Event Notification Report for April 29, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/28/1999 - 04/29/1999 ** EVENT NUMBERS ** 35645 35646 35647 35648 35649 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35645 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 04/28/1999| | UNIT: [1] [] [] STATE: VT |NOTIFICATION TIME: 11:21[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 04/28/1999| +------------------------------------------------+EVENT TIME: 07:30[EDT]| | NRC NOTIFIED BY: DENNIS MAY |LAST UPDATE DATE: 04/28/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CLIFFORD ANDERSON R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI SYSTEM INOPERABLE | | | | During an I&C surveillance test of pressure switches associated with the | | High Pressure Coolant Injection (HPCI) steam line, one of four low steam | | line pressure switches failed its test. The licensee closed both HPCI steam | | isolation valves rendering HPCI inoperable. The licensee has verified the | | operability of the Automatic Depressurization System (ADS) as required by | | plant Technical Specifications. | | | | The NRC resident inspector has been informed of this notification by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35646 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ALLIED-SIGNAL INC. |NOTIFICATION DATE: 04/28/1999| | RXTYPE: URANIUM HEXAFLUORIDE PRODUCTION |NOTIFICATION TIME: 12:20[EDT]| | COMMENTS: UF6 CONVERSION (DRY PROCESS) |EVENT DATE: 04/28/1999| | |EVENT TIME: 10:30[CDT]| | |LAST UPDATE DATE: 04/28/1999| | CITY: METROPOLIS REGION: 3 +-----------------------------+ | COUNTY: MASSAC STATE: IL |PERSON ORGANIZATION | |LICENSE#: SUB-526 AGREEMENT: Y |JOHN MADERA R3 | | DOCKET: 04003392 |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HUGH ROBERTS | | | HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF AN EMERGENCY SYSTEM WITH NO REDUNDANT EQUIPMENT AVAILABLE FOR | | BACKUP - 24-HOUR REPORT IN ACCORDANCE WITH 10CFR40.60(b) | | | | The failure involves a health physics vacuum pump and a communication device | | (the red lights for notification of respiratory conditions). Power is not | | available to these devices. The licensee cannot switch to standby power due | | to a common bus outage. The licensee was in the process of putting another | | scrubber onto this system as part of an annual shutdown. The power feed | | coming in from the local company (CIPS) went down, and the standby system | | was not available due to ongoing work. The power outage occurred at 1003 | | CDT, and it lasted for 2 minutes and 10 seconds. The licensee determined | | that the health physic pump and red lights were inoperable at 1030 CDT. | | | | Prior to this event, the fluorination and distillation portions of this UF6 | | conversion facility were down, and the licensee was operating the uranium | | tetra-fluoride (UF4) portion of the facility. The licensee shut this | | portion of the facility down a few minutes ago because there was no standby | | power to the area due to a common bus outage. | | | | The licensee plans to inform the NRC Region 3 office and three NRC | | inspectors that are currently located on site. (Call the NRC operations | | officer for a licensee contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35647 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 04/28/1999| | UNIT: [1] [2] [] STATE: MI |NOTIFICATION TIME: 15:57[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/28/1999| +------------------------------------------------+EVENT TIME: 15:00[EDT]| | NRC NOTIFIED BY: BRIAN MUTZ |LAST UPDATE DATE: 04/28/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN MADERA R3 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF A SAFEGUARDS SYSTEM DEGRADATION RELATED TO THE PROTECTED AREA | | (1-HOUR REPORT) | | | | Security personnel discovered a safeguard system degradation related to the | | protected area. Immediate compensatory actions were taken upon discovery. | | (Contact the NRC operations officer for additional details.) | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35648 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 04/29/1999| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 00:45[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 04/28/1999| +------------------------------------------------+EVENT TIME: 18:00[EDT]| | NRC NOTIFIED BY: BRUCE BUTLER |LAST UPDATE DATE: 04/29/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 16 Power Operation |16 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - HPCI SYSTEM INOPERABLE DUE TO TRIPPED BAROMETRIC CONDENSER VACUUM PUMP | | BREAKER - | | | | AT 1800 ON 04/28/99, WITH UNIT 1 AT 16% POWER, THE HIGH PRESSURE COOLANT | | INJECTION (HPCI) SYSTEM BAROMETRIC CONDENSER VACUUM PUMP TRIPPED DURING A | | TECH SPEC SURVEILLANCE TEST. PLANT OPERATORS WERE UNABLE TO RESET THE | | VACUUM PUMP CIRCUIT BREAKER AND SHUT THE HPCI SYSTEM DOWN AND DECLARED THE | | IT INOPERABLE. MAINTENANCE ELECTRICIANS RESET THE VACUUM PUMP CIRCUIT | | BREAKER THERMAL OVERLOADS RESTORING POWER TO THE VACUUM PUMP. MAINTENANCE | | ELECTRICIANS REPLACED THE HPCI SYSTEM VACUUM PUMP CONTROL SWITCH BECAUSE THE | | SWITCH HAS RECENTLY EXPERIENCED PROBLEMS NOT RETURNING TO ITS MID POSITION, | | AS DESIGNED. THE LICENSEE IS CONTINUING TO INVESTIGATE THE CAUSE OF THE | | VACUUM PUMP TRIP. | | | | TECH SPEC LCO ACTION STATEMENT 3.5.1 REQUIRES THE LICENSEE TO VERIFY THE | | OPERABILITY OF THE REACTOR CORE ISOLATION COOLING (RCIC) SYSTEM AND RESTORE | | THE HPCI SYSTEM TO OPERABLE STATUS WITHIN 14 DAYS OR SHUT UNIT 1 DOWN. AT | | 1925, THE LICENSEE VERIFIED THE OPERABILITY OF THE RCIC SYSTEM. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35649 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 04/29/1999| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 02:06[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 04/28/1999| +------------------------------------------------+EVENT TIME: 21:51[CDT]| | NRC NOTIFIED BY: RUSS GODWIN |LAST UPDATE DATE: 04/29/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID GRAVES R4 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Fuel Building inoperable due to loss of vacuum in Fuel Building due to an | | open Fuel Building/Annulus door - | | | | At 2151 CDT on 04/28/99, with the plant in Operational Condition 5 in a | | refueling outage, the Fuel Building was determined to be inoperable. At the | | time, fuel inspection activities were in progress in the Fuel Building. | | | | The Fuel Building was rendered inoperable when a Fuel Building/Annulus door | | was opened. The door was opened to allow entry of personnel for completion | | of required testing of lighting circuits. The control room staff was alerted | | to this condition when the "Fuel Building Pressure High" alarm was received. | | Upon receipt of the alarm, the Control Room Supervisor directed that fuel | | handling activities be suspended. Fuel handling activities were immediately | | suspended and not resumed until the door was closed to reestablish Fuel | | Building integrity. | | | | The fuel inspection activities in progress consisted of removing single fuel | | pins from an irradiated bundle. The irradiated bundle was located in the | | fuel preparation machine. | | | | The Fuel Building/Annulus door was required to be closed to maintain the | | leak tightness of the Fuel Building. Plant staff personnel are continuing to | | evaluate this event. However, as a result of the open door, the Fuel | | Building may not have been able to perform its design function. | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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