Event Notification Report for May 14, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/13/1999 - 05/14/1999 ** EVENT NUMBERS ** 35560 35686 35690 35695 35710 35711 35712 35713 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35560 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 04/08/1999| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 15:41[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 02/17/1999| +------------------------------------------------+EVENT TIME: [EDT]| | NRC NOTIFIED BY: KILBY |LAST UPDATE DATE: 05/13/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |FRANK COSTELLO R1 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNESCORTED ACCESS GRANTED INAPPROPRIATELY. IMMEDIATE COMPENSATORY MEASURES | | TAKEN UPON DISCOVERY. CONTACT HOO FOR ADDITIONAL DETAILS. | | | | ******************** UPDATE AT 1131 ON 05/13/99 FROM MIKE DAVID TO TROCINE | | ******************** | | | | The following text is a portion of a facsimile received from the licensee: | | | | "North Atlantic [Energy Service Corporation] is providing this update | | because the NRC Daily Report (Event Number: 35560) described this event as | | 'Unescorted Access Granted Inappropriately.' North Atlantic believes that | | the Unescorted Access was granted in accordance with the appropriate | | procedures and that it did not violate any NRC regulations; hence, it was | | appropriate. Furthermore, the appropriate action was taken when the FBI | | information was received. North Atlantic believes that the event would have | | been more accurately described as 'Unescorted Access Revoked.'" | | | | Contact the NRC operations officer for additional details. | | | | The licensee notified the NRC resident inspector. The NRC operations | | officer notified the R1DO (Caruso). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35686 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 05/06/1999| | UNIT: [] [] [3] STATE: CT |NOTIFICATION TIME: 18:44[EDT]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 05/06/1999| +------------------------------------------------+EVENT TIME: 18:00[EDT]| | NRC NOTIFIED BY: MARTIN |LAST UPDATE DATE: 05/13/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES LINVILLE R1 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N N 0 Cold Shutdown |0 Cold Shutdown | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VALVE FAILED LOCAL LEAK RATE TEST (LLRT). | | | | VALVE 3QSS*V4 IS A CHECK VALVE IN THE QUENCH SPRAY SYSTEM, AND THE CAUSE OF | | THE LLRT FAILURE IS UNKNOWN AND BEING INVESTIGATED, BUT MOST LIKELY MAY BE | | DUE TO VALVE DEGRADATION. WHEN THE RESULTS OF ITS LLRT WERE ADDED TO THE | | OTHER CATEGORY "C" VALVES' RESULTS, THE TOTAL LEAKAGE EXCEEDED TECHNICAL | | SPECIFICATION ALLOWABLE LIMITS OF 43 SCFH (TOTAL MEASURED CATEGORY "C" WAS | | 335 SCFH); HOWEVER, THE TOTAL LEAKAGE OF EVERYTHING STILL DID NOT EXCEED THE | | 0.6 La VALUE. CORRECTIVE ACTION WILL BE TO REPAIR THE VALVE PRIOR TO | | STARTUP. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED ALONG WITH STATE, LOCAL AND OTHER | | GOVERNMENT AGENCIES. | | | | * * * UPDATE 1134 5/13/99 FROM STEVE LAWHEAD TAKEN BY STRANSKY * * * | | | | Local leak rate testing of valve SIL*V6 (RHS Loop 1 Cold Leg Check Valve) | | found the leakage to be excessive. This leakage, when combined with the | | other known leakage, caused TS LCO 3.6.1.2.b to be exceeded. The TS | | requires a combined leakage rate of less than 0.6 La for all penetrations | | and valves subject to Type B and C tests, when pressurized to Pa. The NRC | | resident inspector has been informed of this update. Notified R1DO | | (Cowgill). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35690 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 05/07/1999| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 12:41[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 05/07/1999| +------------------------------------------------+EVENT TIME: 09:50[EDT]| | NRC NOTIFIED BY: LANGE |LAST UPDATE DATE: 05/13/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES LINVILLE R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 59 Power Operation |59 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE DECLARED THE HIGH PRESSURE CORE SPRAY (HPCS) SYSTEM INOPERABLE | | AND ENTERED A 14-DAY LCO ACTION STATEMENT. | | | | THE HPCS SYSTEM FAILED TO MEET THE CHANNEL CHECK CRITERIA AND WAS DECLARED | | INOPERABLE, BUT FUNCTIONAL. TWO TRIP UNITS WERE FOUND NOT TO BE WITHIN THE | | 13-INCH LIMIT FOR LEVEL INITIATION INSTRUMENTATION. (THEY MEASURED 15 | | INCHES.) A WORK ORDER HAS BEEN GENERATED TO CORRECT THE PROBLEM BEFORE THE | | TIME CLOCK EXPIRES FOR THE LCO ACTION STATEMENT. THE REACTOR IS CURRENTLY | | IN SINGLE LOOP OPERATION AT 59% POWER. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | ***RETRACTION ON 04/13/99 AT 1651 EDT FROM ROY GREEN TAKEN BY MACKINNON*** | | | | IT HAS BEEN DETERMINED THAT THE CHANNEL CHECK CRITERIA WAS MET AND THAT THE | | HIGH PRESSURE CORE SPRAY SYSTEM WAS, THEREFORE, NOT INOPERABLE. PROCEDURAL | | GUIDANCE THAT LED TO THE INOPERABLE DETERMINATION HAS BEEN CHANGED AFTER | | ENGINEERING PROVIDED THE NECESSARY JUSTIFICATION. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. THE R1DO (JOHN CARUSO) | | WAS NOTIFIED BY THE NRC OPERATIONS OFFICER. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35695 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/09/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 20:22[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/09/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:45[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/13/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MONTE PHILLIPS R3 | | DOCKET: 0707002 |JOHN GREEVES NMSS | +------------------------------------------------+FRANK CONGEL IRO | | NRC NOTIFIED BY: LARSON | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NRC BULLETIN 91-01, 4-HOUR REPORT | | | | AT 1645 ON 05/09/99, DURING A PRESSURE DECAY TEST OF THE #1 AUTOCLAVE IN THE | | X-342 BUILDING, A LIGHT DUSTING OF UO2F2 WAS OBSERVED INSIDE THE AUTOCLAVE, | | AND A HEAVIER ACCUMULATION OF UO2F2 WAS OBSERVED ON THE PRESSURE DECAY | | FILTER USED TO PREVENT URANIUM FROM ENTERING THE AUTOCLAVE DURING THIS TEST. | | THE AUTOCLAVE WAS PLACED IN A CONTAINMENT MODE ISOLATING IT FROM ALL SUPPORT | | SYSTEMS. HEALTH PHYSICS TECHNICIANS PERFORMED CONTAMINATION AND AIRBORNE | | SAMPLING, AND ALL SAMPLES WERE LESS THAN DETECTABLE LIMITS. HAVING URANIUM | | INSIDE THE SHELL OF THE AUTOCLAVE IS A LOSS OF ONE CONTROL OF THE DOUBLE | | CONTINGENCY PRINCIPLE CONTAINED IN NCSA_342A002. THE ACCUMULATION OF UO2F2 | | ON THE OUTSIDE OF THE PRESSURE DECAY FILTER IS NOT EXPECTED. ADDITIONAL | | EVALUATIONS ARE BEING CONDUCTED AT THIS TIME. | | | | THERE IS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. | | THIS EVENT DOES NOT PRESENT ANY IMMINENT DANGER OF A CRITICALITY. | | | | THE AUTOCLAVE HAS BEEN ISOLATED FROM ALL POTENTIAL MODERATOR SOURCES, SO | | CRITICALITY IS NOT POSSIBLE. MODERATION, ENRICHMENT, AND GEOMETRY | | PARAMETERS WERE MAINTAINED THROUGHOUT THIS EVENT. THE UNLIKELIHOOD OF | | URANIUM INSIDE THE AUTOCLAVE SHELL AND OUTSIDE OF THE UF6 CYLINDER WAS A | | LOST PARAMETER. THE AUTOCLAVE WAS TAGGED TO PREVENT ANY OPERATION UNTIL | | RECOVERY PLANS ARE DEVELOPED. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED BY PORTSMOUTH PERSONNEL. | | | | ***UPDATE ON 05/13/99 AT 2248 EDT FROM J. CASTLE TAKEN BY MACKINNON*** | | | | REVISION TO THE NCS ANOMALOUS CONDITIONS INCIDENT REPORT (NSI-99-02603 REV. | | 1) IDENTIFIES THAT THE MAXIMUM AMOUNT OF U-235 THAT COULD HAVE BEEN RELEASED | | IN THE AUTOCLAVE WAS 755.2 GRAMS. THIS AMOUNT OF U-235 IS LESS THAN THE | | ALWAYS SAFE MASS OF 800 GRAMS FOR 5% ENRICHED MATERIAL AND IS WELL BELOW THE | | SUBCRITICAL LIMIT OF 1640 GRAMS AT 5% ENRICHMENT. THIS INCIDENT REPRESENTS | | A DEGRADATION IN THE MARGIN OF SAFETY FOR THE MASS CONTROL PARAMETER BUT DID | | NOT RESULT IN A LOSS OF DOUBLE CONTINGENCY BASED ON THE MAXIMUM AMOUNT OF | | MATERIAL POTENTIALLY LOST. | | | | SAFETY SIGNIFICANCE OF EVENTS: THE EVENT RESULTED IN A DUSTING OF URANIUM | | INSIDE THE AUTOCLAVE (A/C) SHELL AS WELL AS URANIUM ON THE PRESSURE DECAY | | FILTER. THE MAXIMUM CREDIBLE AMOUNT OF U-235 RELEASED INSIDE THE A/C WAS | | CALCULATED BY ENGINEERING TO BE 755.2 GRAMS OF U-235 BASED ON ASSUMING THE | | ENTIRE AVAILABLE UF6 PIPING VOLUME AND PRESSURE DECAY FILTER VOLUME WERE | | FILLED WITH URANIUM AT MAXIMUM DENSITY PRIOR TO THE EVENT. THIS IS LESS | | THAN THE SAFE MASS OF 800 GRAMS U-235 AT 5% ENRICHMENT AND MUCH LESS THAN | | THE SUBCRITICAL MASS LIMIT OF 1,640 GRAMS OF U-235. THEREFORE, A | | CRITICALITY COULD NOT HAVE OCCURRED WITHOUT THE ADDITION OF MORE MASS AND | | MODERATION TO THE AUTOCLAVE. BOTH ADDITIONS ARE UNLIKELY AS THE AUTOCLAVE | | IS SHUTDOWN AND ISOLATED, PENDING CLEANUP. THE DOUBLE CONTINGENCY PRINCIPLE | | WAS, THEREFORE, STILL MET FOLLOWING THIS EVENT. | | | | POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO OF HOW CRITICALITY | | COULD OCCUR): A CRITICALITY WOULD ONLY BE POSSIBLE IF MORE THAN 300 lbs OF | | WATER IS ADDED TO THE AUTOCLAVE. THE AUTOCLAVE HAS BEEN ISOLATED FROM ALL | | POTENTIAL MODERATOR SOURCES. AT LEAST 885 GRAMS OF U-235 WOULD NEED TO BE | | ADDED TO THE AUTOCLAVE IN ADDITION TO AT LEAST 300 POUNDS OF WATER IN ORDER | | FOR A CRITICALITY TO BE POSSIBLE IN THE AUTOCLAVE GEOMETRY. THE AUTOCLAVE | | HAS BEEN ISOLATED FROM ALL POTENTIAL SOURCES OF MODERATION AND URANIUM. | | MODERATION AND ENRICHMENT CONTROL WERE MAINTAINED, AND ALSO, GEOMETRY OF THE | | PRESSURE DECAY FILTER WAS MAINTAINED. | | | | NUCLEAR CRITICALITY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION OF THE | | FAILURES OR DEFICIENCIES: THE PRESENCE OF UO2F2 INSIDE THE AUTOCLAVE SHELL | | IN AN AMOUNT LESS THAN A SAFE MASS REPRESENTS A DEGRADATION IN ONE OF THE | | TWO CONTROLS FOR DOUBLE CONTINGENCY, BUT IT DOES NOT REPRESENT A COMPLETE | | LOSS OF THAT CONTROL. TWO UNLIKELY, INDEPENDENT AND CONCURRENT EVENTS WOULD | | STILL NEED TO OCCUR IN ORDER FOR A CRITICALITY TO BE POSSIBLE IN THE | | AUTOCLAVE. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: | | AT 1805 HOURS ON 05/09/99, THE AUTOCLAVE WAS DANGER TAGGED TO PREVENT ANY | | OPERATION UNTIL RECOVERY PLANS ARE DEVELOPED. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED OF THIS EVENT BY THE CERTIFICATE | | HOLDER. THE NMSS EO (JOE HOLONICH) AND R3DO (ROGER LANKSBURY) WERE NOTIFIED | | BY THE NRC OPERATIONS OFFICER. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35710 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BYRON REGION: 3 |NOTIFICATION DATE: 05/13/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 09:47[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/13/1999| +------------------------------------------------+EVENT TIME: 08:10[CDT]| | NRC NOTIFIED BY: DAVE FLOWERS |LAST UPDATE DATE: 05/13/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO AN INADVERTENT POWER RANGE HIGH FLUX SIGNAL | | DURING THE PERFORMANCE OF SURVEILLANCE TESTING | | | | At 0810 CDT, Unit 1 experienced an automatic reactor trip from 100% power | | due to an inadvertent power range high flux trip signal during the | | performance of instrumentation and control surveillance testing. All rods | | fully inserted. Following the trip, feedwater isolated as expected, and the | | auxiliary feedwater pumps automatically started on low 2 steam generator | | level (18% narrow range) as designed. (Steam generator level decreased to | | 0% narrow range, and normal steam generator level is 63%.) In addition, the | | 'K' steam dump failed to reclose, and this caused reactor coolant system | | temperature to decrease slightly below the P-12 setpoint of 550�F for a | | short period of time. (Normal temperature is 557�F.) When temperature | | reached 550�F, the steam dumps automatically isolated. The 'K' steam dump | | was manually isolated. The steam dumps were re-opened when temperature went | | above 550�F. All other post-trip actuations occurred as expected. None of | | the primary safety valves or power-operated relief valves lifted. However, | | some of the secondary feedwater heater relief valves lifted. The licensee | | stated that it is not unusual for these valves to lift following a reactor | | trip, and the licensee plans to isolate them. The licensee also stated that | | these valves are not large enough to cause a problem with cooldown. There | | were no emergency core cooling system actuations, and none were required. | | An investigation to determine the exact cause of the reactor trip is in | | progress. | | | | The unit is currently stable in Mode 3. The reactor coolant pumps, normal | | charging and letdown, and pressurizer heaters and sprays are being utilized | | for primary system transport, level, and pressure control. Containment | | parameters are normal. Secondary steam is being dumped to the condenser, | | and water is being supplied to the steam generators via the auxiliary | | feedwater pumps and startup feedwater pump. The licensee plans to secure | | auxiliary feedwater. Offsite power is available, and the emergency diesel | | generators are operable and available if needed. The licensee is in the | | process of re-closing the ring bus located in the switchyard to increase | | offsite power reliability. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35711 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: GREEN BAY PACKAGING |NOTIFICATION DATE: 05/13/1999| |LICENSEE: GREEN BAY PACKAGING |NOTIFICATION TIME: 14:12[EDT]| | CITY: WINCHESTER REGION: 2 |EVENT DATE: 05/21/1998| | COUNTY: FREDERICK STATE: VA |EVENT TIME: 12:00[EDT]| |LICENSE#: 45-25268-01 AGREEMENT: N |LAST UPDATE DATE: 05/13/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |RUDOLPH BERNHARD R2 | | |SCOTT MOORE NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: M. DICKEY | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |IBBF 30.50(b)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INTERMITTENT STUCK SHUTTER (MECHANICAL PROBLEM) ON OHMART SCANNING GAUGES | | REPORTED AFTER PERFORMANCE OF AN NRC INSPECTION. | | | | The licensee reported two past incidents which occurred at their facility | | after an NRC inspection determined that the two past incidences should have | | been reported. | | | | On 05/19/98 or 05/20/98, the shutter of an Ohmart scanning gauge, used to | | measure the thickness of paper, was found to intermittently stick open. As | | of late 1993, the Ohmart scanning gauge (Model # OD120) contained 300 | | millicuries of Kr-85. Kr-85 is a beta-gamma emitter with a half life of | | 10.76 years. On 05/21/98, Alternative Process Service of Alabama repaired | | the intermittently sticking shutter on the gauge. There was no exposure to | | personnel in the area when the shutter was stuck open because the gauge is | | hard to get to (0.5" gap). It was determined that broken screws had caused | | the shutter to intermittently stick open. | | | | On 05/03/99, a shutter on a different Ohmart scanning gauge was found to be | | stuck open. The licensee lightly tapped the source case of the Ohmart | | scanning gauge (Model # OD120) which caused the shutter to go closed. The | | licensee called Honeywell Measurex and informed them that the shutter had | | stuck open on the scanning gauge. Honeywell Measurex will send someone to | | Green Bay Packaging during the week of 05/17/99 to repair the scanning | | gauge. This gauge also contained 300 millicuries of Kr-85 as of late 1993. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35712 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 05/14/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 00:30[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 05/13/1999| +------------------------------------------------+EVENT TIME: 23:00[CDT]| | NRC NOTIFIED BY: RICH CHEAR |LAST UPDATE DATE: 05/14/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 4 Startup |4 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT THE LEAK RATE OF A MAIN STEAM ISOLATION VALVE IS GREATER THAN | | THE INBOARD LEAKAGE CONTROL SYSTEM PROVEN TREATMENT FLOW RATE | | | | The following text is a portion of a facsimile received from the licensee: | | | | "Clinton Power Station has identified that the Inboard Main Steam Isolation | | Valve (MSIV) Leakage Control System (LCS) is not calibrated to process the | | design MSIV leakage of 28 standard cubic feet per hour (scfh) per one main | | steam line. One MSIV has been identified as having a leakage rate of 22.5 | | scfh which is greater than the Inboard LCS proven treatment flow rate of | | 21.3 scfh. Currently, the engineering team is still investigating." | | | | The licensee stated that the unit was in a 30-day technical specification | | limiting condition for operation as a result of this issue. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35713 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 05/14/1999| | UNIT: [] [] [3] STATE: CA |NOTIFICATION TIME: 01:54[EDT]| | RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 05/13/1999| +------------------------------------------------+EVENT TIME: 21:44[PDT]| | NRC NOTIFIED BY: MATT THURBURN |LAST UPDATE DATE: 05/14/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 M/R Y 97 Power Operation |0 Hot Standby | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP AND MANUAL INITIATION OF EMERGENCY FEEDWATER DUE TO THE | | LOSS OF BOTH MAIN FEEDWATER PUMPS DURING THE PERFORMANCE OF MAINTENANCE ON | | THE FEEDWATER CONTROL SYSTEM | | | | At 2144 PDT on 05/13/99, both main feedwater pumps tripped for unknown | | reasons. Reactor operators recognized this loss, manually tripped the | | reactor from 97% power, and manually initiated emergency feedwater. All | | rods fully inserted, and all systems functioned as required. There were no | | engineered safety feature actuations other than the manual initiation of | | emergency feedwater. The main steam isolation valves remained open, none of | | the relief valves opened, and there was no loss of offsite power. | | | | The cause of the loss of both feedwater pumps is under investigation. The | | licensee stated that maintenance personnel were performing voltage checks in | | the feedwater control system at the time of the event. | | | | The reactor is currently stable in Mode 3. The reactor coolant pumps, | | normal charging and letdown, and pressurizer heaters and sprays are being | | utilized for primary system transport, level, and pressure control. | | Containment parameters are normal. Emergency feedwater is supplying water | | to the steam generators, and secondary steam is being dumped to the main | | condenser. Offsite power is available. The 'A' emergency diesel generator | | is currently out of service for planned maintenance. However, the 'B' | | emergency diesel generator and the crossties from the other unit are | | available if needed. | | | | The licensee notified the NRC resident inspector and plans to issue a | | media/press release. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021