Event Notification Report for May 20, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/19/1999 - 05/20/1999 ** EVENT NUMBERS ** 35325 35726 35734 35737 35738 35739 35740 35741 35742 35743 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Hospital |Event Number: 35325 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: DETROIT MACOMB HOSPITAL |NOTIFICATION DATE: 01/29/1999| |LICENSEE: DETROIT MACOMB HOSPITAL |NOTIFICATION TIME: 11:28[EST]| | CITY: DETROIT REGION: 3 |EVENT DATE: 01/28/1999| | COUNTY: STATE: MI |EVENT TIME: 16:10[EST]| |LICENSE#: 21-01190-05 AGREEMENT: N |LAST UPDATE DATE: 05/19/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |TONY VEGEL R3 | | |DONALD COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ARTHUR EWALD | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION DUE TO PATIENT INTERVENTION | | | | During brachytherapy treatment of a patient's endobronchial area, the | | patient dislodged the catheter approximately 25 cm, causing the treatment | | site to receive only 3.8% of the prescribed dose. Additionally, the | | patient's nasal area received approximately 13 rads (13 cGy) due to the | | displacement. The licensee estimates that the catheter was dislodged for | | approximately 10 minutes before being discovered. | | | | The patient's referring physician has been informed of this event. | | | | * * * RETRACTED AT 1356 EDT ON 5/19/99 BY ART EWALD TO STEVE SANDIN * * * | | | | The licensee is retracting this report based on review and consultation with | | the NRC. Notified R3DO(Clayton) and NMSS(Camper). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35726 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: U.S. ARMY |NOTIFICATION DATE: 05/17/1999| |LICENSEE: U.S. ARMY |NOTIFICATION TIME: 12:03[EDT]| | CITY: ROCK ISLAND REGION: 3 |EVENT DATE: 05/16/1999| | COUNTY: STATE: IL |EVENT TIME: [CDT]| |LICENSE#: 12-00722-13 AGREEMENT: Y |LAST UPDATE DATE: 05/19/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRENT CLAYTON R3 | | |PETER ESELGROTH R1 | +------------------------------------------------+JOE HOLONICH NMSS | | NRC NOTIFIED BY: JEFF HAVENER |FEMA, DOE, USDA, HHS FAX | | HQ OPS OFFICER: FANGIE JONES |EPA, DOT (VIA NRC) FAX | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST OR STOLEN 3-CURIE TRITIUM SOURCE FROM AN M140 ALIGNMENT DEVICE | | | | Sometime on 5/16/99 near Watervliet Arsenal (about 35 miles from Albany, NY) | | at a contractor's facility (Wright Malta Corporation at Wright Malta | | Station), a break-in occurred. In the facility was a howitzer with an M1A1 | | collimator (10 curies tritium) and an M140 alignment device (3 curies | | tritium). The two devices were taken but were recovered on site when the | | thieves were interrupted on the way out and dropped them. However, the | | source was missing from the M140 alignment device, and it is unknown whether | | the source was missing previously or removed and taken by the thieves. The | | local police are following up on the break-in and theft. The Watervliet | | Arsenal contacted the State of New York, who in turn notified NRC Region 1. | | | | (Call the NRC operations officer for additional information.) | | | | * * * UPDATE 1730EDT ON 5/19/99 FROM JEFF HAVENNER TO S.SANDIN * * * | | | | Additional information received by the licensee on 5/19/99 indicates that an | | M58 and an M59 aiming post light may also be missing. These are 5 and 4 | | Curies of tritium for a total of 9 Curies. Notified R1DO(Eselgroth), | | R3DO(Clayton), NMSS(Haughney) and FEMA, DOE, USDA, HHS, EPA, and DOT (via | | NRC) by fax. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35734 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 05/18/1999| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 15:52[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 05/18/1999| +------------------------------------------------+EVENT TIME: 15:00[EDT]| | NRC NOTIFIED BY: RON STRICKLAND |LAST UPDATE DATE: 05/19/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PETER ESELGROTH R1 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 85 Power Operation |85 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 1-HOUR SECURITY REPORT | | | | SAFEGUARDS SYSTEM DEGRADATION RELATED TO DETECTION/MONITORING/ALARM OF VITAL | | AREA ACCESS DOORS. IMMEDIATE COMPENSATORY ACTIONS TAKEN UPON DISCOVERY. | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. CONTACT THE | | HEADQUARTERS OPERATIONS CENTER FOR ADDITIONAL DETAILS. | | | | * * * RETRACTED AT 1300 EDT ON 5/19/99 BY MIKE KILEY TO FANGIE JONES * * * | | | | THIS NOTIFICATION WAS RETRACTED AS IT WAS ONLY REQUIRED TO BE LOGGED DUE TO | | COMPENSATORY MEASURES TAKEN UPON DISCOVERY ON THE DEGRADATION. THE LICENSEE | | NOTIFIED THE NRC RESIDENT INSPECTOR AND THE HEADQUARTERS OPERATIONS OFFICER | | NOTIFIED THE R1DO (PETER ESELGROTH) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35737 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 05/19/1999| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 10:19[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 05/19/1999| +------------------------------------------------+EVENT TIME: 08:35[CDT]| | NRC NOTIFIED BY: ADAMS |LAST UPDATE DATE: 05/19/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRENT CLAYTON R3 | |10 CFR SECTION: | | |AENS 50.72(b)(1)(v) ENS INOPERABLE | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | |2 N Y 55 Power Operation |55 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BOTH COMMERCIAL AND FTS PHONES OUT OF SERVICE. | | | | THE PHONE SYSTEM FAILED WHEN AN INADVERTENT UNDERGROUND CABLE WAS CUT DURING | | ROAD CONSTRUCTION ON A NEARBY ROAD, AMERITECH IS WORKING ON THE CABLE | | REPAIR AND IT SHOULD BE FIXED BY 1130 EDT. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | * * * UPDATE AT 1224 EDT ON 5/19/99 BY PHILLIP SHORT TO FANGIE JONES * * * | | | | ALL PHONE LINES HAVE BEEN RESTORED TO SERVICE. THE NRC RESIDENT INSPECTOR | | WAS NOTIFIED BY THE LICENSEE AND THE R3DO (BRENT CLAYTON) WAS NOTIFIED BY | | THE HEADQUARTERS OPERATION OFFICER. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35738 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 05/19/1999| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 12:12[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 05/19/1999| +------------------------------------------------+EVENT TIME: 11:00[CDT]| | NRC NOTIFIED BY: DAVID ERBE |LAST UPDATE DATE: 05/19/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PHYSICAL SECURITY REPORT | | | | Unescorted access granted inappropriately, immediate compensatory measures | | taken upon discovery. The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35739 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 05/19/1999| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 13:38[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/19/1999| +------------------------------------------------+EVENT TIME: 10:30[EDT]| | NRC NOTIFIED BY: TIM HEAFNER |LAST UPDATE DATE: 05/19/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-hour Condition of License report involving fire protection barriers. | | | | "On May 19,1999 at 1030 hours. McGuire Nuclear Station determined that | | provisions of the McGuire fire protection program had not been maintained as | | required by conditions C.(4) (Unit I) and C.(7) (Unit 2) of the McGuire | | Facility Operating License. | | | | "Selected Licensee Commitment 16.9-5 requires that all fire rated assemblies | | and sealing devices separating | | | | 1. Safety from non-safety related areas or, | | 2. Redundant analyzed post fire safe shutdown equipment or, | | 3. The Control Complex (Control Room, Cable Rooms, and Battery Rooms) from | | the remainder of the plant or, | | 4. Containment from Non-containment areas shall be operable. | | | | "Contrary to this, numerous fire barrier penetrations designed to satisfy | | the above separation criteria for certain containment to non-containment | | penetrations have been determined to be inoperable. This discovery was made | | as part of routine surveillance testing. A particular penetration design | | has been identified to have been installed in non-conformance with the | | design. The design specifies the incorporation of a fire resistive block | | material surrounded by a metal frame as the physical penetration which is | | installed in the wall as a unit. Necessary cables then penetrate through the | | fire resistive block. Physical penetrations were installed in excess of | | those actually necessary for transporting cables to accommodate future | | modifications or other contingencies. Penetrations in these 'blank | | locations' incorporated a welded steel plate as opposed to the design | | described above. This configuration has not been qualified as a 3 hour fire | | rated assembly. | | | | "Remedial actions required by Selected Licensee Commitment 16.9-5 have been | | implemented (fire watches). The ability of the facility to achieve safe | | shutdown conditions under a postulated design bases fire has not been | | compromised by the discovered condition. Therefore, McGuire did not operate | | outside the design basis of the plant. | | | | "The resident Inspector has been notified. A follow-up written report will | | be issued within 14 days. Note that this event is not reportable under the | | requirements of 10CFR50.72 or 10CFR50.73." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35740 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: U.S. ARMY |NOTIFICATION DATE: 05/19/1999| |LICENSEE: U.S. ARMY |NOTIFICATION TIME: 15:18[EDT]| | CITY: ROCK ISLAND REGION: 3 |EVENT DATE: 05/19/1999| | COUNTY: STATE: IL |EVENT TIME: [CDT]| |LICENSE#: 12-00722-06 AGREEMENT: Y |LAST UPDATE DATE: 05/19/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRENT CLAYTON R3 | | |ANN BOLAND R2 | +------------------------------------------------+LARRY CAMPER NMSS | | NRC NOTIFIED BY: JEFF HAVENNER |FEMA, DOE, USDA, HHS FAX | | HQ OPS OFFICER: STEVE SANDIN |EPA, DOT(VIA NRC) FAX | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING MUZZLE REFERENCE SENSOR CONTAINING 10 CURIE TRITIUM SOURCE. | | | | ON 5/19/99 WHILE TRAINING AT FT. PICKETT, VA, A TANK UNIT OF THE | | PENNSYLVANIA ARMY NATIONAL GUARD NOTED THAT A MUZZLE REFERENCE SENSOR | | MOUNTED ON THE END OF THE TANK GUN BARREL WAS MISSING. THE DEVICE CONTAINS | | 10 CURIES TRITIUM GAS. A SEARCH IS UNDERWAY TO LOCATE THE MISSING SOURCE. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35741 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NC BUREAU OF RAD PROTECTION |NOTIFICATION DATE: 05/19/1999| |LICENSEE: STERIGENICS INTERNATIONAL CORP |NOTIFICATION TIME: 15:53[EDT]| | CITY: CHARLOTTE REGION: 2 |EVENT DATE: 05/13/1999| | COUNTY: STATE: NC |EVENT TIME: 21:30[EDT]| |LICENSE#: NC 060-0974-1 AGREEMENT: Y |LAST UPDATE DATE: 05/19/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANN BOLAND R2 | | |LARRY CAMPER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: J. MARION EADDY III | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING PANORAMIC IRRADIATOR SOURCE RACK FAILURE TO | | RETRACT TO THE FULLY SHIELDED POSITION. | | | | The following information was provided by the NC Bureau of Radiation | | Protection via fax: | | | | LICENSEE: | | | | SteriGenics International Corporation | | 10811 Withers Cove Park | | Charlotte, NC 28278 | | N.C. Radioactive Materials License No. 060-0974-1 | | | | DESCRIPTION OF THE EVENT: | | | | The N. C. Division of Radiation Protection (DRP) was notified by telephone | | on 14 May 1999 at 15:50 that a power failure had occurred at the above | | referenced facility on 13 May 1999 at approximately 21:30. The licensee has | | two (2) irradiator pools at the facility. One of the racks (the 'smaller' | | activity rack) did not return to its fully shielded position as required by | | 10 CFR 36.37 and had to be manually lowered into the pool. The Radiation | | Safety Officer at the facility stated that no cell entry occurred and that | | all interlocks were operational during the event. | | | | SteriGenics is in the process of conducting tests of the uninterruptable | | power supply(ies) on site, as well as other systems. Their engineering staff | | is currently analyzing the root cause of the failure. SteriGenics has been | | notified by DRP of the 30 day reporting requirement in 10 CFR 36.83. | | | | North Carolina has assigned Log No. 99-08 to this incident. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35742 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 05/19/1999| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 17:27[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/19/1999| +------------------------------------------------+EVENT TIME: 15:00[CDT]| | NRC NOTIFIED BY: GREG JANAK |LAST UPDATE DATE: 05/19/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR REPORT INVOLVING VIOLATION OF OPERATING LICENSE BASED ON INOPERABLE | | AUXILIARY FEEDWATER TRAIN. | | | | "On May 13, 1999, it was discovered that Train 'D' Auxiliary Feedwater | | Regulating Valve FV-7526 would not open as required during surveillance | | testing. Investigations revealed that at 05:00 on May 10, 1999, Train 'D' | | Auxiliary Feedwater was removed from service to perform a static diagnostic | | test on AF-FV-7526. This test was completed and Train 'D' Auxiliary | | Feedwater was declared operable at 09:20 on May 11, 1999. | | | | "The failure of AF-FV-7526 was found to be caused by a misadjusted bracket | | for the limit switch which could have been caused during the static | | diagnostic test that was performed on May 10. 1999. This problem was | | corrected and Train 'D' Auxiliary Feedwater was declared operable at 00:10 | | on May 14,1999. This rendered Train 'D' Auxiliary Feedwater inoperable for a | | period of 91 hours and 10 minutes. This exceeded the time allowed under | | Technical Specification 3.7.1.2 action b., which states that the inoperable | | component must be restored to [an]operable[condition] within 72 hours. | | | | "This is a violation of Operating License NPF-076, Section 2G." | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35743 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRAIDWOOD REGION: 3 |NOTIFICATION DATE: 05/19/1999| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 20:53[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/19/1999| +------------------------------------------------+EVENT TIME: 19:17[CDT]| | NRC NOTIFIED BY: LARRY BROOKS |LAST UPDATE DATE: 05/19/1999| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |BRENT CLAYTON R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 4 Startup |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO SPIKING ON INTERMEDIATE RANGE NUCLEAR | | INSTRUMENT (IRNI) "N-36" DUE TO AN APPARENT INSTRUMENTATION PROBLEM. | | | | DURING STARTUP OF UNIT 2 FOLLOWING A REFUELING OUTAGE, THE IRNI "N-36" | | UNEXPECTEDLY SPIKED CAUSING A "HIGH FLUX" TRIP (FIRST OUT). IT APPEARS TO | | BE AN INSTRUMENTATION PROBLEM. THERE WAS NO I&C MAINTENANCE IN PROGRESS AT | | THE TIME. ALL CONTROL RODS FULLY INSERTED. DECAY HEAT WHICH IS LOW IS | | BEING REJECTED TO THE MAIN CONDENSER VIA THE STEAM DUMPS. THE STARTUP | | FEEDWATER PUMP IS IN SERVICE SUPPLYING WATER TO THE STEAM GENERATORS. ALL | | SYSTEM FUNCTIONED AS REQUIRED WITH ALL SAFETY-RELATED EQUIPMENT OPERATIONAL. | | THE LICENSEE WILL MAINTAIN THE UNIT IN MODE 3 PENDING THE RESULTS OF THE | | INVESTIGATION. THERE WAS NO RADIOACTIVE RELEASE. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021