Event Notification Report for May 11, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/10/1999 - 05/11/1999 ** EVENT NUMBERS ** 35696 35697 35698 35699 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35696 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NEW YORK CITY DEPART OF HEALTH |NOTIFICATION DATE: 05/10/1999| |LICENSEE: BROWNING FERRIS INDUSTRIES |NOTIFICATION TIME: 11:47[EDT]| | CITY: NEW YORK REGION: 1 |EVENT DATE: 05/07/1999| | COUNTY: STATE: NY |EVENT TIME: 08:00[EDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 05/10/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CURTIS COWGILL R1 | | |FRED COMBS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: BORRI (NYC DPT OF HEALTH) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LANDFILL REJECTED HOSPITAL SOLID WASTE CONTAINING 300 MILLICURIES OF | | TECHNETIUM-99m | | | | BROWNING FERRIS INDUSTRIES (BFI) RECEIVED A LOAD OF SOLID WASTE FROM CITY | | HOSPITAL CENTER AT ELMHURST IN NEW YORK CITY AND TOOK IT TO THEIR TRANSFER | | STATION IN BROOKLYN, NY. THE WASTE WAS THEN MOVED TO A LANDFILL IN | | COMSTOCK, PA WHERE IT WAS REJECTED AND RETURNED TO THE BFI FACILITY IN | | BROOKLYN ON 05/07/99. THE WASTE CONTAINED APPROXIMATELY 300 MILLICURIES OF | | TECHNETIUM-99m. THE WASTE IS BEING RETURNED TO THE HOSPITAL. THE CITY IS | | INVESTIGATING THIS INCIDENT. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35697 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 05/10/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 15:18[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 05/10/1999| +------------------------------------------------+EVENT TIME: 13:00[EDT]| | NRC NOTIFIED BY: BELDEN |LAST UPDATE DATE: 05/10/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CURTIS COWGILL R1 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 VALVES FAILED THEIR LOCAL LEAK RATE TEST. | | | | UNDER THE APPENDIX J PROGRAM PLAN (#NMP1-APPJ-001) SECTION III/1.8 OUTAGE | | TESTING REQUIREMENTS INCLUDE MAINTAINING A COMBINED TOTAL TYPE 'B' AND 'C' | | AS-FOUND MINIMUM PATHWAY LEAKAGE. IN ACCORDANCE WITH TECH SPEC 6.16.4, THE | | COMBINED LOCAL LEAK RATE TEST (TYPE 'B' & 'C' TESTS INCLUDING AIRLOCKS) | | ACCEPTANCE CRITERIA IS LESS THAN 0.6 La, CALCULATED IN THE MINIMUM PATHWAY | | BASIS, AT ALL TIMES WHEN CONTAINMENT INTEGRITY IS REQUIRED. THE VALUE OF | | 0.6 La FOR UNIT 1 WAS CALCULATED TO BE 388.44 SCFH. THE RESULTS OF THE TEST | | MEASURED 388.756 SCFH, WHICH EXCEED THE CALCULATED VALUE FOR THE COMBINED | | AS-FOUND TYPE 'B' AND 'C' LOCAL LEAK RATE TESTS. THIS CONDITION WOULD HAVE | | BEEN A TECH SPEC VIOLATION IF IDENTIFIED DURING POWER OPERATION. | | | | THIS CONDITION WILL BE CORRECTED PRIOR TO PLANT RESTART. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35698 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 05/10/1999| | UNIT: [2] [3] [] STATE: PA |NOTIFICATION TIME: 19:51[EDT]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 05/10/1999| +------------------------------------------------+EVENT TIME: 09:30[EDT]| | NRC NOTIFIED BY: KOVALCHICK |LAST UPDATE DATE: 05/10/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CURTIS COWGILL R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TRACES OF A CONTROLLED SUBSTANCE FOUND IN A BATHROOM INSIDE THE PROTECTED | | AREA | | | | ON 04/15/99, THREE SUSPECTED ITEMS WERE FOUND IN A BATHROOM INSIDE THE PLANT | | PROTECTED AREA AND WERE TURNED OVER TO PECO ENERGY CORPORATE SECURITY. AT | | 0930 ON 05/10/99, THE LICENSEE RECEIVED A REPORT FROM AN INDEPENDENT | | LABORATORY THAT INDICATED THAT, ALTHOUGH THERE WAS NO VISIBLE RESIDUE | | PRESENT, A GAS CHROMATOGRAPHY/MASS SPECTROMETRY DETECTED AND CONFIRMED THE | | PRESENCE OF A CONTROLLED SUBSTANCE. AT THE PRESENT TIME, THE SUSPECTED | | ITEMS HAVE NOT BEEN ASSOCIATED WITH ANY SPECIFIC INDIVIDUAL. THE LICENSEE | | IS CONTINUING TO INVESTIGATE THIS SITUATION. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35699 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 05/10/1999| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 21:34[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 05/10/1999| +------------------------------------------------+EVENT TIME: 16:58[CDT]| | NRC NOTIFIED BY: CARLSON |LAST UPDATE DATE: 05/10/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DIV 1 EDG INITIATION AND RHR LPCI "A" & LPCS INJECTION INTO THE RPV DUE TO | | AN INVALID SIGNAL | | | | WITH THE PLANT IN OPERATIONAL CONDITION 5 IN A REFUELING OUTAGE, THE START | | OF THE DIVISION 1 EMERGENCY DIESEL GENERATOR (EDG) AND INJECTION INTO THE | | REACTOR PRESSURE VESSEL (RPV) VIA THE RESIDUAL HEAT REMOVAL (RHR) LOW | | PRESSURE COOLANT INJECTION (LPCI) "A" AND LOW PRESSURE CORE SPRAY (LPCS) | | SYSTEMS OCCURRED DUE TO AN INVALID EMERGENCY CORE COOLING SYSTEM INITIATION | | SIGNAL. | | | | THE CAUSE OF THE INITIATION SIGNAL WAS A FAILED ROSEMONT TRIP UNIT | | (#B21-N671A), WHICH WAS NEWLY INSTALLED AND PLACED INTO SERVICE DURING THE | | PRESENT REFUELING OUTAGE IN | | RESPONSE TO THE SAFETY/RELIEF VALVE LOGIC SMART FIRE ISSUE. WHEN THE TRIP | | UNIT FAILED, IT AFFECTED POWER TO THE DIVISION 1 INSTRUMENT RACK RESULTING | | IN THE GENERATION OF AN INVALID RPV LEVEL 1 INITIATION SIGNAL CAUSING THE | | ESF ACTUATIONS. PLANT OPERATORS VERIFIED THE REACTOR CAVITY LEVEL AND | | IMMEDIATELY OVERRODE THE OPEN INJECTION VALVE SIGNAL TO STOP THE INJECTION. | | APPROXIMATELY TWO INCHES OF WATER HAD BEEN ADDED TO THE REACTOR CAVITY LEVEL | | FROM THE SUPPRESSION POOL. THE EDG DID NOT LOAD AND WAS SECURED AFTER | | APPROXIMATELY TWO HOURS. | | | | WHEN THE OPEN LPCS INJECTION VALVE SIGNAL WAS OVERRIDDEN, THE SYSTEM MINIMUM | | FLOW VALVE DID NOT REOPEN AND CONTROL ROOM OPERATORS OPENED THE MINIMUM FLOW | | VALVE TO PROVIDE LPCS PUMP PROTECTION. ALSO, THE RHR "A" INJECTION CHECK | | VALVE WAS STILL INDICATING OPEN (UNCLEAR IF THIS IS AN INDICATION PROBLEM OR | | A STUCK OPEN VALVE PROBLEM) AFTER THE INJECTION VALVE HAD BEEN SHUT. THE | | LICENSEE IS INVESTIGATING BOTH OF THESE CONDITIONS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+
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