS     |
| GREATER THAN 140�F.                                                          |
|                                                                              |
| "THE ESTIMATED AMOUNT OF MATERIAL IN THE DRUM IS LESS THAN 600 gms. U-235 (A |
| SAFE MASS AT 10% ENRICHMENT) DUE TO THE FACT THAT THE DRUM WAS EVACUATED     |
| PRIOR TO MAINTENANCE.  WHEN THE PRESSURE SENSOR WAS VALVED BACK INTO THE     |
| DRUM, THE DRUM WAS STILL AT A VACUUM (NOTE: THE NCSA PRESSURE LIMIT ON THE   |
| DRUM IS 17 psia).  THE MAXIMUM ENRICHMENT IN THIS DRUM IS 10%.  THE FORM OF  |
| THE MATERIAL IS EITHER UF6 OR UO2F2.                                         |
|                                                                              |
| "THE MAINTENANCE PROCEDURE REQUIRES THE PRESSURE INDICATOR TO BE ISOLATED    |
| FOR CALIBRATION.  THIS WAS DONE ON 5/20/99.  WHEN THE SENSOR COULD NOT BE    |
| CALIBRATED, THE LINE WAS LEFT VALVED OFF AND OPERATIONS DID NOT KNOW THIS.   |
| THE NCSA REQUIRES THE PRESSURE ON THE DRUM TO BE MONITORED AND RECORDED EACH |
| SHIFT, OPERATIONS WAS READING THE MT&E SENSOR INSTALLED.  HOWEVER, SINCE THE |
| LINE WAS VALVED OFF THE DRUM PRESSURE WAS NOT MEASURED AS REQUIRED.          |
|                                                                              |
| "THE RESIDENT NRC INSPECTOR HAS BEEN NOTIFIED."                              |
|                                                                              |
| * * * UPDATE AT 2120 EDT ON 6/4/99 BY ERIC SPAETH TO FANGIE JONES * * *      |
|                                                                              |
| Clarification:  the normal pressure indicator is read in the control room.   |
| That indicator is still not calibrated and a local calibrated pressure gauge |
| was valved in for indication on 6/4/99 and is read locally each shift.       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35800       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CRYSTAL RIVER            REGION:  2  |NOTIFICATION DATE: 06/05/1999|
|    UNIT:  [3] [] []                 STATE:  FL |NOTIFICATION TIME: 01:27[EDT]|
|   RXTYPE: [3] B&W-L-LP                         |EVENT DATE:        06/04/1999|
+------------------------------------------------+EVENT TIME:        23:55[EDT]|
| NRC NOTIFIED BY:  WILLIAM KISNER               |LAST UPDATE DATE:  06/05/1999|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |KENNETH BARR         R2      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|3     N          Y       85       Power Operation  |85       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LIVE TURTLE FOUND IN INTAKE STRUCTURE                                        |
|                                                                              |
| The licensee notified the Florida Department of Environmental Protection     |
| regarding the discovery of a live Loggerhead Turtle on the intake bar racks. |
| The turtle was removed and transported to the mariculture center.  The NRC   |
| resident inspector has been informed of this notification by the licensee.   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35801       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: QUAD CITIES              REGION:  3  |NOTIFICATION DATE: 06/06/1999|
|    UNIT:  [1] [] []                 STATE:  IL |NOTIFICATION TIME: 18:07[EDT]|
|   RXTYPE: [1] GE-3,[2] GE-3                    |EVENT DATE:        06/06/1999|
+------------------------------------------------+EVENT TIME:        14:40[CDT]|
| NRC NOTIFIED BY:  MIKE MacLENNON               |LAST UPDATE DATE:  06/06/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |DAVID HILLS          R3      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |55       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LIGHTNING STRIKE CAUSED SOME MINOR ALARMS AND PARTIAL GROUP ONE ISOLATIONS   |
|                                                                              |
| "On 6/6/99 at approximately 1440 hours, a lightning strike caused valves     |
| 1-0220-44 and 1-0220-45, Reactor Recirculation sample valves, to close on an |
| invalid signal.  These valves close automatically on a Group One isolation,  |
| and therefore this is considered to be an ESF actuation.                     |
|                                                                              |
| "The power change indicated above was also a result of the lightning strike. |
| An emergency load reduction was made in response to a partial loss of        |
| feedwater heaters.  Reactor recirculation flow was manually reduced and      |
| control rods were inserted to reduce the flow control line below 100%.       |
| Miscellaneous other minor alarms were received on both units due to the      |
| lightning strike.                                                            |
|                                                                              |
| "The above mentioned sample valves have been reopened, and a load increase   |
| to full power has been initiated as of 1635 hours."                          |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35802       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE              REGION:  2  |NOTIFICATION DATE: 06/06/1999|
|    UNIT:  [] [2] []                 STATE:  FL |NOTIFICATION TIME: 21:14[EDT]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        06/06/1999|
+------------------------------------------------+EVENT TIME:        18:45[EDT]|
| NRC NOTIFIED BY:  ALAN HALL                    |LAST UPDATE DATE:  06/06/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |KENNETH BARR         R2      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     A          N       0        Hot Standby      |0        Hot Standby      |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| WITH THE REACTOR SHUTDOWN, AN AUTOMATIC REACTOR TRIP WAS GENERATED           |
|                                                                              |
| "At 1845 EDT, an inadvertent partial opening of the 2B MSIV occurred,        |
| causing a steam generator pressure transient that resulted in an Reactor     |
| Protection System Asymmetrical Steam Generator Pressure Transient.  The      |
| plant was in Mode 3, all control element assemblies were fully inserted, the |
| trip circuit breakers were closed, and opened as expected in response to the |
| trip signal.  Investigation proceeding."                                     |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+


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