Event Notification Report for May 5, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/04/1999 - 05/05/1999 ** EVENT NUMBERS ** 35668 35669 35670 35671 35672 35673 35674 35675 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35668 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 05/04/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 00:09[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 05/03/1999| +------------------------------------------------+EVENT TIME: 23:30[EDT]| | NRC NOTIFIED BY: DOUGLAS J. GOMEZ |LAST UPDATE DATE: 05/04/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES LINVILLE R1 | |10 CFR SECTION: |CECIL THOMAS NRR | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS |CHARLES MILLER IRO | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 90 Power Operation |85 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECHNICAL SPECIFICATION SHUTDOWN DUE TO THREE OUT OF FOUR OVERTEMPERATURE | | DELTA TEMPERATURE AND OVERPOWER DELTA POWER CHANNELS BEING DECLARED | | INOPERABLE | | | | During calibrations of Protection Channels, it was determined that three out | | of four Overtemperature and Overpower Delta Channels were inoperable | | requiring entry into Technical Specification 3.0.3 requiring Mode 3 (Hot | | Standby) within 6 hours (0530 EDT on 05/04/99). | | | | The summer coming out of the Delta Temperature Channels is superimposing an | | AC ripple on top of the DC output, and depending on whether it is feeding | | out through an NUS bistable or Foxboro bistable, the Foxboro bistable | | apparently allows the AC ripple to continue through and cause the Delta | | Temperature Setpoints to be non-conservative. The licensee did not know | | when a surveillance test had last been performed on the channels. | | | | All Emergency Core Cooling Systems and the Emergency Diesel Generators are | | fully operable. The electrical grid is stable. | | | | The NRC Resident Inspector will be notified by the licensee. | | | | **** Update on 05/04/99 at 0442 EDT from Dan Berry taken by MacKinnon **** | | | | The licensee exited Technical Specification 3.0.3 at 0437 EDT when three | | Channels were declared operable and the fourth channel was defeated | | (bistables were tripped). Reactor power level was reduced to 21% before | | Technical Specification 3.0.3 was exited. The licensee plans to increase | | reactor power level to between 30 to 35%, at which point, the licensee plans | | to stabilize reactor power level and repair a steam leak on MSR "2B." | | | | The NRC Resident Inspector will be notified by the licensee. The R1DO (Jim | | Linville) was notified by the NRC Operations Officer. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35669 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 05/04/1999| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 10:17[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/04/1999| +------------------------------------------------+EVENT TIME: 09:30[EDT]| | NRC NOTIFIED BY: GRADY PICKLER |LAST UPDATE DATE: 05/04/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |AUNA 50.72(b)(1)(ii)(A) UNANALYZED COND OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MECHANICAL PROBLEMS ASSOCIATED WITH MANUAL STEAM GENERATOR PORV OPERATION | | WERE DISCOVERED AND CORRECTED. | | | | On March 14, 1999, McGuire Nuclear Station identified mechanical problems | | with one Unit 2 Steam Generator Power-Operated Relief Valve (PORV). A | | similar problem was identified with another Unit 2 Steam Generator PORV on | | March 20, 1999. On May 3, 1999, it was determined that, as a result of the | | observed mechanical problems, both of the affected Unit 2 Steam Generator | | PORVs were inoperable for a period of time greater than allowed by McGuire | | Technical Specification 3.7.4. This condition affected the ability of the | | PORVs to operate in manual. Manual operation of the PORVs is credited in | | mitigation of design basis accidents. Consequently, on May 4, 1999, at 0930 | | hours it was determined that this issue was reportable as a 1-hour | | Unanalyzed Condition event. | | | | The mechanical problem discussed above is that a pin is used to connect the | | handwheel to the shaft that operates a Steam Generator PORV valve. It was | | found that the pin for operation of two of the Steam Generator PORV valves | | was inserted into the handwheel, but the pin was not inserted far enough to | | go into the shaft. Therefore, the handwheel would have turned, but the | | shaft going to the PORV would not have turned. The licensee has corrected | | this problem, and an investigation of Unit 1 did not find this type of | | problem. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35670 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 05/04/1999| | UNIT: [] [2] [] STATE: SC |NOTIFICATION TIME: 13:53[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/04/1999| +------------------------------------------------+EVENT TIME: 12:55[EDT]| | NRC NOTIFIED BY: BILL RUDY |LAST UPDATE DATE: 05/04/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHRIS CHRISTENSEN R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 8 Power Operation |8 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUXILIARY FEEDWATER DECLARED INOPERABLE | | | | All Auxiliary Feedwater (AFW) Pumps have been declared inoperable, including | | the #2A and #2B motor-driven and the #2 turbine-driven AFW Pumps. | | | | "The suction piping to the [AFW] System from the Nuclear Service Water | | System was discovered to have excessive fouling that resulted in the AFW | | system being outside its design basis. Engineering analysis determined that | | under certain accident scenarios involving AFW system runout flow, there is | | inadequate suction pressure to assure AFW pump operability. The | | turbine-driven AFW pump has been isolated as an interim | | compensatory measure. This action reduces the system runout flow which | | should increase the suction pressure to the two remaining motor-driven AFW | | pumps sufficiently to assure pump operability. Engineering analysis is in | | progress to verify the adequacy of this action. The affected piping will be | | cleaned which will ultimately correct the problem." | | | | Unit 2 will remain at its present power level until the engineering analysis | | is complete and corrective actions are determined to be adequate. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35671 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 05/04/1999| |LICENSEE: UNIVERSITY COMMUNITY HOSPITAL |NOTIFICATION TIME: 17:14[EDT]| | CITY: TAMPA REGION: 2 |EVENT DATE: 05/03/1999| | COUNTY: STATE: FL |EVENT TIME: 12:00[EDT]| |LICENSE#: 0549-1 AGREEMENT: Y |LAST UPDATE DATE: 05/04/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |CHRIS CHRISTENSEN R2 | | |JOHN GREEVES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHARLES ADAMS | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - RADIATION THERAPY SEEDS BURNED | | | | "475 Pd-103 seeds arrived at the licensee's receiving department on Friday, | | 30 April 99. The package was taken to the radiation therapy section, and | | the technician says he advised the physicist that the package was in the | | hall outside the door. The physicist says that he doesn't remember being so | | advised. Later that day, a janitor stated that she picked up what she | | assumed was a empty box and placed it in the trash. The package was taken | | to the county waste facility and incinerated. The package was consumed in | | the 2,000�F heat, but since palladium does not vaporize until 2,800�F, it | | should have remained as ash. That small amount of ash diluted in huge | | bunches of ash was not detected by the waste stream monitor. A state survey | | of the waste energy facility did not detect any activity. The package was | | noted missing on 3 May 99, and this office [State of Florida Bureau of | | Radiation Control] was so advised. Further action is referred to Material | | Licensing." | | | | The seeds constituted 666 mCi as of 1200 on 4 May 99. | | | | (Call the NRC operations officer for a contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35672 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 05/04/1999| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 17:35[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 05/04/1999| +------------------------------------------------+EVENT TIME: 16:45[EDT]| | NRC NOTIFIED BY: ERIC OLSON |LAST UPDATE DATE: 05/04/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES LINVILLE R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 80 Power Operation |80 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI AND RCIC DIFFERENCES FOUND BETWEEN DESIGN BASIS AND TECHNICAL | | SPECIFICATIONS. | | | | "During license design-basis reconstitution efforts it was discovered that | | the specific values in the PNPS TS for HPCI and RCIC operability testing are | | not in accordance with the plant design. In accordance with the TS, the | | HPCI System is tested to ensure the HPCI pump can deliver at least 4,250 gpm | | for a system head corresponding to a reactor pressure of 1,000 to 150 psig. | | The RCIC test requirement is that RCIC shall deliver at least 400 gpm for a | | system head corresponding to a reactor pressure of 1,000 to 150 psig. The | | applicable Tech Spec Sections are 3.5.C for HPCI and 3.5.D for RCIC. | | | | "The design requirement of HPCI and RCIC is to achieve 4,250 gpm and 400 | | gpm, respectively, for a reactor pressure corresponding to the Safety Relief | | Valve (SRV) setpoint. Currently, the SRV upper setpoint limit is 1,115 | | +/-11 psig. Therefore, the corresponding discharge pressure of the pumps | | shall be that required to achieve the required flow rate at the given | | reactor vessel pressure (1,126 psig) taking into account system head loss, | | elevation changes, lowering level in the CST or suction taken from the torus | | and instrument setpoint error. For both HPCI and RCIC, this pressure should | | be approximately 1,243 psig (slightly less for RCIC due to lower head loss | | from the lower flow criteria). | | | | "Both the HPCI and RCIC systems are considered operable per Operability | | Evaluation #99-024 and #99-025. This is a verbal evaluation based on | | engineering judgement that there is sufficient horsepower available to | | achieve the design parameters of both systems and that, [during] past | | testing, the actual values have, in fact, been achieved. However, the | | systems have not been tested to the design values on a periodic (quarterly) | | test basis. During a normal surveillance test of HPCI on 03/13/98, the HPCI | | discharge pressure was 1,260 psig. During startup testing, the RCIC system | | was tested to 1,280 psig discharge pressure." | | | | The licensee plans to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35673 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 05/04/1999| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 18:19[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/04/1999| +------------------------------------------------+EVENT TIME: 15:00[EDT]| | NRC NOTIFIED BY: DONALD KOSLOFF |LAST UPDATE DATE: 05/04/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SI THROTTLE VALVES CAVITATION DURING LOCA COULD LEAD TO FAILURE OF SI | | PUMPS. | | | | "On March 27, 1999, engineering personnel investigating NRC Information | | Notice 97-76 concluded that a preliminary flow analysis indicated that six | | Unit 1 safety injection (SI) throttle valves could experience cavitation | | during a LOCA. As a result of that conclusion, SI throttle valve #1-SI-121S | | was radiographed to determine its position. On April 8, 1999, a review of | | the radiograph indicated that the valve was about 43 percent open. The | | radiograph also showed indications of possible erosion of the valve that | | could have been caused by cavitation. Valve cavitation during a LOCA could | | cause the valves to allow excessive flow, leading to SI pump runout and | | subsequent failure of the SI pumps. Valve #1-SI-141L1 was also radiographed | | and determined to be 27 percent open. | | | | "A fax from the valve vendor indicated that SI throttle valves that were | | less than 32 percent open may not be capable of allowing passage of sump | | debris of the expected maximum size, 0.25 inch diameter. Several of the | | valves may be less than 32 percent open. This condition could restrict SI | | flow to the reactor coolant system during a LOCA. | | | | "On May 4, 1999, during continuing evaluation of the above conditions, plant | | personnel determined that the conditions were reportable. Both conditions | | may also exist in Unit 2. Both Units are currently in Mode 5. Evaluation | | of these conditions, including determination of the need for physical | | modification, is ongoing, and the conditions will be resolved prior to | | startup of the units." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35674 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/04/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 23:52[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/04/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 13:50[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/04/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MONTE PHILLIPS R3 | | DOCKET: 0707002 |JOHN GREEVES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KURT SISLER | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VALID SAFETY SYSTEM ACTUATION OF AN OVERHEAD CRANE HOIST BRAKE RESULTING IN | | A FULL, 10-TON, UF6 CYLINDER BEING SUSPENDED ABOVE THE AUTOCLAVE ROLLERS IN | | THE X-343 BUILDING | | | | The following text is a portion of a facsimile received from Portsmouth: | | | | "On May 04, 1999, at 1350 hours, during removal of a full, 10-ton, UF6 | | cylinder from autoclave #5, the hoist on the North overhead crane stopped | | due to an actuation of the hoist brake caused by a power failure. The hoist | | brake did perform its design function upon this loss of power. This power | | failure resulted in the cylinder being suspended approximately 1 foot above | | the autoclave rollers. Procedure XP2-TE-TE5030 steps were implemented, and | | after the power breaker was reset, the cylinder was lowered within the | | confines of the autoclave, and the North crane was declared inoperable." | | | | "This event is being categorized and reported as a valid actuation of a 'Q' | | Safety System in accordance with Safety Analysis Report, Section 8.9 | | (24-hour report)." | | | | "There was no loss of hazardous/radioactive material or | | radioactive/radiological contamination exposure as a result of this event." | | | | Portsmouth personnel notified the NRC resident inspector and the Department | | of Energy site representative. (Call the NRC operations officer for a site | | contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35675 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 05/05/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 04:38[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 05/05/1999| +------------------------------------------------+EVENT TIME: 02:00[EDT]| | NRC NOTIFIED BY: GREG SOSSON |LAST UPDATE DATE: 05/05/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES LINVILLE R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ISOLATION OF THE 'B' LOOP DRYWELL CHILLED WATER INBOARD SUPPLY AND RETURN | | VALVES DURING PERFORMANCE OF A SPECIAL PROCEDURE TO DEENERGIZE A SAFEGUARDS | | BUS | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 05/05/99 at 0200 hours, it was discovered that an [engineered safety | | feature] actuation occurred on the Unit 2 Drywell Chilled Water (DWCW) | | system. This isolation occurred at approximately 2300 on 05/02/99 during | | performance of a special procedure to deenergize the D22 safeguards bus." | | | | "With Unit 2 in OPCON 5, the 'B' loop DWCW inboard supply and return valves | | HV--087-222 and HV-087-223 isolated when the power supply to an interposing | | relay was deenergized per a special procedure on 05/02/99. This special | | procedure did not properly address the valve closure. During this special | | procedure, power was later removed from both valves. This removed control | | room indication of their position, and their closure was not immediately | | detected. Later, station personnel observed increasing drywell | | temperatures. The follow-up investigation revealed the isolation valves were | | closed by local verification." | | | | "Additional investigation found several containment atmosphere sample valves | | and primary containment instrument gas [primary containment isolation | | valves] that also closed during the loss of power. These conditions were | | also expected but not properly documented in the special procedure." | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021