Event Notification Report for April 26, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/23/1999 - 04/26/1999 ** EVENT NUMBERS ** 35600 35612 35622 35623 35624 35625 35627 35628 35629 35630 35631 35632 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35600 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 04/17/1999| | UNIT: [] [] [3] STATE: IL |NOTIFICATION TIME: 11:58[EDT]| | RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 04/17/1999| +------------------------------------------------+EVENT TIME: 09:59[CDT]| | NRC NOTIFIED BY: DAVE SLAGER |LAST UPDATE DATE: 04/23/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN JACOBSON R3 | |10 CFR SECTION: | | |ADEG 50.72(b)(1)(ii) DEGRAD COND DURING OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 99 Power Operation |99 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF A PRIMARY CONTAINMENT AIR SAMPLE RETURN ISOLATION VALVE TO MEET | | MAXIMUM INSERVICE TEST STROKE-TIME REQUIREMENTS | | | | While performing quarterly valve stroke-time testing on Unit 3, a primary | | containment air sample return isolation valve exceeded its specified maximum | | stroke-time limit. The sample return line was isolated in accordance with | | Technical Specification 3.7.D for primary containment isolation valves, and | | this action satisfied the 4-hour limiting condition for operation action | | statement requirements. The second in-line primary containment isolation | | system valve remains operable. | | | | The licensee stated that no other valves failed to meet the maximum | | stroke-time limits. The licensee also stated that, during a test that was | | performed last month, the valve in question was identified as being in the | | 'Alert' time range for inservice test timing requirements and that it was | | being tested per the required increased testing frequency. Corrective | | actions are being initiated, and troubleshooting activities are in | | progress. | | | | The licensee plans to notify the NRC resident inspector. | | | | *** UPDATE ON 04/23/99 AT 0443 FROM GADBOIS TO GOULD *** RETRACTION | | | | UPON FURTHER REVIEW, IT WAS DETERMINED THAT THIS EVENT DID NOT CONSTITUTE A | | REPORTABLE CONDITION SINCE THE PENETRATION HAD AN OPERABLE REDUNDANT VALVE | | WHICH COULD HAVE ISOLATED THE CONTAINMENT PENETRATION. THEREFORE, THE | | LICENSEE IS RETRACTING THIS EVENT NOTIFICATION. | | | | THE LICENSEE PLANS TO NOTIFY THE NRC RESIDENT INSPECTOR. THE R3DO (LEACH) | | WAS NOTIFIED BY THE NRC OPERATIONS OFFICER. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35612 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MA DEPT OF PUBLIC HEALTH RCP |NOTIFICATION DATE: 04/21/1999| |LICENSEE: AEA TECHNOLOGIES QSA, INC |NOTIFICATION TIME: 15:00[EDT]| | CITY: BURLINGTON REGION: 1 |EVENT DATE: 04/21/1999| | COUNTY: STATE: MA |EVENT TIME: 14:00[EDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 04/23/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MOHAMED SHANBAKY R1 | | |FREDERICK COMBS NMSS | +------------------------------------------------+JOSEPH GIITTER IRO | | NRC NOTIFIED BY: KEN TRAEGDE |DONNA MARIE PEREZ IP | | HQ OPS OFFICER: DICK JOLLIFFE |LEN WERT R2 | +------------------------------------------------+DALE POWERS R4 | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |NOCM COMM ASST BRIEF | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - SHIPMENT OF 8 Ir-192 SOURCES (866 CURIES TOTAL) FROM BURLINGTON, MA, | | OVERDUE IN MEXICO - | | | | AT 1500 EDT ON 04/21/99, KEN TRAEGDE OF THE MA DEPARTMENT OF PUBLIC HEALTH | | RADIATION CONTROL PROGRAM (RCP) LOCATED IN BOSTON, MA, REPORTED THAT ON | | 04/16/99, AEA TECHNOLOGY QSA, INC., LOCATED IN BURLINGTON, MA, SHIPPED A | | MODEL #855 SOURCE CHANGER LOADED WITH 8 Ir-192 SOURCES (TOTALING 866 CURIES) | | VIA FEDERAL EXPRESS TO VICONT S.A. DE C.V. LOCATED IN TOLUCA, MEXICO. THE | | UNDAMAGED PACKAGE HAD A TRANSPORT INDEX OF 1.4 (NORMAL READINGS OF 1.4 mR/HR | | AT 1 METER AND 55 mR/HR AT THE SURFACE) AT THE TIME OF SHIPMENT. | | | | THE SHIPMENT WAS SCHEDULED TO ARRIVE IN MEXICO ON 04/17/99. AS OF 1400 EDT | | ON 04/21/99, THE RECIPIENT (VICONT S.A. DE C.V.) HAD RECEIVED THE SHIPPING | | PAPERS BUT NOT THE CONTAINER. THE SHIPPER AND FEDERAL EXPRESS HAVE LAUNCHED | | A FULL SEARCH FOR THE PACKAGE. THE FEDERAL EXPRESS HAZARDS MATERIAL | | INVESTIGATION TEAM HAS CONDUCTED A PHYSICAL SEARCH OF EXPRESS DEPOTS IN | | BOSTON, MEMPHIS, LOS ANGELES, AND MEXICO. | | | | THE LICENSE NUMBERS ARE: SU-1485, 12-8361, 52-0243, 54-0237, AND 58-0242. | | | | THE NRC OPERATIONS OFFICER NOTIFIED THE DOT NATIONAL RESPONSE CENTER | | (GAUTHIER); REPORT NUMBER 481132. | | | | (CONTACT THE NRC OPERATIONS OFFICER FOR APPLICABLE TELEPHONE NUMBERS.) | | | | *********************************** UPDATE AT 1345 ON 04/22/99 BY JONES | | *********************************** | | | | The NRC entered the Monitoring Phase of Normal Mode at 1345 on 04/22/99. | | The NRC operations officer notified, the R1DO (Shanbaky), Region 1 (Miller), | | IRO (Congel and Giitter), NMSS (Paperiello), RCT (Weinstein), PAO (Gagner), | | EDO's office (Charleen Raddatz), and Chairman's office (Holian). The RCT | | notified FEMA (Dan Rishe), DOE (Thomas Yates), EPA (Ms. Reddy), USDA (Bob | | Conley), HHS/CDC (James Raab), and DOT (Rick Boyle). | | | | *********************************** UPDATE AT 1600 ON 04/22/99 BY JONES | | *********************************** | | | | A Commissioner's Assistants Briefing was conducted at 1600 on 04/22/99. The | | following notifications were made (* office did not participate): IRO (Joe | | Giitter and Eric Weinstein), Chairman Jackson (Dan Gillen), Commissioner | | Dicus (Joel Lubenau), Commissioner Diaz (Patrick Castleman), Commissioner | | McGaffigan (Janet Schlueter), Commissioner Merrifield (JohnThoma), EDO (*), | | DEDE (*), NMSS (Don Cool and Carl Paperiello), NMSS EO (Fred Combs), R1DO | | (Mohamed Shanbaky), PAO (Joe Gilland), CAO (Thomas Madden), SECY (Andrew | | Bates), SP (Paul Lohaus), IP (Ron Hauber), Region 1 (Felicia Hinson and Jim | | Wiggins, etc), and Region 2 (Doug Collins, Chuck Hosey, and Dick Woodruff). | | The briefer was Fred Combs of NMSS. | | | | At 1610, the NRC operations officer played a tape of briefing for EDO (Dan | | Martin) and DEDE (Jocelyn Mitchell). | | | | ****************************** UPDATE AT 1230 ON 04/23/99 BY TROCINE AND | | JONES ****************************** | | | | A conference call was conducted at 1230 on 04/23/99 to update the status of | | this event. The following NRC offices participated (among others): IRO | | (Himes), NMSS (Brach, Combs, and Cook), Region 1 (Loyd), Region 2 (Collins | | and Woodruff), Region 4 (Andrews), PAO (Hayden), IP (Lieberman), SP | | (Lohaus), and EDO (Raddatz). In addition, the following agencies | | participated: Department of Transportation (Rick Boyle), Massachusetts | | Department of Public Health RCP (Ken Traegdy), Federal Express (Scott Mugno, | | Pat Oppenheimer, and Roy Parker), State of Tennessee (Alan Grewe), Tennessee | | Division of Radiation Health (Eddy Nanney), AEA Technologies QSA, Inc. (Eric | | Okvist), and Environmental Protection Agency located in Atlanta (Paul | | Wagner). | | | | During this conference call, representatives of Federal Express reported | | that they are confident that the shipment of 8 Ir-192 sources left Boston. | | They issued an 'all-points' search order, faxed a description to all | | 'logical' locations, and conducted repeat physical searches in Memphis, | | Boston, and Mexico, all without locating the shipment to date. (The Los | | Angeles depot was not searched as had been reported on 04/21/99.) | | Massachusetts and Tennessee health authorities conducted radiological | | surveys in Boston and Memphis on 04/22/99 with negative results. | | | | Rick Boyle of the Department of Transportation notified the competent | | authority in Mexico, and Federal Express requested a detailed search of the | | Customs facilities in Mexico City. | | | | The next conference call is scheduled for 1230 EDT on Wednesday, 04/28/99. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35622 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 04/23/1999| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 04:33[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 04/23/1999| +------------------------------------------------+EVENT TIME: 02:14[CDT]| | NRC NOTIFIED BY: WELLER |LAST UPDATE DATE: 04/23/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HPCI SYSTEM DECLARED INOPERABLE, AND PLANT ENTERED LCO ACTION STATEMENT. | | | | THE HPCI SYSTEM WAS DECLARED INOPERABLE FROM 0214 CDT TO 0220 CDT DUE TO | | MOISTURE IN THE TURBINE STEAM INLET LINE. A 14-DAY LCO ACTION STATEMENT WAS | | ENTERED, AND RCIC WAS VERIFIED OPERABLE. HPCI TURBINE INLET HIGH DRAIN POT | | LEVEL ANNUNCIATION WAS RECEIVED DUE TO STROKING MO-2036 (TURBINE STEAM | | SUPPLY VALVE) AS PART OF THE REACTOR SHUTDOWN PROCEDURE AT REACTOR PRESSURE | | OF 500 PSIG. THE STEAM LINE MANUAL DRAIN VALVE WAS OPENED, AND THE | | ANNUNCIATOR CLEARED AT 0220 CDT. HPCI WAS DECLARED OPERABLE AND IN STANDBY. | | THE 14-DAY LCO ACTION STATEMENT WAS ALSO EXITED AT 0220 CDT. | | | | THE NRC RESIDENT INSPECTOR WILL BE NOTIFIED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35623 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 04/23/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 10:16[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 04/23/1999| +------------------------------------------------+EVENT TIME: 07:53[EDT]| | NRC NOTIFIED BY: GILLOW |LAST UPDATE DATE: 04/23/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 35 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD A REACTOR TRIP FROM 35% POWER ON A 2-OUT-OF-4 POWER RANGE HIGH | | SIGNAL. | | | | THE REACTOR TRIP OCCURRED WHILE THE PLANT WAS COMING OUT OF A REFUELING | | OUTAGE AND THE I&C TECHNICIANS WERE WORKING ON THE NUCLEAR INSTRUMENTATION | | RACKS ADJUSTING POWER RANGE TRIP SETPOINTS. CHANNEL 1 HAD JUST BEEN | | COMPLETED, AND CHANNEL 2 WAS IN PROGRESS WITH BOTH BISTABLES TRIPPED IN THE | | CHANNEL 2 PROTECTION RACKS. AT THIS POINT, CONTROL ROOM TURNOVER HAD | | STARTED, AND THE TECHNICIANS HAD STOPPED WORK UNTIL TURNOVER WAS COMPLETE. | | UPON RESUMING WORK, THE TECHNICIANS INADVERTENTLY WENT TO NIS CHANNEL 3 AND | | PULLED INSTRUMENT POWER FUSES. THE REACTOR TRIPPED ON 2 OUT OF 4 POWER | | RANGE HI LEVEL IMMEDIATELY UPON PULLING THE CHANNEL 3 FUSES. ALL RODS FULLY | | INSERTED, NO ECCS OCCURRED, AND NO SAFETY RELIEF VALVES LIFTED. THE PLANT | | IS USING THE ATMOSPHERIC RELIEF VALVES AS THE HEAT SINK. THE PLANT IS | | CURRENTLY IN MODE 3, Tavg IS 547�F, AND RCS PRESSURE AT 2,235 PSIG. | | | | SINCE THE LICENSEE WAS COMING OUT OF A REFUELING OUTAGE, THE MAIN STEAM | | ISOLATION VALVES WERE CLOSED DUE TO LOW DECAY HEAT, AND THE MAIN STEAM | | GENERATOR ATMOSPHERIC VALVE ON EACH STEAM GENERATOR WAS USED TO MAINTAIN | | Tavg. | | | | THE INCIDENT WAS DUE TO PERSONNEL ERROR. | | | | THE NRC RESIDENT INSPECTOR WAS INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35624 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NATIONAL INSTITUTE OF HEALTH |NOTIFICATION DATE: 04/23/1999| |LICENSEE: NATIONAL INSTITUTE OF HEALTH |NOTIFICATION TIME: 13:38[EDT]| | CITY: BETHERSDA REGION: 1 |EVENT DATE: 04/21/1999| | COUNTY: MONTGOMERY STATE: MD |EVENT TIME: 14:30[EDT]| |LICENSE#: 19-00296-17 AGREEMENT: Y |LAST UPDATE DATE: 04/23/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MOHAMED SHANBAKY R1 | | |FREDERICK COMBS NMSS | +------------------------------------------------+JOSEPH GIITTER IRO | | NRC NOTIFIED BY: ROBERT ZOON | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AN IRRADIATOR FAILED TO PROPERLY RETURN THE SOURCE TO THE FULLY SHIELDED | | POSITION. | | | | The following text is a portion of a facsimile received from the licensee: | | | | "This is a report in accordance with condition 17.E. of license 19-00296-17 | | which requires that with respect to each J. L. Shepherd and Associates Mark | | 1 Cesium-137 Irradiator, we ' ... notify the Commission by telephone ... if | | ... any malfunction of the irradiator is detected. | | | | "At approximately 2:30 p.m. April 21, 1999, a health physicist (HP) in the | | Radiation Safety Branch was continuing a quarterly inspection and leak test | | procedure which he had initiated on April 19, 1999. During this follow-up | | visit, he became aware of an apparent problem with a J. L. Shepherd Mark I | | Cesium-137 irradiator, which is located in Building 37, Room B440. This | | self-contained self-shielded irradiator contains approximately 3,850 Ci of | | Cs-137. | | | | "The [HP] reported the results of his investigation to me at 9:15 a.m. this | | morning. The problem was reported to the HP on April 21 by a designated | | user who explained that the source failed on at least one occasion to return | | to the fully shielded position following an irradiation procedure. The door | | interlock functioned as designed, which prevented the door from being | | opened. Thus, this situation resulted in NO safety problem or radiation | | exposure. | | | | "The HP, continuing his investigation, was able to duplicate a similar | | problem one additional time during the inspection. However, numerous | | repeated attempts to duplicate the problem did not result in a failure of | | the irradiator to properly stow the source. The HP did not, therefore, | | judge the irradiator to have malfunctioned. | | | | "Following the HP's discussion with me this morning, it was my judgement | | that the problem observed could be interpreted as a malfunction of the | | irradiator. Therefore, effective this morning, I directed the irradiator | | custodian to remove this irradiator from service and to contact J. L. | | Shepherd for maintenance to correct this problem. At that time, I also | | elected to report this apparent malfunction directly to you [Judith Joustra, | | Chief, Nuclear Materials Safety Branch, Region 1]. Upon your advice, I am | | simultaneously reporting this finding to the NRC Operations Center. | | | | "Upon receipt of the report of maintenance from the J. L. Shepherd service | | representative, I will forward you the explanation for the irradiator's | | failure to operate." | | | | (Call the NRC operations officer for a site contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35625 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 04/23/1999| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 16:42[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/23/1999| +------------------------------------------------+EVENT TIME: 16:00[EDT]| | NRC NOTIFIED BY: S. SAUER |LAST UPDATE DATE: 04/23/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUXILIARY BUILDING DISCOVERED AT POSITIVE PRESSURE TO THE OUTSIDE. | | | | The licensee determined at 1600 on 04/23/99 that this report met the | | criteria for reporting under 10CFR50.72 as a 1-hour report. | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 04/13/99 at 2135, the Unit 1 auxiliary building was found to be at a | | +0.03 inches of water with respect to the outdoors. The Updated Final | | Safety Analysis Report (UFSAR) states that the auxiliary building is | | designed to be at a slight negative pressure continuously with respect to | | the outdoors, to satisfy the criterion for preventing the uncontrolled | | release of radioactivity. Subsequent investigation found that the #12 | | auxiliary building exhaust fan was rotating backwards. The fan had been | | returned to service at 1337 on 04/13/99, the fan was removed from service at | | 2216. Maintenance inspections had been performed earlier that day that | | required the motor leads to be disconnected. The apparent cause is miss | | wiring of the motor by the maintenance technician. The fan was reworked and | | returned to service at 1110 on 04/14/99. Tech Spec 3.7.7.1 was in effect | | for the duration." | | | | The licensee intends to notify the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35627 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 04/24/1999| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 05:09[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 04/24/1999| +------------------------------------------------+EVENT TIME: 04:19[EDT]| | NRC NOTIFIED BY: BRIAN WEAVER |LAST UPDATE DATE: 04/24/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: |WILLIAM BATEMAN NRR | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS |JOSEPH GIITTER IRO | |ACCS 50.72(b)(1)(iv) ECCS INJECTION | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR SCRAM DUE TO UNKNOWN ELECTRICAL TRANSIENT | | | | The reactor scrammed due to an unknown electrical transient. All control | | rods fully inserted into the core. Both electric-driven reactor feedwater | | pumps tripped, all three condensate booster pumps tripped, and the | | recirculation pumps tripped. The plant is in natural circulation with high | | pressure core spray (HPCS) system injecting and maintaining reactor vessel | | water level between 160 to 200 inches. (Normal reactor vessel water level | | is 184 inches, and the top of the active fuel is -18 inches.) Reactor core | | isolation cooling (RCIC) and HPCS received automatic initiation signals on | | Level 2, and the Division 3 diesel automatically started but did not load. | | The RCIC pump failed to come up to speed and has been tripped. The main | | steam isolation valves are open, and reactor vessel pressure is being | | maintained at 600 to 700 psig. Uninterruptible power supply (UPS) "3B" | | tripped and has a blown fuse which prevents resetting of the inboard | | containment isolation valves. Both Containment Monitoring System(CMS) | | cabinets 10A and 10B are isolated (leak detection for particulate and | | gaseous) causing entry into Technical Specification 3.0.3. Due to UPS "3B" | | being tripped, the licensee has a one-half isolation signal to the main | | steam isolation valves. UPS "3B" provides logic to the scram system, etc. | | (UPS "3B" is essentially a major logic power supply for UPS.) | | | | The electrical transient (not sure if the transient was caused from offsite | | site power loss) caused a partial loss of lighting in the control room, a | | complete loss of lighting to the turbine building (was reported), and a loss | | of site perimeter lighting for a very short period of time. All UPS went to | | a battery source of power for a short period of time and then transferred | | back to normal power source (normally happens on a big electrical | | transient). All electrical in-house buses powered up, and the plant is | | stable. A condensate booster pump has been reestablished, and the licensee | | is starting to investigate what caused the electrical transient, RCIC not | | coming up to speed (places them in Tech Spec 3.7.4), and what caused the | | fuse to blow to UPS "3B." | | | | The licensee had not, at the time of this call, checked with Unit 1 to see | | if it had experienced a power loss for a short period of time. | | | | The NRC resident inspector will be notified of this event by the licensee. | | | | ***UPDATE AT 0751 EDT FROM ROY GREEN TAKEN BY MACKINNON*** | | | | The licensee updated this event to add the 4-hour notifications under 10 CFR | | 50.72 (b)(2) for a reactor protection system actuation, engineered safety | | feature (ESF) actuations, and accident mitigation. The 4-hour notifications | | were required for the reactor scram and the following ESF actuations: | | reactor water cleanup system isolation, standby gas initiation, control room | | special filter train initiation, reactor vessel water Level 2 containment | | isolations, and Division 3 (HPCS) automatic start on HPCS initiation. The | | third 4-hour notification was required for accident mitigation due to single | | train RCIC failure upon initiation. | | | | Plant Status: | | | | The scram has been reset, normal cooldown is in progress via the turbine | | bypass valves, reactor vessel water level is being maintained in its normal | | band with normal feedwater system, and UPS-3B remains de-energized | | preventing containment isolation recovery. Troubleshooting is in progress | | on UPS-3B and RCIC. (The region of instability on the power to flow map was | | not entered.) | | | | The licensee plans to place the unit in a Cold Shutdown condition on natural | | circulation. | | | | The NRC resident inspector was notified of this update by the licensee. The | | R1DO ( Mohamed Shanbaky) was notified by the NRC operations officer. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35628 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: GAMMA-METRICS |NOTIFICATION DATE: 04/23/1999| |LICENSEE: GAMMA-METRICS |NOTIFICATION TIME: 18:00[EDT]| | CITY: SAN DIEGO REGION: 4 |EVENT DATE: 04/23/1999| | COUNTY: STATE: CA |EVENT TIME: [PDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 04/24/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MOHAMED SHANBAKY R1 | | |LEN WERT R2 | +------------------------------------------------+MELVYN LEACH R3 | | NRC NOTIFIED BY: ROBERT BARNES |VERN HODGE(FAX) NRR | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INFORMATION ON A DEVIATION THAT DOES NOT REACH THE LEVEL OF A PART 21 | | REPORT | | | | There was an incorrect resistor shipped on log amplifier printed circuit | | assemblies. The worst case environmental temperature deviation would cause | | a maximum deviation of 6% (equivalent full-scale) error in the indicating | | region from 3 X 10-3% to 50% power. This would not compromise the ability | | to monitor safe shutdown reactor power level adequately during and after a | | design basis event. | | | | The following text is a portion of a facsimile received from GAMMA-METRICS: | | | | "Our lot control capability allowed us to determine that nineteen of the | | incorrect resistors were shipped from GAMMA-METRICS to our customers. ... We | | are recalling all nineteen defective resistors or the printed circuit | | assemblies. We will replace the resistors with the correct component and | | re-certify the repair at no charge to any of the listed customers." | | | | The following is a list of the facilities affected: | | | | 1. Georgia Power, Vogtle 1 and 2 - 9 assemblies (replaced in March 1999) | | 2. Duke Energy, Catawba - 1 assembly | | 3. AEP DC Cook - 2 assemblies (not installed) | | 4. Ontario Hydro, Pickering - 1 assembly (not installed) | | 5. Maine Yankee - 4 assemblies (not installed and plant shutdown for | | decommissioning) | | 6. Penn State University - 2 assemblies (not installed) | | | | There were letters sent to the affected customers. | | | | (Call the NRC operations officer for a contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35629 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 04/24/1999| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 13:09[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 04/24/1999| +------------------------------------------------+EVENT TIME: [CDT]| | NRC NOTIFIED BY: KEVIN PETERSON |LAST UPDATE DATE: 04/24/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR WATER LEVEL HIGH ENOUGH TO ENTER THE MAIN STEAM LINES (Refer to | | event numbers 35617 and 35618 for event-related information.) | | | | During an engineering evaluation of the reactor scram that occurred on | | 04/22/99, it was determined that reactor water level entered the main steam | | lines. This potentially made reactor core isolation cooling and high | | pressure coolant injection inoperable. The cause of the high water level | | condition is under investigation. | | | | The licensee notified the NRC Resident Inspector and intends to notify state | | and local government agencies. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35630 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 04/24/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 15:28[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 04/24/1999| +------------------------------------------------+EVENT TIME: [CDT]| | NRC NOTIFIED BY: JIM SCHOTTEL |LAST UPDATE DATE: 04/24/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY PARAMETER DISPLAY SYSTEM (SPDS) OUT OF SERVICE DUE TO MAINTENANCE. | | | | Planned maintenance on an uninterruptible power supply bus (1B) for the | | process computer will disable some points on the SPDS for 48 hours. | | Operators are taking compensatory measures for monitoring parameters. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35631 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRAIDWOOD REGION: 3 |NOTIFICATION DATE: 04/24/1999| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 22:15[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/24/1999| +------------------------------------------------+EVENT TIME: 19:36[CDT]| | NRC NOTIFIED BY: MARK ANDREWS |LAST UPDATE DATE: 04/24/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH STEAM GENERATOR LEVEL ESF ACTUATION | | | | During cooldown, after performing a plant shutdown for a refueling outage, | | narrow range level was noted to be increasing in the '2A' and '2C' steam | | generators. The feedwater isolation valves were checked closed, and | | additional manual isolation valves were closed. Steam generator blowdown | | was in the process of being put in service when level reached the P14 | | setpoint which caused an engineered safety features actuation (includes main | | feedwater pump trip and feedwater isolation signal). | | | | Further investigation found auxiliary feedwater valves open that together | | with the pressure head from the water level in the condensate tank was | | sufficient to feed the steam generators. | | | | Steam generator level was restored once blowdown was established. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35632 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 04/26/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 01:41[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 04/26/1999| +------------------------------------------------+EVENT TIME: 00:01[EDT]| | NRC NOTIFIED BY: FERNSLER |LAST UPDATE DATE: 04/26/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 2 Startup |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 WAS MANUALLY SCRAMMED FROM 2% POWER TO PERMIT ENTRY INTO THE DRYWELL | | FOR REPAIR WORK. | | | | THE UNIT WAS MANUALLY SHUTDOWN TO PERMIT ENTRY INTO CONTAINMENT TO PERFORM | | REPAIRS TO THE TRANSVERSING INCORE PROBE(TIP) CHANNEL TUBING. PRIOR TO | | SHUTDOWN THE UNIT WAS IN THE PROCESS OF RESTARTING FOLLOWING THE 9TH | | REFUELING OUTAGE. DURING POST MAINTENANCE TESTING, A RESTRICTION WAS | | DISCOVERED IN THE TUBING OF THE "C" TIP MECHANISM. THIS PREVENTED INSERTION | | OF ITS DETECTOR AND CALIBRATION OF ITS ASSOCIATED LPRM. IN ORDER TO PERFORM | | REPAIRS, THE REACTOR HAD TO BE SHUTDOWN FOR DRYWELL ENTRY. FOLLOWING | | SHUTDOWN REACTOR WATER LEVEL REMAINED ESSENTIALLY UNCHANGED AT 35.7" AS | | RECORDED ON THE NARROW RANGE INSTRUMENTATION. ALL RODS FULLY INSERTED, NO | | ECCS INITIATIONS OR DIESEL STARTS OCCURRED AND NO SAFETY RELIEF VALVES | | LIFTED. THIS EVENT IS NOT REPORTABLE AS A RPS ACTUATION SINCE IT IS | | PROCEDURALLY RECOGNIZED AS PRE-PLANNED. HEAT SINK IS THE SHUTDOWN COOLING | | TO THE SUPPRESSION POOL. THEY WILL CONTINUE COOLDOWN TO MODE 4. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021