The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for April 23, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           04/22/1999 - 04/23/1999

                              ** EVENT NUMBERS **

35600  35611  35612  35617  35618  35619  35620  35621  35622  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35600       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DRESDEN                  REGION:  3  |NOTIFICATION DATE: 04/17/1999|
|    UNIT:  [] [] [3]                 STATE:  IL |NOTIFICATION TIME: 11:58[EDT]|
|   RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3           |EVENT DATE:        04/17/1999|
+------------------------------------------------+EVENT TIME:        09:59[CDT]|
| NRC NOTIFIED BY:  DAVE SLAGER                  |LAST UPDATE DATE:  04/23/1999|
|  HQ OPS OFFICER:  LEIGH TROCINE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JOHN JACOBSON        R3      |
|10 CFR SECTION:                                 |                             |
|ADEG 50.72(b)(1)(ii)     DEGRAD COND DURING OP  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|                                                   |                          |
|3     N          Y       99       Power Operation  |99       Power Operation  |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| FAILURE OF A PRIMARY CONTAINMENT AIR SAMPLE RETURN ISOLATION VALVE TO MEET   |
| MAXIMUM INSERVICE TEST STROKE-TIME REQUIREMENTS                              |
|                                                                              |
| While performing quarterly valve stroke-time testing on Unit 3, a primary    |
| containment air sample return isolation valve exceeded its specified maximum |
| stroke-time limit.  The sample return line was isolated in accordance with   |
| Technical Specification 3.7.D for primary containment isolation valves, and  |
| this action satisfied the 4-hour limiting condition for operation action     |
| statement requirements.  The second in-line primary containment isolation    |
| system valve remains operable.                                               |
|                                                                              |
| The licensee stated that no other valves failed to meet the maximum          |
| stroke-time limits.  The licensee also stated that, during a test that was   |
| performed last month, the valve in question was identified as being in the   |
| 'Alert' time range for inservice test timing requirements and that it was    |
| being tested per the required increased testing frequency.  Corrective       |
| actions are being initiated, and troubleshooting activities are in           |
| progress.                                                                    |
|                                                                              |
| The licensee plans to notify the NRC resident inspector.                     |
|                                                                              |
| *** UPDATE ON 4/23/99 @ 0443 BY GADBOIS TO GOULD ***  RETRACTION             |
|                                                                              |
| UPON FURTHER REVIEW, IT WAS DETERMINED THAT THIS EVENT DID NOT CONSTITUTE A  |
| REPORTABLE CONDITION SINCE THE PENETRATION HAD A OPERABLE REDUNDANT VALVE    |
| WHICH COULD HAVE ISOLATED THE CONTAINMENT PENETRATION.  THEREFORE, THEY ARE  |
| RETRACTING THIS EVENT.                                                       |
|                                                                              |
| THE RESIDENT INSPECTOR WILL BE NOTIFIED.                                     |
|                                                                              |
| THE REG 3 RDO(LEACH) WAS NOTIFIED.                                           |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35611       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LIMERICK                 REGION:  1  |NOTIFICATION DATE: 04/20/1999|
|    UNIT:  [1] [] []                 STATE:  PA |NOTIFICATION TIME: 19:21[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        04/20/1999|
+------------------------------------------------+EVENT TIME:        18:32[EDT]|
| NRC NOTIFIED BY:  RAY McKINLEY                 |LAST UPDATE DATE:  04/22/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MOHAMED SHANBAKY     R1      |
|10 CFR SECTION:                                 |CURT COWGILL         R1      |
|ACCS 50.72(b)(1)(iv)     ECCS INJECTION         |R. BLOUGH/D. FLOREK  R1      |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |ART BURRITT          SRI     |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |WILLIAM BATEMAN      NRR     |
|                                                |CHARLES MILLER       IRO     |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       100      Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - AUTO REACTOR SCRAM FROM 100% POWER DUE TO LOSS OF MAIN FEEDWATER; ECCS     |
| INJECTION -                                                                  |
|                                                                              |
| AT 1832 ON 04/20/99, WITH UNIT 1 AT 100% POWER, ALL EIGHT CONDENSATE SYSTEM  |
| DEEP BED DEMINERALIZER OUTLET MOTOR OPERATED VALVES FAILED CLOSED POSSIBLY   |
| DUE TO A COMPUTER MALFUNCTION.  THE DEMINERALIZER BYPASS VALVES TRIPPED DUE  |
| TO THERMAL OVERLOADS AND FAILED TO OPEN, CAUSING ALL THREE STEAM DRIVEN MAIN |
| FEEDWATER PUMPS TO TRIP.  THE REACTOR VESSEL WATER LEVEL DROPPED FROM A      |
| NORMAL LEVEL OF +35 INCHES TO +12.5 INCHES, CAUSING THE REACTOR TO           |
| AUTOMATICALLY SCRAM FROM 100% POWER DUE TO LOW REACTOR VESSEL WATER LEVEL.   |
| ALL CONTROL RODS INSERTED COMPLETELY; HOWEVER, ROD #30-39 INSERTED SLOWLY.   |
| NO SAFETY/RELIEF VALVES LIFTED.  STEAM IS BEING DUMPED TO THE MAIN           |
| CONDENSER.                                                                   |
|                                                                              |
| REACTOR VESSEL WATER LEVEL FURTHER DROPPED TO -38 INCHES, CAUSING THE HIGH   |
| PRESSURE COOLANT INJECTION (HPCI)  AND THE REACTOR CORE ISOLATION COOLING    |
| (RCIC) SYSTEMS TO ACTUATE AND INJECT INTO THE REACTOR VESSEL.  THE REDUNDANT |
| REACTIVITY CONTROL SYSTEM INITIATED TO TRIP THE CIRCUIT BREAKERS FOR THE     |
| REACTOR RECIRCULATION PUMPS.  PRIMARY CONTAINMENT ISOLATION SYSTEM GROUPS    |
| 1B, 2A, 2B, 2C, 3, 6A, 6B, 6C, 7B, AND 8B ISOLATED.  THE DIVISION 'A'        |
| ATWS/RPT CIRCUIT BREAKER FOR THE 'A' RECIRC MOTOR GENERATOR SET FAILED TO    |
| TRIP, AS REQUIRED.  SMOKE WAS OBSERVED TO BE COMING FROM THE BREAKER.  THE   |
| BREAKER WAS MANUALLY TRIPPED FROM THE CONTROL ROOM AND THE SMOKING STOPPED.  |
| THE 'A' AND 'B' RECIRC MOTOR GENERATOR SET DRIVE MOTOR CIRCUIT BREAKERS ALSO |
| FAILED TO TRIP ON THE 13 kV BUS FAST TRANSFER.  THE BREAKERS WERE MANUALLY   |
| TRIPPED.                                                                     |
|                                                                              |
| REACTOR VESSEL WATER LEVEL DROPPED TO A LOW LEVEL OF -75 INCHES ABOUT 40     |
| SECONDS INTO THE EVENT (TOP OF ACTIVE FUEL IS  -161 INCHES).  THE HPCI AND   |
| RCIC SYSTEMS RECOVERED REACTOR VESSEL WATER LEVEL TO +25 INCHES, AT WHICH    |
| TIME CONTROL ROOM OPERATORS MANUALLY SECURED THE HPCI SYSTEM.  THE RCIC      |
| SYSTEM IS MAINTAINING REACTOR VESSEL WATER LEVEL AT +25 INCHES WITH REACTOR  |
| PRESSURE AT 875 PSIG AT AN INJECTION RATE OF 300 GPM.                        |
|                                                                              |
| PLANT OPERATORS ENCOUNTERED A PROBLEM WITH THE AUXILIARY STEAM SYSTEM AND    |
| THE MECHANICAL VACUUM PUMP.  THEY MANUALLY CLOSED THE MAIN STEAM ISOLATION   |
| VALVES.  THEY ARE CONTROLLING REACTOR VESSEL WATER LEVEL WITH THE RCIC       |
| SYSTEM AND REACTOR COOLANT SYSTEM PRESSURE WITH THE HPCI SYSTEM.             |
|                                                                              |
| UNIT 1 IS STABLE IN OPERATIONAL CONDITION 3 (HOT SHUTDOWN) AND COOLING DOWN  |
| TO COLD SHUTDOWN.  PRIMARY CONTAINMENT PARAMETERS ARE NORMAL.  THERE WAS NO  |
| RELEASE OF RADIOACTIVE MATERIAL.  RELEASE RATES ARE NORMAL.  THIS EVENT HAD  |
| NO IMPACT ON UNIT 2 WHICH IS IN OPERATIONAL CONDITION 5 IN A REFUELING       |
| OUTAGE.                                                                      |
|                                                                              |
| THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR AND IS INVESTIGATING THIS   |
| EVENT.  THEY PLAN TO ISSUE A PRESS RELEASE.                                  |
|                                                                              |
| *** UPDATE ON 4/21/99 @ 0418 BY HUNTER TO GOULD ***                          |
|                                                                              |
| THE REACTOR IS IN OPCON 3 AT 350 PSIG CONTINUING TO COLD SHUTDOWN.           |
| CONDENSER VACUUM IS BEING REESTABLISHED IN ORDER TO RE-OPEN THE MSIVs AND    |
| SECURE HPCI FROM PRESSURE CONTROL MODE.  FEEDWATER SYSTEM IS BEING           |
| REPRESSURIZED TO REESTABLISH NORMAL FEED AND SECURE RCIC FROM LEVEL CONTROL  |
| MODE.                                                                        |
|                                                                              |
| ALSO THE "1A" AND "1B" MG SET DRIVE MOTOR BREAKERS DID NOT TRIP DURING THE   |
| TRANSIENT SINCE PLANT LOADS WERE PREVIOUSLY TRANSFERRED BY A REACTOR         |
| OPERATOR PRIOR TO THE TURBINE TRIP.  THE BREAKERS, THEREFORE, OPERATED AS    |
| DESIGNED.                                                                    |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED.                                         |
|                                                                              |
| THE REG 1 RDO(SHANBAKY) WAS NOTIFIED.                                        |
|                                                                              |
| *** UPDATE ON 4/22/99 @ 0220 BY HUNTER TO GOULD ***                          |
|                                                                              |
| THE UNIT IS IN COLD SHUTDOWN AS OF 2214 ON 4/21/99.   RESOLUTION OF          |
| EQUIPMENT PROBLEMS WHICH RESULTED IN THE SHUTDOWN ARE IN PROGRESS.           |
| ACTIVITIES ARE ALSO IN PROGRESS FOR PLANT STARTUP.                           |
|                                                                              |
| ALL CONTROL RODS INCLUDING 30-39 WENT FULL IN WITHIN THE REQUIRED TECHNICAL  |
| SPECIFICATION TIME.  ROD 30-39 POSITION INDICATION WAS LOST FOR              |
| APPROXIMATELY TWO MINUTES AFTER THE SCRAM, THEN THE "00" FULL IN POSITION    |
| INDICATION BECAME AVAILABLE AND REMAINED AVAILABLE THROUGHOUT THE SHUTDOWN.  |
|                                                                              |
| THE RESIDENT INSPECTOR WILL BE INFORMED.  THE REG 1 RDO(SHANBAKY) WAS        |
| INFORMED.                                                                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   35612       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  MA DEPT OF PUBLIC HEALTH RCP         |NOTIFICATION DATE: 04/21/1999|
|LICENSEE:  AEA TECHNOLOGIES QSA, INC            |NOTIFICATION TIME: 15:00[EDT]|
|    CITY:  BURLINGTON               REGION:  1  |EVENT DATE:        04/21/1999|
|  COUNTY:                            STATE:  MA |EVENT TIME:        14:00[EDT]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  04/22/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |MOHAMED SHANBAKY     R1      |
|                                                |FREDERICK COMBS      NMSS    |
+------------------------------------------------+JOSEPH GIITTER       IRO     |
| NRC NOTIFIED BY:  KEN TRAEGDE                  |DONNA MARIE PEREZ    IP      |
|  HQ OPS OFFICER:  DICK JOLLIFFE                |LEN WERT             R2      |
+------------------------------------------------+DALE POWERS          R4      |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|NOCM                     COMM ASST BRIEF        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - SHIPMENT OF 8 Ir-192 SOURCES (866 CURIES TOTAL) FROM BURLINGTON, MA,       |
| OVERDUE IN MEXICO -                                                          |
|                                                                              |
| AT 1500 EDT ON 04/21/99, KEN TRAEGDE OF THE MA DEPARTMENT OF PUBLIC HEALTH   |
| RADIATION CONTROL PROGRAM (RCP) LOCATED IN BOSTON, MA, REPORTED THAT ON      |
| 04/16/99, AEA TECHNOLOGY QSA, INC., LOCATED IN BURLINGTON, MA, SHIPPED A     |
| MODEL #855 SOURCE CHANGER LOADED WITH 8 Ir-192 SOURCES (TOTALING 866 CURIES) |
| VIA FEDERAL EXPRESS TO VICONT S.A. DE C.V. LOCATED IN TOLUCA, MEXICO.  THE   |
| UNDAMAGED PACKAGE HAD A TRANSPORT INDEX OF 1.4 (NORMAL READINGS OF 1.4 mR/HR |
| AT 1 METER AND 55 mR/HR AT THE SURFACE) AT THE TIME OF SHIPMENT.             |
|                                                                              |
| THE SHIPMENT WAS SCHEDULED TO ARRIVE IN MEXICO ON 04/17/99.  AS OF 1400 EDT  |
| ON 04/21/99, THE RECIPIENT (VICONT S.A. DE C.V.) HAD RECEIVED THE SHIPPING   |
| PAPERS BUT NOT THE CONTAINER.  THE SHIPPER AND FEDERAL EXPRESS HAVE LAUNCHED |
| A FULL SEARCH FOR THE PACKAGE.  THE FEDERAL EXPRESS HAZARDS MATERIAL         |
| INVESTIGATION TEAM HAS CONDUCTED A PHYSICAL SEARCH OF EXPRESS DEPOTS IN      |
| BOSTON, MEMPHIS, LOS ANGELES, AND MEXICO.                                    |
|                                                                              |
| THE LICENSE NUMBERS ARE:  SU-1485, 12-8361, 52-0243, 54-0237, AND 58-0242.   |
|                                                                              |
| CONTACT THE NRC OPERATIONS OFFICER FOR APPLICABLE TELEPHONE NUMBERS.         |
|                                                                              |
| THE NRC OPERATIONS OFFICER NOTIFIED THE DOT NATIONAL RESPONSE CENTER         |
| (GAUTHIER); REPORT NUMBER 481132.                                            |
|                                                                              |
| *********************************** UPDATE AT 1345 ON 04/22/99 BY JONES      |
| ***********************************                                          |
|                                                                              |
| The NRC entered the Monitoring Phase of Normal Mode at 1345 on 04/22/99.     |
| The NRC operations officer notified, the R1DO (Shanbaky), Region 1 (Miller), |
| IRO (Congel and Giitter), NMSS (Paperiello), RCT (Weinstein), PAO (Gagner),  |
| EDO's office (name unknown), and Chairman's office (Holian).  The RCT        |
| notified  FEMA (Dan Rishe), DOE (Thomas Yates), EPA (Ms. Reddy), USDA (Bob   |
| Conley), HHS/CDC (James Raab), and DOT (Rick Boyle).                         |
|                                                                              |
|                                                                              |
|                                                                              |
| *********************************** UPDATE AT 1600 ON 04/22/99 BY JONES      |
| ***********************************                                          |
|                                                                              |
| A Commissioner's Assistants Briefing was conducted at 1600 on 04/22/99. The  |
| following notifications were made (* office did not participate):  IRO (Joe  |
| Giitter, Erick Weinstein), Chairman Jackson (Dan Gillen), Commissioner Dicus |
| (Joel Lubenau), Commissioner Diaz (Patrick Castleman), Commissioner          |
| McGaffigan (Janet Schlueter), Commissioner Merrifield (JohnThoma), EDO (*),  |
| DEDE (*), NMSS (Don Cool, Carl Paperiello), NMSS EO (Fred Combs), R1DO       |
| (Mohamed Shanbaky), PAO (Joe Gilland), CAO (Thomas Madden), SECY (Andrew     |
| Bates), SP (Paul Lohaus), IP (Ron Hauber), R1 (Felicia Hinson, Jim Wiggins,  |
| etc), and R2 (Doug Collins, Chuck Hosey, Rich Woodruff).  The briefer was    |
| Fred Combs of NMSS.                                                          |
|                                                                              |
| 1610 Played back tape of briefing for EDO (Dan Martin) and DEDE (Jocelyn     |
| Mitchell).                                                                   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35617       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MONTICELLO               REGION:  3  |NOTIFICATION DATE: 04/22/1999|
|    UNIT:  [1] [] []                 STATE:  MN |NOTIFICATION TIME: 03:00[EDT]|
|   RXTYPE: [1] GE-3                             |EVENT DATE:        04/22/1999|
+------------------------------------------------+EVENT TIME:        01:31[CDT]|
| NRC NOTIFIED BY:  PFEFFER                      |LAST UPDATE DATE:  04/22/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MELVYN LEACH         R3      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       100      Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE PLANT HAD A REACTOR SCRAM ON LOW REACTOR WATER LEVEL.                    |
|                                                                              |
| THE PLANT HAD A REACTOR SCRAM FROM 100% POWER DUE TO A LOW REACTOR WATER     |
| LEVEL.  CAUSE OF THE LOW REACTOR WASTER LEVEL IS UNKNOWN AND BEING           |
| INVESTIGATED.  ALL RODS FULLY INSERTED, NO ECCS INJECTION OCCURRED, AND NO   |
| SAFETY RELIEF VALVES LIFTED.  PLANT DID HAVE GROUP 2 AND GROUP 3 ISOLATIONS. |
| THE GROUP 3 ISOLATION HAS BEEN RESET, AND  PRESENTLY  THEY ARE IN PROGRESS   |
| OF RESETTING THE GROUP 2 ISOLATION.  THE MAIN CONDENSER IS THE HEAT SINK.    |
|                                                                              |
| THE RESIDENT INSPECTOR WILL BE INFORMED.                                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35618       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MONTICELLO               REGION:  3  |NOTIFICATION DATE: 04/22/1999|
|    UNIT:  [1] [] []                 STATE:  MN |NOTIFICATION TIME: 06:32[EDT]|
|   RXTYPE: [1] GE-3                             |EVENT DATE:        04/22/1999|
+------------------------------------------------+EVENT TIME:        01:45[CDT]|
| NRC NOTIFIED BY:  WELLER                       |LAST UPDATE DATE:  04/22/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MELVYN LEACH         R3      |
|10 CFR SECTION:                                 |                             |
|AINB 50.72(b)(2)(iii)(B) POT RHR INOP           |                             |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION    |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Hot Shutdown     |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE LICENSEE DECLARED HPCI INOPERABLE AND ENTERED AN LCO ACTION STATEMENT.   |
|                                                                              |
| THE HPCI SYSTEM WAS DECLARED INOPERABLE FROM 0145 TO 0236 DUE TO MOISTURE IN |
| THE TURBINE STEAM INLET LINE.  A HPCI TURBINE INLET HIGH DRAIN POT LEVEL     |
| ANNUNCIATION WAS  RECEIVED AT 0145.  RCIC WAS VERIFIED OPERABLE.  THE        |
| STEAMLINE MANUAL DRAIN VALVE WAS OPENED AND THE DRAIN LINE ANNUNCIATOR       |
| CLEARED AT 0236.  HPCI WAS DECLARED OPERABLE AND PLACED IN STANDBY.          |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED.                                         |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35619       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CALVERT CLIFFS           REGION:  1  |NOTIFICATION DATE: 04/22/1999|
|    UNIT:  [1] [2] []                STATE:  MD |NOTIFICATION TIME: 14:36[EDT]|
|   RXTYPE: [1] CE,[2] CE                        |EVENT DATE:        04/21/1999|
+------------------------------------------------+EVENT TIME:             [EDT]|
| NRC NOTIFIED BY:  BRUCE MONTGOMERY             |LAST UPDATE DATE:  04/22/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MOHAMED SHANBAKY     R1      |
|10 CFR SECTION:                                 |                             |
|NINF                     INFORMATION ONLY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          N       0        Refueling        |0        Refueling        |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - VOLUNTARY FITNESS-FOR-DUTY REPORT -                                        |
|                                                                              |
| A licensed operator was determined to be just below the limit by random      |
| test.  The employee's access to the plant was terminated.  Refer to the HOO  |
| Log for additional details.                                                  |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Other Nuclear Material                           |Event Number:   35620       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  U.S. ARMY (ACALA)                    |NOTIFICATION DATE: 04/22/1999|
|LICENSEE:  U.S. ARMY (ACALA)                    |NOTIFICATION TIME: 17:22[EDT]|
|    CITY:  ROCK ISLAND              REGION:  3  |EVENT DATE:        04/22/1999|
|  COUNTY:                            STATE:  IL |EVENT TIME:             [CDT]|
|LICENSE#:  12-00722-06           AGREEMENT:  Y  |LAST UPDATE DATE:  04/22/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |MOHAMED SHANBAKY     R1      |
|                                                |MELVYN LEACH         R3      |
+------------------------------------------------+FREDERICK COMBS      NMSS    |
| NRC NOTIFIED BY:  GAVIN ZIGLER                 |                             |
|  HQ OPS OFFICER:  FANGIE JONES                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|IBAC 30.50(b)(1)(i)      ACCESS DENIED >24 HRS  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| DAMAGED VIAL CONTAINING 0.8 CURIES OF TRITIUM                                |
|                                                                              |
| During repair activities at Fort Drum, New York, in the arms room, an M224   |
| range indicator was apparently damaged.  The illuminator was checked working |
| prior to the maintenance and noted not to be working later.  The contained   |
| vial of tritium, 0.8 Ci, used in the illuminator is assumed to be broken.    |
| The device has been double bagged and the area secured until the results of  |
| surveys are obtained.  Survey results were sent off site as lab facilities   |
| are not available on site.  Investigation of the event is ongoing, and no    |
| further information is available at this time.                               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35621       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CRYSTAL RIVER            REGION:  2  |NOTIFICATION DATE: 04/22/1999|
|    UNIT:  [3] [] []                 STATE:  FL |NOTIFICATION TIME: 19:02[EDT]|
|   RXTYPE: [3] B&W-L-LP                         |EVENT DATE:        04/22/1999|
+------------------------------------------------+EVENT TIME:        18:08[EDT]|
| NRC NOTIFIED BY:  BILL BANDHAUGER              |LAST UPDATE DATE:  04/22/1999|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LEN WERT             R2      |
|10 CFR SECTION:                                 |                             |
|AOUT 50.72(b)(1)(ii)(B)  OUTSIDE DESIGN BASIS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|3     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| POSSIBLE OVERLOAD OF ESF TRANSFORMER IN AN ABNORMAL OPERATING PROCEDURE      |
| FOUND                                                                        |
|                                                                              |
| While investigating a previous LER concerned with backfeed the following was |
| discovered:                                                                  |
|                                                                              |
| "During a scenario involving a Loss of Off-Site Power resulting from a loss  |
| of the BEST and Startup transformers, the Crystal River Unit 3 abnormal      |
| operating procedures could have caused an overload of the safety-related     |
| Engineered Safeguards 4160V to 480V transformer.  Assuming a single failure  |
| of the 'B' side diesel generator, power could have been unavailable to both  |
| trains of 480V Engineered safeguards loads.                                  |
|                                                                              |
| "This condition is considered reportable per 10 CFR 50.72(b)(l)(ii)(B) and   |
| 10 CFR 50.73(a)(2)(ii)(B) as a condition outside of the design basis of the  |
| plant.                                                                       |
|                                                                              |
| "Loads have been identified which can be administratively maintained off     |
| during this scenario to avoid the overload condition, and therefore, the     |
| transformer is operable."                                                    |
|                                                                              |
| This is under investigation, and further actions will be forthcoming.        |
|                                                                              |
| The licensee intends to notify the NRC Resident Inspector.                   |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35622       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MONTICELLO               REGION:  3  |NOTIFICATION DATE: 04/23/1999|
|    UNIT:  [1] [] []                 STATE:  MN |NOTIFICATION TIME: 04:33[EDT]|
|   RXTYPE: [1] GE-3                             |EVENT DATE:        04/23/1999|
+------------------------------------------------+EVENT TIME:        02:14[CDT]|
| NRC NOTIFIED BY:  WELLER                       |LAST UPDATE DATE:  04/23/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |MELVYN LEACH         R3      |
|10 CFR SECTION:                                 |                             |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION    |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Hot Shutdown     |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| HPCI SYSTEM DECLARED INOPERABLE AND PLANT ENTERED LCO ACTION STATEMENT       |
|                                                                              |
| THE HPCI SYSTEM WAS DECLARED INOPERABLE FROM 0214 TO 0220 DUE TO MOISTURE IN |
| THE TURBINE STEAM INLET LINE.  A 14-DAY LCO ACTION STATEMENT WAS ENTERED,    |
| AND RCIC WAS VERIFIED OPERABLE.  HPCI TURBINE INLET HIGH DRAIN POT LEVEL     |
| ANNUNCIATION WAS RECEIVED  DUE TO STROKING MO-2036 (TURBINE STEAM SUPPLY     |
| VALVE) AS PART OF THE REACTOR SHUTDOWN PROCEDURE AT REACTOR PRESSURE OF 500  |
| PSIG.  THE STEAM LINE MANUAL DRAIN VALVE WAS OPENED, AND THE ANNUNCIATOR     |
| CLEARED AT 0220.  HPCI DECLARED OPERABLE AND IN STANDBY.  THE 14-DAY LCO     |
| ACTION STATEMENT WAS ALSO EXITED AT 0220.                                    |
|                                                                              |
| THE RESIDENT INSPECTOR WILL BE NOTIFIED.                                     |
+------------------------------------------------------------------------------+


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