Event Notification Report for April 22, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/21/1999 - 04/22/1999 ** EVENT NUMBERS ** 35494 35611 35612 35613 35614 35615 35616 35617 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35494 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 03/20/1999| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 20:20[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 03/20/1999| +------------------------------------------------+EVENT TIME: 18:57[EST]| | NRC NOTIFIED BY: ERIC OLSON |LAST UPDATE DATE: 04/21/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JACK MCFADDEN R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RCIC INOPERABLE | | | | The licensee declared Reactor Core Isolation Cooling (RCIC) inoperable | | because of a problem found during a surveillance. Relay 13A-k30 contacts 1 | | - 7 were found to have a high resistance. These contacts close to provide | | the 'A' channel input to the RCIC high level shutdown. A high resistance | | across these contacts may prevent the actuating relay (13A-k38) from | | energizing, and thereby prevent a shutdown of RCIC on a high reactor vessel | | water level. The RCIC high water level shutdown requires both channels 'A' | | and 'B' signals be present to occur. | | | | The licensee entered a 14 day LCO because of this condition. Repair | | efforts are in progress. RCIC remains available for use in the event of an | | emergency. | | | | The licensee will inform the NRC resident inspector. | | | | * * * UPDATE at 1903 on 04/21/99 by MIKE ENGLAND to JOLLIFFE * * * | | | | After further evaluation of this event, the licensee determined that the | | as-found condition of the RCIC System did not affect its operability since | | the last surveillance test. NUREG-1022, Rev 1, Section 3.2.2, Item 3, | | discusses this instance. Therefore, the RCIC System was not inoperable due | | to the above problem. Thus, the licensee desires to retract this report. | | | | The licensee notified the NRC Resident Inspector. The NRC Operations | | Officer notified the R1DO MOHAMED SHANBAKY. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35611 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 04/20/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 19:21[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 04/20/1999| +------------------------------------------------+EVENT TIME: 18:32[EDT]| | NRC NOTIFIED BY: RAY McKINLEY |LAST UPDATE DATE: 04/22/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: |CURT COWGILL R1 | |ACCS 50.72(b)(1)(iv) ECCS INJECTION |R. BLOUGH/D. FLOREK R1 | |ARPS 50.72(b)(2)(ii) RPS ACTUATION |ART BURRITT SRI | |AESF 50.72(b)(2)(ii) ESF ACTUATION |WILLIAM BATEMAN NRR | | |CHARLES MILLER IRO | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - AUTO REACTOR SCRAM FROM 100% POWER DUE TO LOSS OF MAIN FEEDWATER; ECCS | | INJECTION - | | | | AT 1832 ON 04/20/99, WITH UNIT 1 AT 100% POWER, ALL EIGHT CONDENSATE SYSTEM | | DEEP BED DEMINERALIZER OUTLET MOTOR OPERATED VALVES FAILED CLOSED POSSIBLY | | DUE TO A COMPUTER MALFUNCTION. THE DEMINERALIZER BYPASS VALVES TRIPPED DUE | | TO THERMAL OVERLOADS AND FAILED TO OPEN, CAUSING ALL THREE STEAM DRIVEN MAIN | | FEEDWATER PUMPS TO TRIP. THE REACTOR VESSEL WATER LEVEL DROPPED FROM A | | NORMAL LEVEL OF +35 INCHES TO +12.5 INCHES, CAUSING THE REACTOR TO | | AUTOMATICALLY SCRAM FROM 100% POWER DUE TO LOW REACTOR VESSEL WATER LEVEL. | | ALL CONTROL RODS INSERTED COMPLETELY; HOWEVER, ROD #30-39 INSERTED SLOWLY. | | NO SAFETY/RELIEF VALVES LIFTED. STEAM IS BEING DUMPED TO THE MAIN | | CONDENSER. | | | | REACTOR VESSEL WATER LEVEL FURTHER DROPPED TO -38 INCHES, CAUSING THE HIGH | | PRESSURE COOLANT INJECTION (HPCI) AND THE REACTOR CORE ISOLATION COOLING | | (RCIC) SYSTEMS TO ACTUATE AND INJECT INTO THE REACTOR VESSEL. THE REDUNDANT | | REACTIVITY CONTROL SYSTEM INITIATED TO TRIP THE CIRCUIT BREAKERS FOR THE | | REACTOR RECIRCULATION PUMPS. PRIMARY CONTAINMENT ISOLATION SYSTEM GROUPS | | 1B, 2A, 2B, 2C, 3, 6A, 6B, 6C, 7B, AND 8B ISOLATED. THE DIVISION 'A' | | ATWS/RPT CIRCUIT BREAKER FOR THE 'A' RECIRC MOTOR GENERATOR SET FAILED TO | | TRIP, AS REQUIRED. SMOKE WAS OBSERVED TO BE COMING FROM THE BREAKER. THE | | BREAKER WAS MANUALLY TRIPPED FROM THE CONTROL ROOM AND THE SMOKING STOPPED. | | THE 'A' AND 'B' RECIRC MOTOR GENERATOR SET DRIVE MOTOR CIRCUIT BREAKERS ALSO | | FAILED TO TRIP ON THE 13 kV BUS FAST TRANSFER. THE BREAKERS WERE MANUALLY | | TRIPPED. | | | | REACTOR VESSEL WATER LEVEL DROPPED TO A LOW LEVEL OF -75 INCHES ABOUT 40 | | SECONDS INTO THE EVENT (TOP OF ACTIVE FUEL IS -161 INCHES). THE HPCI AND | | RCIC SYSTEMS RECOVERED REACTOR VESSEL WATER LEVEL TO +25 INCHES, AT WHICH | | TIME CONTROL ROOM OPERATORS MANUALLY SECURED THE HPCI SYSTEM. THE RCIC | | SYSTEM IS MAINTAINING REACTOR VESSEL WATER LEVEL AT +25 INCHES WITH REACTOR | | PRESSURE AT 875 PSIG AT AN INJECTION RATE OF 300 GPM. | | | | PLANT OPERATORS ENCOUNTERED A PROBLEM WITH THE AUXILIARY STEAM SYSTEM AND | | THE MECHANICAL VACUUM PUMP. THEY MANUALLY CLOSED THE MAIN STEAM ISOLATION | | VALVES. THEY ARE CONTROLLING REACTOR VESSEL WATER LEVEL WITH THE RCIC | | SYSTEM AND REACTOR COOLANT SYSTEM PRESSURE WITH THE HPCI SYSTEM. | | | | UNIT 1 IS STABLE IN OPERATIONAL CONDITION 3 (HOT SHUTDOWN) AND COOLING DOWN | | TO COLD SHUTDOWN. PRIMARY CONTAINMENT PARAMETERS ARE NORMAL. THERE WAS NO | | RELEASE OF RADIOACTIVE MATERIAL. RELEASE RATES ARE NORMAL. THIS EVENT HAD | | NO IMPACT ON UNIT 2 WHICH IS IN OPERATIONAL CONDITION 5 IN A REFUELING | | OUTAGE. | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR AND IS INVESTIGATING THIS | | EVENT. THEY PLAN TO ISSUE A PRESS RELEASE. | | | | *** UPDATE ON 4/21/99 @ 0418 BY HUNTER TO GOULD *** | | | | THE REACTOR IS IN OPCON 3 AT 350 PSIG CONTINUING TO COLD SHUTDOWN. | | CONDENSER VACUUM IS BEING REESTABLISHED IN ORDER TO RE-OPEN THE MSIVs AND | | SECURE HPCI FROM PRESSURE CONTROL MODE. FEEDWATER SYSTEM IS BEING | | REPRESSURIZED TO REESTABLISH NORMAL FEED AND SECURE RCIC FROM LEVEL CONTROL | | MODE. | | | | ALSO THE "1A" AND "1B" MG SET DRIVE MOTOR BREAKERS DID NOT TRIP DURING THE | | TRANSIENT SINCE PLANT LOADS WERE PREVIOUSLY TRANSFERRED BY A REACTOR | | OPERATOR PRIOR TO THE TURBINE TRIP. THE BREAKERS, THEREFORE, OPERATED AS | | DESIGNED. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | THE REG 1 RDO(SHANBAKY) WAS NOTIFIED. | | | | *** UPDATE ON 4/22/99 @ 0220 BY HUNTER TO GOULD *** | | | | THE UNIT IS IN COLD SHUTDOWN AS OF 2214 ON 4/21/99. RESOLUTION OF | | EQUIPMENT PROBLEMS WHICH RESULTED IN THE SHUTDOWN ARE IN PROGRESS. | | ACTIVITIES ARE ALSO IN PROGRESS FOR PLANT STARTUP. | | | | ALL CONTROL RODS INCLUDING 30-39 WENT FULL IN WITHIN THE REQUIRED TECHNICAL | | SPECIFICATION TIME. ROD 30-39 POSITION INDICATION WAS LOST FOR | | APPROXIMATELY TWO MINUTES AFTER THE SCRAM, THEN THE "00" FULL IN POSITION | | INDICATION BECAME AVAILABLE AND REMAINED AVAILABLE THROUGHOUT THE SHUTDOWN. | | | | THE RESIDENT INSPECTOR WILL BE INFORMED. THE REG 1 RDO(SHANBAKY) WAS | | INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35612 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MA DEPT OF PUBLIC HEALTH RCP |NOTIFICATION DATE: 04/21/1999| |LICENSEE: AEA TECHNOLOGIES QSA, INC |NOTIFICATION TIME: 15:00[EDT]| | CITY: BURLINGTON REGION: 1 |EVENT DATE: 04/21/1999| | COUNTY: STATE: MA |EVENT TIME: 14:00[EDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 04/21/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MOHAMED SHANBAKY R1 | | |FREDERICK COMBS NMSS | +------------------------------------------------+JOSEPH GIITTER IRO | | NRC NOTIFIED BY: KEN TRAEGDE |DONNA MARIE PEREZ IP | | HQ OPS OFFICER: DICK JOLLIFFE |LEN WERT R2 | +------------------------------------------------+DALE POWERS R4 | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - SHIPMENT OF 8 Ir-192 SOURCES (866 CURIES TOTAL) FROM BURLINGTON, MA, | | OVERDUE IN MEXICO - | | | | AT 1500 EDT ON 04/21/99, KEN TRAEGDE, MA DEPARTMENT OF PUBLIC HEALTH | | RADIATION CONTROL PROGRAM (RCP), BOSTON, MA, REPORTED THAT ON 04/16/99, AEA | | TECHNOLOGY QSA, INC, BURLINGTON, MA, SHIPPED A MODEL #855 SOURCE CHANGER | | LOADED WITH EIGHT Ir-192 SOURCES (TOTALING 866 CURIES) VIA FEDERAL EXPRESS | | TO VICONT SA DE CV, TALUCA, MEXICO. THE UNDAMAGED PACKAGE HAS A TRANSPORT | | INDEX OF 1.4 (NORMAL READINGS OF 1.4 MR/HR AT ONE METER AND 55 MR/HR AT THE | | SURFACE) AT THE TIME OF SHIPMENT. | | | | THE SHIPMENT WAS SCHEDULED TO ARRIVE IN MEXICO ON 04/17/99. AS OF 1400 EDT | | ON 04/21/99, THE RECEIVER HAD RECEIVED THE SHIPPING PAPERS BUT NOT THE | | CONTAINER. THE SHIPPER AND FEDERAL EXPRESS HAVE LAUNCHED A FULL SEARCH FOR | | THE PACKAGE. THE FEDEX HAZARDS MATERIAL INVESTIGATION TEAM HAS CONDUCTED A | | PHYSICAL SEARCH OF EXPRESS DEPOS IN BOSTON, MEMPHIS, LOS ANGELES, AND | | MEXICO. | | | | LICENSE NUMBERS ARE: SU-1485, 12-8361, 52-0243, 54-0237, 58-0242. | | | | CONTACT THE NRC OPERATIONS OFFICER FOR TELEPHONE NUMBERS. | | | | THE NRC OPERATIONS OFFICER NOTIFIED THE DOT NATIONAL RESPONSE CENTER | | (GAUTHIER), REPORT NUMBER 481132. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35613 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 04/21/1999| | UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 18:03[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/21/1999| +------------------------------------------------+EVENT TIME: 10:15[CDT]| | NRC NOTIFIED BY: KLAY KLIMPLE |LAST UPDATE DATE: 04/21/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DALE POWERS R4 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - FITNESS FOR DUTY REPORT - | | | | AT 1015 CDT ON 04/21/99, A PLANT EMPLOYEE WAS DETERMINED TO BE UNDER THE | | INFLUENCE OF ALCOHOL DURING A RANDOM TEST. THE EMPLOYEE'S ACCESS | | AUTHORIZATION TO THE PLANT HAS BEEN TERMINATED. REFER TO THE HOO LOG FOR | | ADDITIONAL DETAILS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35614 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 04/21/1999| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 22:16[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 04/21/1999| +------------------------------------------------+EVENT TIME: 21:17[EDT]| | NRC NOTIFIED BY: PHIL SANTINI |LAST UPDATE DATE: 04/21/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N Y 99 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - UNIT 2 OUTSIDE ITS PLANT DESIGN BASIS FOR 30 SECONDS DUE TO A FAILED | | TRANSFER SWITCH - | | | | DURING A SURVEILLANCE TEST, DC CONTROL POWER TRANSFER SWITCH #EDD-2 FAILED | | TO TRANSFER TO THE EMERGENCY POWER SUPPLY FOR 480-VOLT BUS 2A.. PLANT | | OPERATORS RESTORED DC CONTROL POWER TO 480-VOLT BUS 2A FROM ITS NORMAL POWER | | SUPPLY IN APPROXIMATELY 30 SECONDS. | | | | THIS LOSS OF DC CONTROL POWER TO 480-VOLT BUS 2A PLACED UNIT 2 OUTSIDE ITS | | PLANT DESIGN BASIS FOR 30 SECONDS. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35615 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 04/21/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 22:30[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 04/21/1999| +------------------------------------------------+EVENT TIME: 20:00[EDT]| | NRC NOTIFIED BY: DOUG PETERSON |LAST UPDATE DATE: 04/21/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 2 Startup |2 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - INADVERTENT TDAFW PUMP START DURING A MOVATS TEST - | | | | During the restoration of motor operated valve #MOV-3505A from Motor | | Operated Valve Analysis and Test System (MOVATS) test #M-64.1.2, the turbine | | driven auxiliary feedwater (TDAFW) pump inadvertently started. A system | | engineer standing near the TDAFW pump called the control room and reported | | that the pump was running. The control operator isolated the TDAFW system | | discharge to the steam generators with the discharge air operated valves, | | and the control room foreman directed the auxiliary operator to close the | | manual isolation valve which secured the steam to the TDAFW pump. | | | | This resulted in a 2�F cooldown of the reactor coolant system (RCS) during | | the approximate 1 minute run of the TDAFW pump. | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35616 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 04/21/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 23:19[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 04/21/1999| +------------------------------------------------+EVENT TIME: 20:25[EDT]| | NRC NOTIFIED BY: CURT WOLTON |LAST UPDATE DATE: 04/22/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MOHAMED SHANBAKY R1 | |10 CFR SECTION: | | |AMED 50.72(b)(2)(v) OFFSITE MEDICAL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - POTENTIALLY CONTAMINATED INDIVIDUAL TRANSPORTED TO OFFSITE MEDICAL | | FACILITY - | | | | AT 2025 ON 04/21/99, A WORKER RECEIVED AN INJURY TO HIS HAND. THE INJURY | | WAS SERIOUS ENOUGH THAT THE EMERGENCY MEDICAL TECHNICIAN AND HEALTH PHYSICS | | TECHNICIAN DID NOT REMOVE THE WORKERS GLOVE BEFORE TRANSPORTING HIM TO THE | | POTTSTOWN HOSPITAL FOR TREATMENT. THE HEALTH PHYSICS TECHNICIAN | | SUBSEQUENTLY DETERMINED THAT THE INDIVIDUAL WAS NOT CONTAMINATED. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35617 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 04/22/1999| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 03:00[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 04/22/1999| +------------------------------------------------+EVENT TIME: 01:31[CDT]| | NRC NOTIFIED BY: PFEFFER |LAST UPDATE DATE: 04/22/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MELVYN LEACH R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD A REACTOR SCRAM ON LOW REACTOR WATER LEVEL. | | | | THE PLANT HAD A REACTOR SCRAM FROM 100% POWER DUE TO A LOW REACTOR WATER | | LEVEL. CAUSE OF THE LOW REACTOR WASTER LEVEL IS UNKNOWN AND BEING | | INVESTIGATED. ALL RODS FULLY INSERTED, NO ECCS INJECTION OCCURRED, AND NO | | SAFETY RELIEF VALVES LIFTED. PLANT DID HAVE GROUP 2 AND GROUP 3 ISOLATIONS. | | THE GROUP 3 ISOLATION HAS BEEN RESET, AND PRESENTLY THEY ARE IN PROGRESS | | OF RESETTING THE GROUP 2 ISOLATION. THE MAIN CONDENSER IS THE HEAT SINK. | | | | THE RESIDENT INSPECTOR WILL BE INFORMED. | +------------------------------------------------------------------------------+
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