Event Notification Report for May 13, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/12/1999 - 05/13/1999 ** EVENT NUMBERS ** 35704 35705 35706 35707 35708 35709 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35704 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 05/12/1999| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 03:59[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 05/12/1999| +------------------------------------------------+EVENT TIME: 00:38[CDT]| | NRC NOTIFIED BY: DAVE DEES |LAST UPDATE DATE: 05/12/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: |JOSE CALVO NRR | |AESF 50.72(b)(2)(ii) ESF ACTUATION |FRANK CONGEL IRO | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 55 Power Operation |55 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PARTIAL LOSS OF OFFSITE POWER (ONE OF THREE SOURCES) DUE TO A TRANSFORMER | | LOCKOUT | | | | At 0038 CDT, the east bus (345 kV) was lost due to a lockout on the #7 | | transformer. The loss of the east bus resulted in the loss of normal power | | to the 'A' safeguards bus (4.16 kV). On loss of power to the #7 | | transformer, a shutdown sequencer actuation occurred due to low power. | | This caused the 'A' emergency diesel generator to automatically start and | | load the bus. The following equipment also automatically started: 'A' | | centrifugal charging pump, 'A' component cooling water pump, 'A' essential | | service water pump, 'A' control room air conditioning unit, 'A' class 1E air | | conditioning unit, 'A' motor-driven auxiliary feedwater pump, 'A' and 'C' | | containment coolers, and the turbine-driven auxiliary feedwater pump. The | | licensee stated that all systems functioned as required and that there was | | nothing unusual or not understood. | | | | At 0058 CDT, the licensee reset the #7 transformer lockout, and the east bus | | was restored to service at 0059 CDT. At 0244 CDT, the licensee re-energized | | the #7 transformer (the normal power feed to the safeguards bus | | transformer), and normal offsite power was restored to the 'A' emergency bus | | at 0256 CDT. | | | | The transformer lockout was initially believed to be caused by a lightening | | strike and was later determined to be caused by a raccoon. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35705 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 05/12/1999| | UNIT: [1] [2] [3] STATE: SC |NOTIFICATION TIME: 13:29[EDT]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 05/12/1999| +------------------------------------------------+EVENT TIME: 12:58[EDT]| | NRC NOTIFIED BY: TODD |LAST UPDATE DATE: 05/12/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RUDOLPH BERNHARD R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAS OPERATED OUTSIDE THE DESIGN BASIS IN THE PAST DURING STARTUP. | | | | ON 03/18/99, FRAMATOME (B&W) REQUESTED THE LICENSEE REVIEW A | | PRESSURE-TEMPERATURE LIMIT ANALYSIS FOR OCONEE NUCLEAR STATION | | APPLICABILITY. THE ANALYSIS WAS PERFORMED FOR ANOTHER B&W PLANT AND SHOWED | | THAT PRESSURE INCREASES ARE LARGER WITH NITROGEN IN THE PRESSURIZER. THIS | | RESULTED IN A REVISED SET OF LOW-TEMPERATURE OVERPRESSURE PROTECTION ( LTOP) | | LIMITS FOR STEAM AND NITROGEN OPERATION AT THE OTHER PLANT. FRAMATOME WAS | | NOT AWARE OF NITROGEN PRESENCE BEING CONSIDERED IN THE DETERMINATION OF LTOP | | LIMITS. | | | | OPERATIONS WAS REQUESTED TO USE A DEDICATED LTOP OPERATOR, AS A CONSERVATIVE | | MEASURE, IF LTOP APPLICABILITY EXISTED AND NITROGEN PRESSURE WAS IN THE | | PRESSURIZER. THIS IS A COMPENSATORY MEASURE REQUIRED BY TECHNICAL | | SPECIFICATION 3.4.12, CONDITION 'F.' | | | | THE LICENSEE HAS COMPLETED AN EVALUATION THAT CONCLUDED THAT NITROGEN | | OVERPRESSURE DURING STARTUP COULD RESULT IN LESS THAN 10 MINUTES BEING | | AVAILABLE FOR OPERATOR RESPONSE AFTER THE ALARM SETPOINT IS REACHED DURING | | AN LTOP EVENT. SINCE OPERATOR RESPONSE TO AN ALARM IS ONE TRAIN OF THE | | OCONEE LTOP SYSTEM, THIS MEANS THAT THIS TRAIN HAS BEEN INOPERABLE DURING | | PORTIONS OF PAST STARTUPS. THE APPLICABLE TIME PERIODS ARE ASSUMED TO HAVE | | EXCEEDED THE 4 HOURS ALLOWED BY TECHNICAL SPECIFICATION 3.4.12, CONDITION | | 'F,' FOR IMPLEMENTING COMPENSATORY MEASURES. SINCE THE LTOP MITIGATION | | SYSTEM WOULD NOT MEET THE SINGLE FAILURE CRITERION DURING THESE TIME | | PERIODS, THIS CONDITION IS BEING REPORTED AS OPERATION OUTSIDE THE DESIGN | | BASIS OF THE PLANT. | | | | LTOP REQUIREMENTS DO NOT APPLY DURING PLANT OPERATION IN THE RUN MODE, AND | | THERE HAVE BEEN NO LTOP EVENTS DURING PLANT OPERATION WITH A NITROGEN | | PRESSURE BUBBLE IN THE PRESSURIZER. THEREFORE, THIS IS NOT CONSIDERED TO | | REPRESENT AN ACTUAL CHALLENGE TO THE HEALTH AND SAFETY OF THE PUBLIC. | | | | THE RESIDENT INSPECTOR WAS INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35706 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 05/12/1999| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 16:12[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 05/12/1999| +------------------------------------------------+EVENT TIME: 15:15[EDT]| | NRC NOTIFIED BY: GREEN |LAST UPDATE DATE: 05/12/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CURTIS COWGILL R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR CORE ISOLATION COOLING (RCIC) WAS DECLARED INOPERABLE DURING THE | | QUARTERLY SURVEILLANCE TEST. | | | | DURING THE PERFORMANCE OF THE NORMAL QUARTERLY RCIC SURVEILLANCE TEST, THE | | RCIC TURBINE UNEXPECTEDLY TRIPPED WHEN THE SUCTION PATH WAS SWAPPED FROM | | THE SUPPRESSION POOL TO THE CONDENSATE STORAGE TANK. THE CAUSE OF THE RCIC | | TURBINE TRIP IS UNKNOWN AT THIS TIME, AND TROUBLESHOOTING IS CURRENTLY IN | | PROGRESS. THE PLANT IS IN A 14-DAY LIMITING CONDITION FOR OPERATION ACTION | | STATEMENT. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35707 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RAD CONTROL |NOTIFICATION DATE: 05/12/1999| |LICENSEE: CITRUS MEMORIAL HEALTH FOUNDATION, IN|NOTIFICATION TIME: 17:32[EDT]| | CITY: INVERNESS REGION: 2 |EVENT DATE: 05/12/1999| | COUNTY: STATE: FL |EVENT TIME: [EDT]| |LICENSE#: 2067-1 AGREEMENT: Y |LAST UPDATE DATE: 05/12/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |RUDOLPH BERNHARD R2 | | |JOE HOLONICH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ADAMS | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE FLORIDA BUREAU OF RADIATION CONTROL REPORTED A RADIOLOGICAL INCIDENT, | | #FL99-066, WHICH OCCURRED AT THE CITRUS MEMORIAL HEALTH FOUNDATION, INC., | | LOCATED IN INVERNESS, FLORIDA. | | | | SIX IMPLANTED I-125 SEEDS MEASURING 0.265 mCi EACH WERE REMOVED FROM A | | PATIENT AT THE FACILITY. WHEN THE SEEDS WERE TO BE RETRIEVED FOR SHIPMENT | | BACK TO THE MANUFACTURER, ONLY ONE COULD BE FOUND. A THOROUGH SURVEY OF THE | | ROOM AND SEWER TRAPS FAILED TO LOCATE THE OTHER FIVE SEEDS. THE MISSING | | MATERIAL WAS PROBABLY LOST IN THE SANITARY SEWER. A STATE INSPECTOR IS | | INVESTIGATING THE INCIDENT. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35708 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: KANSAS DEPT OF HEALTH & ENVIROMENT |NOTIFICATION DATE: 05/12/1999| |LICENSEE: VIA CHRISTI REGIONAL MEDICAL CTR |NOTIFICATION TIME: 18:11[EDT]| | CITY: WICHITA REGION: 4 |EVENT DATE: 05/07/1999| | COUNTY: SEDGWICK STATE: KS |EVENT TIME: 10:00[CDT]| |LICENSE#: 19-C030-01 AGREEMENT: Y |LAST UPDATE DATE: 05/12/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHARLES CAIN R4 | | |JOE HOLONICH NMSS | +------------------------------------------------+FRANK CONGEL IRO | | NRC NOTIFIED BY: FRAASS | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ON 05/12/99, THE VIA CHRISTI REGIONAL MEDICAL CENTER NOTIFIED THE KANSAS | | RADIATION CONTROL PROGRAM THAT A PROBABLE MEDICAL MISADMINISTRATION OCCURRED | | ON 05/07/99 AT 1000 CDT. | | | | A 28-YEAR-OLD FEMALE, WHO IS APPARENTLY 19 WEEKS PREGNANT, WAS GIVEN A | | THERAPEUTIC DOSE OF I-131 (11.8 MILLICURIES). THE CENTER'S RADIATION SAFETY | | OFFICER CONTACTED REAC/TS, AND THE ONCOLOGIST WHO REQUESTED THE STUDY HAS | | ALREADY BEEN CONTACTED BY A PHYSICIAN FROM REAC/TS. A SECOND CONFERENCE | | CALL IS SCHEDULED WITH THE PATIENT'S OB/GYN PHYSICIAN. THE KANSAS | | DEPARTMENT OF HEALTH AND ENVIRONMENT HAS BEGUN AN INVESTIGATION INTO THIS | | INCIDENT. | | | | CONTACT THE OPERATIONS CENTER FOR THE STATE CONTACT'S TELEPHONE NUMBER. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35709 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/12/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 22:42[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/12/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 02:29[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/12/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |ROGER LANKSBURY R3 | | DOCKET: 0707001 |JOE HOLONICH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CAGE | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF THE UF6 RELEASE DETECTION SYSTEM - 24-HOUR NOTIFICATION | | | | THE FACILITY EXPERIENCED A FAILURE OF THE UF6 RELEASE DETECTION SAFETY | | SYSTEM IN C-333, UNIT 5, CELL 3. THE FAILURE OCCURRED DURING THE | | TWICE-PER-SHIFT TECHNICAL SAFETY REQUIREMENT (TSR) SURVEILLANCE WHICH | | REQUIRES A TEST FIRING OF THE DETECTOR HEADS. THE SAFETY SYSTEM WAS | | IMMEDIATELY DECLARED INOPERABLE, AND THE TSR-REQUIRED ACTIONS, WHICH INCLUDE | | PLACING A SMOKE WATCH IN THE AFFECTED AREA, WERE IMPLEMENTED. IN ADDITION, | | THE OPERATING PRESSURE OF THE AFFECTED EQUIPMENT WAS REDUCED TO BELOW | | ATMOSPHERIC PRESSURE WHICH PLACED THE EQUIPMENT IN A MODE IN WHICH THE | | SAFETY SYSTEM WAS NOT REQUIRED TO BE AVAILABLE AND OPERABLE. | | | | THE NRC RESIDENT INSPECTOR WAS INFORMED. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021