The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for April 15, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           04/14/1999 - 04/15/1999

                              ** EVENT NUMBERS **

35583  35591  35592  35593  35594  

!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35583       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: ARKANSAS NUCLEAR         REGION:  4  |NOTIFICATION DATE: 04/12/1999|
|    UNIT:  [1] [2] []                STATE:  AR |NOTIFICATION TIME: 16:59[EDT]|
|   RXTYPE: [1] B&W-L-LP,[2] CE                  |EVENT DATE:        04/12/1999|
+------------------------------------------------+EVENT TIME:        12:30[CDT]|
| NRC NOTIFIED BY:  REHM                         |LAST UPDATE DATE:  04/14/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA SMITH          R4      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE PLANT HAD AN AUTOMATIC ACTUATION OF THE UNITS 1 & 2 CONTROL ROOM         |
| EMERGENCY AIR RECIRCULATION FAN (VSF-9).                                     |
|                                                                              |
| THE ACTUATION OF VSF-9 WAS DUE TO EXCEEDING THE ACTUATION SETPOINT OF 154    |
| CPM FOR THE UNIT 1 CONTROL ROOM SUPPLY VENTILATION RAD MONITOR               |
| (2RITS-8001A).  THE EVOLUTION WHICH CAUSED THE BACKGROUND RADIATION LEVELS   |
| TO EXCEED THE RAD MONITOR SETPOINT WAS TRANSPORTING  A MULTI-ASSEMBLY SEALED |
| BASKET (MSB) CONTAINED IN THE MSB TRANSFER CASK (MTC) FROM THE SPENT FUEL    |
| POOL AREA (ELEVATION 404) TO THE RAILROAD BAY (ELEVATION 354).  PRIOR TO     |
| COMMENCING THIS EVOLUTION, THE CONTROL ROOM VENTILATION SUPPLY WAS ISOLATED  |
| AND IN RECIRCULATION MODE USING 2VSF-9 (UNIT 2 CONTROL ROOM EMERGENCY AIR    |
| RECIRCULATION FAN).  UNITS 1 AND 2 SHARE A COMMON VENTILATION SYSTEM.   THE  |
| 2RITS-8001A IS LOCATED OUTSIDE OF THE CONTROL ROOM, ADJACENT TO THE SPENT    |
| FUEL POOL AREA.  THE MOVEMENT OF THE MTC NEAR 2RITS-8001A RESULTED IN        |
| INCREASED BACKGROUND RADIATION LEVELS ABOVE THE RAD MONITOR ACTUATION        |
| SETPOINT.  HOWEVER, THERE WAS NO INCREASE IN THE CONTROL ROOM VENTILATION    |
| ACTIVITY LEVELS DUE TO THE CONTROL ROOM VENTILATION SYSTEM SUPPLY BEING      |
| ISOLATED.  FIVE MINUTES AFTER THE ACTUATION, THE RAD MONITOR INDICATED 300   |
| CPM.  THE MONITOR PRESENTLY INDICATES THE NORMAL INDICATION OF 90 CPM.  THE  |
| RVSF WAS SECURED 2 MINUTES AFTER THE ACTUATION OF VSF-9.                     |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED.                                         |
|                                                                              |
| *** UPDATE ON 4/14/99 @ 1401 BY SCHEIDE TO GOULD ***   RETRACTION            |
|                                                                              |
| THE LICENSEE IS RETRACTING THIS EVENT BASED ON GUIDANCE FROM NUREG 1022, REV |
| 1 WHICH LEADS TO THE CONCLUSION THAT THIS EVENT IS NOT REPORTABLE SINCE THE  |
| EVENT INVOLVED THE ACTUATION OF A SINGLE ESF COMPONENT, NOT A TRAIN OR       |
| SYSTEM, AND THE PURPOSE OF THE ACTUATION WAS NOT TO MITIGATE THE             |
| CONSEQUENCES OF AN ACCIDENT.                                                 |
|                                                                              |
| THE RESIDENT INSPECTOR WAS INFORMED.  THE  R4DO (LINDA SMITH) WAS NOTIFIED.  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35591       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: COOPER                   REGION:  4  |NOTIFICATION DATE: 04/14/1999|
|    UNIT:  [1] [] []                 STATE:  NE |NOTIFICATION TIME: 04:32[EDT]|
|   RXTYPE: [1] GE-4                             |EVENT DATE:        04/14/1999|
+------------------------------------------------+EVENT TIME:        01:28[CDT]|
| NRC NOTIFIED BY:  FRED SCHIZAS                 |LAST UPDATE DATE:  04/14/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA SMITH          R4      |
|10 CFR SECTION:                                 |                             |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION    |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - RCIC SYSTEM DECLARED INOPERABLE DUE TO FAILED SYSTEM COOLING VALVE DURING  |
| A TEST -                                                                     |
|                                                                              |
| AT 0128 CDT ON 04/14/99, THE LICENSEE DECLARED THE REACTOR CORE ISOLATION    |
| COOLING (RCIC) SYSTEM INOPERABLE DUE TO THE FAILURE OF THE RCIC SYSTEM       |
| COOLING VALVE, #RCIC-MO-132.  WHEN THE VALVE CONTROL SWITCH WAS PLACED IN    |
| THE CLOSE POSITION IN ORDER TO RECORD THE VALVE STROKE TIME DURING THE RCIC  |
| POWER OPERATED VALVE OPERABILITY SURVEILLANCE TEST, THE VALVE MOVED TO THE   |
| INTERMEDIATE POSITION AND STOPPED.  STATION OPERATORS VERIFIED THAT THE      |
| VALVE WAS NOT CLOSED AND ISOLATED THE RCIC SYSTEM STEAM SUPPLY AND SUCTION   |
| AND DISCHARGE PATHS IN ORDER TO PREVENT SYSTEM INITIATION, EVIDENCE          |
| PRESERVATION, AND EXCESSIVE CYCLING OF THE BAROMETRIC CONDENSER PUMP.        |
| STATION OPERATORS ALSO VERIFIED THAT THE HIGH PRESSURE COOLANT INJECTION     |
| SYSTEM WAS OPERABLE.                                                         |
|                                                                              |
| TECH SPEC LCO A/S 3.5.3.A REQUIRES THE LICENSE TO RESTORE THE RCIC SYSTEM TO |
| OPERABLE STATUS WITHIN 14 DAYS OR SHUT THE PLANT DOWN.                       |
|                                                                              |
| STATION OPERATORS ARE INVESTIGATING THE CAUSE OF THE VALVE FAILURE AND PLAN  |
| TO REPAIR THE VALVE.                                                         |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35592       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRAIDWOOD                REGION:  3  |NOTIFICATION DATE: 04/14/1999|
|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 06:50[EDT]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        04/14/1999|
+------------------------------------------------+EVENT TIME:        04:33[CDT]|
| NRC NOTIFIED BY:  PAT HABEL                    |LAST UPDATE DATE:  04/15/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |JOHN JACOBSON        R3      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     A/R        Y       85       Power Operation  |0        Hot Standby      |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - AUTO Rx TRIP FROM 85% POWER DUE TO MAIN GENERATOR FAULT FOR UNKNOWN        |
| REASONS -                                                                    |
|                                                                              |
| AT 0433 CDT ON 04/14/99, UNIT 2 AUTOMATICALLY TRIPPED FROM 85% POWER DUE TO  |
| A MAIN GENERATOR TRIP CAUSED BY A MAIN GENERATOR FAULT FOR UNKNOWN REASONS.  |
| ALL CONTROL RODS INSERTED COMPLETELY.  BOTH TRAINS OF THE AUXILIARY          |
| FEEDWATER SYSTEM ACTUATED TO RESTORE STEAM GENERATOR WATER LEVELS TO NORMAL. |
| NO SAFETY OR RELIEF VALVES LIFTED.  STEAM IS BEING DUMPED TO THE MAIN        |
| CONDENSER.  ALL SYSTEMS FUNCTIONED AS DESIGNED.                              |
|                                                                              |
| UNIT 2 IS STABLE IN MODE 3 (HOT STANDBY).  THE LICENSEE IS INVESTIGATING THE |
| CAUSE OF THE MAIN GENERATOR FAULT.                                           |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
|                                                                              |
| * * * UPDATE AT 0408 ON 04/15/99 BY JOLLIFFE * * *                           |
|                                                                              |
| THE AUTOMATIC REACTOR TRIP WAS CAUSED BY A PROBLEM WITH A MAIN GENERATOR GIX |
| GROUND FAULT RELAY.  THE LICENSEE HAS BYPASSED THE RELAY AND RESTARTED UNIT  |
| 2.  THE LICENSEE IS CONTINUING TO INVESTIGATE THE ROOT CAUSE OF THE REACTOR  |
| TRIP.                                                                        |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   35593       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  COGEMA MINING INC.                   |NOTIFICATION DATE: 04/14/1999|
|LICENSEE:  COGEMA MINING INC.                   |NOTIFICATION TIME: 12:43[EDT]|
|    CITY:                           REGION:  4  |EVENT DATE:        04/12/1999|
|  COUNTY:  CAMPBELL                  STATE:  WY |EVENT TIME:        14:00[MDT]|
|LICENSE#:  SUA-1341              AGREEMENT:  N  |LAST UPDATE DATE:  04/14/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |LINDA SMITH          R4      |
|                                                |TOM ANDREWS          R4      |
+------------------------------------------------+CHARLES MILLER       IRO     |
| NRC NOTIFIED BY:  VASELIN                      |KEVIN RAMSEY  EO     NMSS    |
|  HQ OPS OFFICER:  CHAUNCEY GOULD               |JOE STAMBAUGH        DOE     |
+------------------------------------------------+STORER               FEMA    |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NONR                     OTHER UNSPEC REQMNT    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| A WELLFIELD INJECTION SOLUTION SPILL OCCURRED IN MINE UNIT 6 OF THE          |
| CHRISTENSEN MINE IN CAMPBELL COUNTY, WY.                                     |
|                                                                              |
| THE SPILL, WHICH WAS ESTIMATED TO BE 32,400 GALLONS WITH A URANIUM           |
| CONCENTRATION OF 0.8mg/l, IS THE RESULT OF A CASING FAILURE ON INJECTION     |
| WELL 6V27-1.  THE SPILL WAS REPORTED SINCE IT IS GREATER THAN 10,000         |
| GALLONS, WHICH IS CONSIDERED SIGNIFICANT FROM AN OPERATIONS STANDPOINT.      |
|                                                                              |
| THE SOLUTION DOES NOT POSE A HEALTH OR ENVIRONMENTAL HAZARD DUE TO ITS LOW   |
| CONCENTRATION OF URANIUM.  HOWEVER, THE SPILL DID ENTER A NEARBY DRAW WHICH  |
| WAS FLOWING AT AN ESTIMATE 1-2 CFM WITH SNOW MELT.  THUS THE SOLUTION MIGHT  |
| HAVE LEFT THE NRC PERMITTED AREA IN A HIGHLY DILUTED STREAM.  LINCH, WY. ,   |
| 15 MILES TO THE SOUTHEAST, IS THE NEAREST COMMUNITY.                         |
|                                                                              |
| INJECTION WELL 6V27-1 WAS SHUT DOWN AND WILL NOT BE USED UNTIL THE WELL      |
| CASING CAN BE REPAIRED.  A SOIL SAMPLE HAS BEEN COLLECTED AT THE SPILL       |
| LOCATION AND WILL BE ANALYZED FOR Ra-226 TO DETERMINE IF SOIL CLEAN-UP IS    |
| NEEDED.                                                                      |
|                                                                              |
| HOO NOTE: SEE SIMILAR EVENTS #35524 AND #35542                               |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35594       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FT CALHOUN               REGION:  4  |NOTIFICATION DATE: 04/14/1999|
|    UNIT:  [1] [] []                 STATE:  NE |NOTIFICATION TIME: 18:40[EDT]|
|   RXTYPE: [1] CE                               |EVENT DATE:        04/14/1999|
+------------------------------------------------+EVENT TIME:        16:52[CDT]|
| NRC NOTIFIED BY:  CHRISTENSEN                  |LAST UPDATE DATE:  04/14/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |LINDA SMITH          R4      |
|10 CFR SECTION:                                 |                             |
|APRE 50.72(b)(2)(vi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE LICENSEE NOTIFIED THE NEBRASKA STATE ENVIRONMENTAL AGENCY THAT THEY      |
| EXCEEDED THEIR NPDES DISCHARGE LIMITS FOR HYDRAZINE.                         |
|                                                                              |
| THE HYDRAZINE DISCHARGE AT OUTFALL 001 (CIRCULATING WATER DISCHARGE) WAS IN  |
| EXCESS OF THEIR NPDES (NATIONAL POLLUTANT DISCHARGE ELIMINATION SYSTEM)      |
| DISCHARGE LIMIT OF 2 PPB.  THE MEASURED DISCHARGE RATE AT THE OUTFALL WAS 3  |
| PPB, BUT THERE WAS NO NET INCREASE IN HYDRAZINE DISCHARGE CONCENTRATION FROM |
| THE SITE SINCE UPSTREAM RIVER CONCENTRATION IS ALSO 3 PPB.                   |
|                                                                              |
| THE RESIDENT INSPECTOR WAS NOTIFIED.                                         |
|                                                                              |
| HOO NOTE:  SEE SIMILAR EVENTS #35524 AND #35542.                             |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021