The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for May 11, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           05/10/1999 - 05/11/1999

                              ** EVENT NUMBERS **

35696  35697  35698  35699  

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   35696       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  NEW YORK CITY DEPART OF HEALTH       |NOTIFICATION DATE: 05/10/1999|
|LICENSEE:  BROWNING FERRIS INDUSTRIES           |NOTIFICATION TIME: 11:47[EDT]|
|    CITY:  NEW YORK                 REGION:  1  |EVENT DATE:        05/07/1999|
|  COUNTY:                            STATE:  NY |EVENT TIME:        08:00[EDT]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  05/10/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CURTIS COWGILL       R1      |
|                                                |FRED COMBS           NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  BORRI (NYC DPT OF HEALTH)    |                             |
|  HQ OPS OFFICER:  CHAUNCEY GOULD               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LANDFILL REJECTED HOSPITAL SOLID WASTE CONTAINING 300 MILLICURIES OF         |
| TECHNETIUM-99m                                                               |
|                                                                              |
| BROWNING FERRIS INDUSTRIES (BFI) RECEIVED A LOAD OF SOLID WASTE FROM CITY    |
| HOSPITAL  CENTER AT ELMHURST IN NEW YORK CITY AND TOOK IT TO THEIR TRANSFER  |
| STATION IN BROOKLYN, NY.   THE WASTE WAS THEN MOVED TO A LANDFILL IN         |
| COMSTOCK, PA  WHERE IT WAS REJECTED AND RETURNED TO THE BFI FACILITY IN      |
| BROOKLYN ON 05/07/99.  THE WASTE CONTAINED APPROXIMATELY 300 MILLICURIES OF  |
| TECHNETIUM-99m.  THE WASTE IS BEING RETURNED TO THE HOSPITAL.  THE CITY IS   |
| INVESTIGATING THIS INCIDENT.                                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35697       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: NINE MILE POINT          REGION:  1  |NOTIFICATION DATE: 05/10/1999|
|    UNIT:  [1] [] []                 STATE:  NY |NOTIFICATION TIME: 15:18[EDT]|
|   RXTYPE: [1] GE-2,[2] GE-5                    |EVENT DATE:        05/10/1999|
+------------------------------------------------+EVENT TIME:        13:00[EDT]|
| NRC NOTIFIED BY:  BELDEN                       |LAST UPDATE DATE:  05/10/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CURTIS COWGILL       R1      |
|10 CFR SECTION:                                 |                             |
|ADAS 50.72(b)(2)(i)      DEG/UNANALYZED COND    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNIT 1 VALVES FAILED THEIR LOCAL LEAK RATE TEST.                             |
|                                                                              |
| UNDER THE APPENDIX J PROGRAM PLAN (#NMP1-APPJ-001) SECTION III/1.8 OUTAGE    |
| TESTING REQUIREMENTS INCLUDE MAINTAINING A COMBINED TOTAL TYPE 'B' AND 'C'   |
| AS-FOUND MINIMUM PATHWAY LEAKAGE.  IN ACCORDANCE WITH TECH SPEC 6.16.4, THE  |
| COMBINED LOCAL LEAK RATE TEST (TYPE 'B' & 'C' TESTS INCLUDING AIRLOCKS)      |
| ACCEPTANCE CRITERIA IS LESS THAN 0.6 La, CALCULATED IN THE MINIMUM PATHWAY   |
| BASIS, AT ALL TIMES WHEN CONTAINMENT INTEGRITY IS REQUIRED.  THE VALUE OF    |
| 0.6 La FOR UNIT 1 WAS CALCULATED TO BE 388.44 SCFH.  THE RESULTS OF THE TEST |
| MEASURED 388.756 SCFH, WHICH EXCEED THE CALCULATED VALUE FOR THE COMBINED    |
| AS-FOUND TYPE 'B' AND 'C' LOCAL LEAK RATE TESTS.  THIS CONDITION WOULD HAVE  |
| BEEN A TECH SPEC VIOLATION IF IDENTIFIED DURING POWER OPERATION.             |
|                                                                              |
| THIS CONDITION WILL BE CORRECTED PRIOR TO PLANT RESTART.                     |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35698       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PEACH BOTTOM             REGION:  1  |NOTIFICATION DATE: 05/10/1999|
|    UNIT:  [2] [3] []                STATE:  PA |NOTIFICATION TIME: 19:51[EDT]|
|   RXTYPE: [2] GE-4,[3] GE-4                    |EVENT DATE:        05/10/1999|
+------------------------------------------------+EVENT TIME:        09:30[EDT]|
| NRC NOTIFIED BY:  KOVALCHICK                   |LAST UPDATE DATE:  05/10/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CURTIS COWGILL       R1      |
|10 CFR SECTION:                                 |                             |
|HFIT 26.73               FITNESS FOR DUTY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2     N          Y       100      Power Operation  |100      Power Operation  |
|3     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TRACES OF A CONTROLLED SUBSTANCE FOUND IN A BATHROOM INSIDE THE PROTECTED    |
| AREA                                                                         |
|                                                                              |
| ON 04/15/99, THREE SUSPECTED ITEMS WERE FOUND IN A BATHROOM INSIDE THE PLANT |
| PROTECTED AREA AND WERE TURNED OVER TO PECO ENERGY CORPORATE SECURITY.  AT   |
| 0930 ON 05/10/99, THE LICENSEE RECEIVED A REPORT FROM AN INDEPENDENT         |
| LABORATORY THAT INDICATED THAT, ALTHOUGH THERE WAS NO VISIBLE RESIDUE        |
| PRESENT, A GAS CHROMATOGRAPHY/MASS SPECTROMETRY DETECTED AND CONFIRMED THE   |
| PRESENCE OF A CONTROLLED SUBSTANCE.  AT THE PRESENT TIME, THE SUSPECTED      |
| ITEMS HAVE NOT BEEN ASSOCIATED WITH ANY SPECIFIC INDIVIDUAL.  THE LICENSEE   |
| IS CONTINUING TO INVESTIGATE THIS SITUATION.                                 |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35699       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: RIVER BEND               REGION:  4  |NOTIFICATION DATE: 05/10/1999|
|    UNIT:  [1] [] []                 STATE:  LA |NOTIFICATION TIME: 21:34[EDT]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        05/10/1999|
+------------------------------------------------+EVENT TIME:        16:58[CDT]|
| NRC NOTIFIED BY:  CARLSON                      |LAST UPDATE DATE:  05/10/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |CHARLES CAIN         R4      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| DIV 1 EDG INITIATION AND RHR LPCI "A" & LPCS INJECTION INTO THE RPV DUE TO   |
| AN INVALID SIGNAL                                                            |
|                                                                              |
| WITH THE PLANT IN OPERATIONAL CONDITION 5 IN A REFUELING OUTAGE, THE START   |
| OF THE DIVISION 1 EMERGENCY DIESEL GENERATOR (EDG) AND INJECTION INTO THE    |
| REACTOR PRESSURE VESSEL (RPV) VIA THE RESIDUAL HEAT REMOVAL (RHR) LOW        |
| PRESSURE COOLANT INJECTION (LPCI) "A" AND LOW PRESSURE CORE SPRAY (LPCS)     |
| SYSTEMS OCCURRED DUE TO AN INVALID EMERGENCY CORE COOLING SYSTEM INITIATION  |
| SIGNAL.                                                                      |
|                                                                              |
| THE CAUSE OF THE INITIATION SIGNAL WAS A FAILED ROSEMONT TRIP UNIT           |
| (#B21-N671A), WHICH WAS NEWLY INSTALLED AND PLACED INTO SERVICE DURING THE   |
| PRESENT REFUELING OUTAGE IN                                                  |
| RESPONSE TO THE SAFETY/RELIEF VALVE LOGIC SMART FIRE ISSUE.  WHEN THE TRIP   |
| UNIT FAILED, IT AFFECTED POWER TO THE DIVISION 1 INSTRUMENT RACK RESULTING   |
| IN THE GENERATION OF AN INVALID RPV LEVEL 1 INITIATION SIGNAL CAUSING THE    |
| ESF ACTUATIONS.  PLANT OPERATORS VERIFIED THE REACTOR CAVITY LEVEL AND       |
| IMMEDIATELY OVERRODE THE OPEN INJECTION VALVE SIGNAL TO STOP THE INJECTION.  |
| APPROXIMATELY TWO INCHES OF WATER HAD BEEN ADDED TO THE REACTOR CAVITY LEVEL |
| FROM THE SUPPRESSION POOL.  THE EDG  DID NOT LOAD AND WAS SECURED AFTER      |
| APPROXIMATELY TWO HOURS.                                                     |
|                                                                              |
| WHEN THE OPEN LPCS INJECTION VALVE SIGNAL WAS OVERRIDDEN, THE SYSTEM MINIMUM |
| FLOW VALVE DID NOT REOPEN AND CONTROL ROOM OPERATORS OPENED THE MINIMUM FLOW |
| VALVE TO PROVIDE LPCS PUMP PROTECTION.  ALSO, THE RHR "A" INJECTION CHECK    |
| VALVE WAS STILL INDICATING OPEN (UNCLEAR IF THIS IS AN INDICATION PROBLEM OR |
| A STUCK OPEN VALVE PROBLEM) AFTER THE INJECTION VALVE HAD BEEN SHUT.  THE    |
| LICENSEE IS INVESTIGATING BOTH OF THESE CONDITIONS.                          |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021