Event Notification Report for April 13, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/12/1999 - 04/13/1999 ** EVENT NUMBERS ** 35576 35577 35578 35579 35580 35581 35582 35583 35584 35585 35586 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35576 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 04/12/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 07:46[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 04/12/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 01:15[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 04/12/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |BRUCE BURGESS R3 | | DOCKET: 0707002 |FRED COMBS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: J. B. HALCOMB | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VALID ACTUATION OF A 'Q' SAFETY SYSTEM - 24 HOUR REPORT | | | | "At 0115 hrs, on 04/12/99, Operations Personnel in the X-344 facility, | | received a steam shutdown alarm on Autoclave #2 during a cylinder heating | | (Mode II). The steam shutdown was caused by the actuation of the High | | Condensate Level Shutoff System ('Q' system). Investigation of the alarm | | and completion of 'as found' testing gave indication that the alarm was | | caused by an actual high condensate level condition, which cleared after the | | steam shutdown occurred. The cylinder in this autoclave was disconnected and | | the autoclave was declared 'inoperable' by the Plant Shift Superintendent. | | Testing of the High Condensate Level Shutoff System will be performed by | | Maintenance and Engineering personnel. Autoclave #2 will remain | | out-of-service pending an Engineering Evaluation and Resolution of the alarm | | condition." | | | | Portsmouth personnel notified the NRC Resident Inspector and the onsite DOE | | representative. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35577 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: PAYNE FIRM |NOTIFICATION DATE: 04/12/1999| |LICENSEE: ARVAN INDUSTRIES |NOTIFICATION TIME: 10:05[EDT]| | CITY: GREENWOOD REGION: 3 |EVENT DATE: 04/09/1999| | COUNTY: STATE: IN |EVENT TIME: [CST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 04/12/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN JACOBSON R3 | | |FRED COMBS NMSS | +------------------------------------------------+ROSEMARY HOGAN IRO | | NRC NOTIFIED BY: DAN WOODY | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RADIATION DEVICE CONTAINING 1 CURIE OF AMERICIUM POSSIBLY STOLEN | | | | Arvan Industries of Greenwood, Indiana contacted the Payne Firm (Dan Woody | | acting as representative) late Friday, 4/9/99, for consultation concerning a | | radiation device containing 1 Ci of Am-241 that is believed stolen. The | | device is missing from the Arvan Exhaust Greenwood Facility located at 101 | | Center St., Greenwood, Indiana during ongoing closure activities. The | | device weighs about 200 pounds, contains a sealed source of 1 Ci of Am-241, | | and was used to measure the thickness of rolled steel. The device, an Xact | | Ray Thickness Gauge 3500 Model, serial #48761-1 and source serial #2786LX | | was manufactured by the Loral Control Systems of Archbald, Pennsylvania. | | The manufacturer is no longer in business. | | | | There is an ongoing investigation and a written report will be submitted | | later. | | | | The police have not been contacted at this time. It will probably be | | reported to the Greenwood, Indiana police of possibly the Indian Highway | | police. | | | | NRC HOO notified Mr John Ruyack of the Indiana Dept of Radiation Protection | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35578 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 04/12/1999| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 11:48[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 04/12/1999| +------------------------------------------------+EVENT TIME: 10:15[EDT]| | NRC NOTIFIED BY: COLEMAN |LAST UPDATE DATE: 04/12/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WALTER RODGERS R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SCRAM PILOT AIR HEADER INADVERTENTLY ISOLATED WHICH RESULTED IN A REACTOR | | SCRAM. NO CONTROL ROD MOVEMENT BECAUSE ALL CONTROL RODS WERE ALREADY FULLY | | INSERTED. | | | | The licensee received a full Reactor Protection System actuation from Scram | | Discharge Volume High Water Level. No control rod movement due to the fact | | that all the control rods were already fully inserted into the core. The | | licensee was performing a clearance to perform work on an air valve | | associated with the Main Steam Isolation Valves. The Scram Pilot air header | | was inadvertently isolated when the air line going to the Main Steam | | Isolation Valves was isolated. | | | | The work involved a valve on the air supply line to the outboard MSIVs. The | | P&ID was inadequate because it was not evident that the isolation valve used | | also isolated the scram pilot air header. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35579 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 04/12/1999| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 15:10[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 04/12/1999| +------------------------------------------------+EVENT TIME: 14:00[CDT]| | NRC NOTIFIED BY: PEDERSON |LAST UPDATE DATE: 04/12/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN JACOBSON R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT DECLARED HPCI INOPERABLE DUE TO THE LOSS OF THE EMERGENCY SERVICE | | WATER TO ONE OF TWO VENTILATION UNITS. | | | | THE EMERGENCY SERVICE WATER WAS LOST AS A RESULT OF THE FAILURE OF #13 | | EMERGENCY SERVICE WATER PUMP TO START, WHICH PUT HPCI OUT OF SERVICE AND | | THE PLANT IN A 24 HR TO SHUTDOWN LCO ACTION STATEMENT. WHEN THEY ATTEMPTED | | TO START #13 EMERGENCY SERVICE WATER PUMP, THE MOTOR WOULD HUM BUT THE | | IMPELLER WOULD NOT TURN AND THAT RESULTED IN THE TRIP OF THE PUMP BREAKER. | | THEY MANUALLY TRIED TO TURN THE IMPELLER , WHICH SEEMED STUCK INITIALLY, BUT | | THEY FINALLY GOT IT TO TURN FREELY. THERE MAY HAVE BEEN SOME TYPE OF | | DEBRIS THAT WAS CAUSING THE IMPELLER NOT TO TURN. CURRENTLY THEY ARE | | PERFORMING OPERABILITY CHECKS ON THE PUMP SO THAT THE LCO CAN BE EXITED. | | DURING THIS EVENT THE NORMAL SERVICE WATER WAS AVAILABLE. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | *** UPDATE ON 4/12/99 @ 1618 BY PEDERSON TO GOULD *** | | | | HPCI OPERABLE AFTER RESTORATION OF THE #13 EMERGENCY SERVICE WATER SYSTEM. | | LCO EXITED AT 1507 CDT. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | REG 3 RDO(JACOBSON) WAS INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35580 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: COOPER ENERGY SERVICES |NOTIFICATION DATE: 04/12/1999| |LICENSEE: COOPER ENERGY SERVICES |NOTIFICATION TIME: 15:55[EDT]| | CITY: GROVE CITY REGION: 1 |EVENT DATE: 04/12/1999| | COUNTY: STATE: PA |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 04/12/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAN HOLODY R1 | | |WALTER RODGERS R2 | +------------------------------------------------+JOHN JACOBSON R3 | | NRC NOTIFIED BY: BILLIG (FAX) |LINDA SMITH R4 | | HQ OPS OFFICER: CHAUNCEY GOULD |VERN HODGE NRR | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THIS PART 21 IS CONCERNED WITH A POTENTIAL DEFECT IN A COMPONENT ON THE | | DSRV-16-4 ENTERPRISE DIESEL GENERATOR SYSTEM. THE POTENTIAL PROBLEM IS WITH | | A CONNECTING ROD ASSEMBLIES BUILT SINCE SEPT 1986 THAT USE OR HAVE BEEN | | CONVERTED TO USE PRESTRESSED FASTENERS TO ATTACH THE ROD BOX TO THE MASTER | | ROD. THESE NEW ROD ASSEMBLIES (P/N 1A-7802) COME ASSEMBLED WITH PRESTRESSED | | FASTENERS THAT ARE SUSPECTED TO BE OF INCORRECT LENGTH. THE PLANTS INVOLVED | | ARE VOGTLE (ENGINE S/N 76021-4) AND PERRY (ENGINE S/N 75051-2). | | | | IN ADDITION, UTILITIES WITH DSRV-4 ENGINES WHO HAVE PURCHASED REPLACEMENT | | P/N 1A-6280 OR 1A-6281 CONNECTING ROD ASSEMBLIES (WITH BOLTS) SINCE SEPT., | | 1986 AND HAVE SUBSEQUENTLY CONVERTED THESE TO PRESTRESSED FASTENERS (OR | | PLANNING TO CONVERT) COULD ALSO BE AFFECTED. THE FOLLOWING SITES MAY BE | | AFFECTED GRAND GULF (ENGINE S/N 74033-6), HARRIS (ENGINE S/N 74046-9), | | CATAWBA (ENGINE S/N 75017-20), PERRY (ENGINE S/N 75051-4), COMANCHE PEAK | | (76001-4), AND VOGTLE (ENGINE S/N 76021-4). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35581 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CRYSTAL RIVER REGION: 2 |NOTIFICATION DATE: 04/12/1999| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 16:12[EDT]| | RXTYPE: [3] B&W-L-LP |EVENT DATE: 04/12/1999| +------------------------------------------------+EVENT TIME: 13:48[EDT]| | NRC NOTIFIED BY: SIMON |LAST UPDATE DATE: 04/12/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WALTER RODGERS R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | KEMPS RIDLEY SEA TURTLE FOUND ALIVE AT THE PLANT'S INTAKE AREA. | | | | THE TURTLE WAS TRANSPORTED TO THE MARICULTURE CENTER FOR OVERNIGHT | | OBSERVATION. FLORIDA DEPARTMENT OF ENVIRONMENT HAS BEEN NOTIFIED. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35582 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 04/12/1999| | UNIT: [] [2] [] STATE: TN |NOTIFICATION TIME: 16:45[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/12/1999| +------------------------------------------------+EVENT TIME: 15:48[EDT]| | NRC NOTIFIED BY: HARRIS |LAST UPDATE DATE: 04/12/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |WALTER RODGERS R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 65 Power Operation |65 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TWO CONTAINMENT ISOLATION VALVES ON SAME PENETRATION DECLARED INOPERABLE | | PLACING PLANT IN 3.0.3 LCO ACTION STATEMENT. | | | | THE INBOARD AND OUTBOARD CONTAINMENT ISOLATION VALVES ON THE GLYCOL SYSTEM | | WERE DECLARED INOPERABLE. THIS CONDITION OCCURRED DURING A TAGGING ACTIVITY | | FOR MAINTENANCE. IT WAS NOTICED THAT THE RED AND GREEN LIGHTS FOR THESE | | VALVES WERE BOTH ON. ENTERING 3.0.3 GIVES THEM ONE HOUR TO REPAIR AND 6 | | HOURS TO BE IN HOT S/B. THEY ARE CURRENTLY TROUBLESHOOTING AND COMMENCING | | REPAIR. THEY ONLY NEED TO RETURN ONE OF THE VALVES TO OPERABLE CONDITION SO | | THAT IT CAN BE ISOLATED WOULD ALLOW THEM TO EXIT 3.0.3. THE BASIS FOR BEING | | OUTSIDE THE DESIGN BASIS IS THAT THEY HAVE A PENETRATION WHICH CAN NOT BE | | ISOLATED. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED. | | | | *** UPDATE ON 4/12/99 @ 1756 BY SIMONS TO GOULD *** RETRACTION | | | | THE LICENSEE SUCCESSFULLY COMPLETED A VALVE STROKE TEST ON ONE VALVE AFTER | | COMPLETION OF THE ADJUSTMENT OF THE VALVE LIMIT SWITCH. THE VALVE WAS | | DECLARED OPERABLE AND THEN ISOLATED WITH POWER REMOVED. BASED ON THESE | | FACTS UNIT 2 WAS NEVER OUTSIDE DESIGN BASIS. UPON FURTHER REVIEW, ENTRY IN | | 3.0.3 WAS NOT REQUIRED, LCO 3.6.1.1 WAS THE CORRECT TS THEY SHOULD HAVE | | ENTERED. THE LICENSEE IS THEREFORE RETRACTING THIS EVENT. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | THE REG 2 RDO(RODGERS) WAS INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35583 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ARKANSAS NUCLEAR REGION: 4 |NOTIFICATION DATE: 04/12/1999| | UNIT: [1] [2] [] STATE: AR |NOTIFICATION TIME: 16:59[EDT]| | RXTYPE: [1] B&W-L-LP,[2] CE |EVENT DATE: 04/12/1999| +------------------------------------------------+EVENT TIME: 12:30[CDT]| | NRC NOTIFIED BY: REHM |LAST UPDATE DATE: 04/12/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA SMITH R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD AN AUTOMATIC ACTUATION OF THE UNITS 1 & 2 CONTROL ROOM | | EMERGENCY AIR RECIRCULATION FAN (VSF-9). | | | | THE ACTUATION OF VSF-9 WAS DUE TO EXCEEDING THE ACTUATION SETPOINT OF 154 | | CPM FOR THE UNIT 1 CONTROL ROOM SUPPLY VENTILATION RADIATION MONITOR | | (2RITS-8001A). THE EVOLUTION WHICH CAUSED THE BACKGROUND RADIATION LEVELS | | TO EXCEED THE RADIATION MONITOR SETPOINT WAS TRANSPORTING A MULTI-ASSEMBLY | | SEALED BASKET (MSB) CONTAINED IN THE MSB TRANSFER CASK (MTC) FROM THE SPENT | | FUEL POOL AREA (ELEV 404) TO THE RAILROAD BAY (ELEV 354). PRIOR TO | | COMMENCING THIS EVOLUTION, THE CONTROL ROOM VENTILATION SUPPLY WAS ISOLATED | | AND IN RECIRCULATION MODE USING 2VSF-9 (UNIT 2 CONTROL ROOM EMERGENCY AIR | | RECIRCULATION FAN). UNITS 1 AND 2 SHARE A COMMON VENTILATION SYSTEM. THE | | 2RITS-8001A IS LOCATED OUTSIDE OF THE CONTROL ROOM, ADJACENT TO THE SPENT | | FUEL POOL AREA. THE MOVEMENT OF THE MTC NEAR 2RITS-8001A RESULTED IN | | INCREASED BACKGROUND RADIATION LEVELS ABOVE THE RADIATION MONITOR ACTUATION | | SETPOINT. HOWEVER, THERE WAS NO INCREASE IN THE CONTROL ROOM VENTILATION | | ACTIVITY LEVELS DUE TO THE CONTROL ROOM VENTILATION SYSTEM SUPPLY BEING | | ISOLATED. FIVE MINUTES FOLLOWING THE ACTUATION, THE RADIATION MONITOR | | INDICATED 300 CPM. THE MONITOR PRESENTLY INDICATES THE NORMAL INDICATION OF | | 90 CPM. THE RVSF WAS SECURED 2 MINUTES FOLLOWING THE ACTUATION OF VSF-9. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35584 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 04/12/1999| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 17:26[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 04/12/1999| +------------------------------------------------+EVENT TIME: 17:00[EDT]| | NRC NOTIFIED BY: FALLACARA |LAST UPDATE DATE: 04/12/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAN HOLODY R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 80 Power Operation |80 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MOTOR CONTROL CENTER (MCC) ENCLOSURE BLOWOUT PANELS OBSTRUCTED. | | | | DURING A PLANT WALKDOWN, IT WAS DISCOVERED THAT THE MCC ENCLOSURE BLOWOUT | | PANELS WERE OBSTRUCTED BY STEEL CHANNELS ON D8/D9 AND THE D7 SEEMED TO BE | | STUCK. THE ENCLOSURES WERE DEGRADED, BUT STILL OPERABLE UNDER CURRENT | | WEATHER CONDITIONS. | | THEY WILL REMOVE ANY OBSTRUCTIONS TO THESE BLOWOUT PANELS. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35585 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 04/12/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 19:48[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 04/12/1999| +------------------------------------------------+EVENT TIME: 16:00[EDT]| | NRC NOTIFIED BY: MICKLOW |LAST UPDATE DATE: 04/12/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAN HOLODY R1 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE DETERMINED THAT THE CHEVRON MOISTURE SEPARATORS WERE INSTALLED | | BACKWARDS. | | | | THIS CONDITION WAS DISCOVERED DURING MAINTENANCE OF THE CONTAINMENT | | RECIRCULATING FAN COOLERS. THE CHEVRON MOISTURE SEPARATORS EFFECTIVENESS IN | | REMOVING MOISTURE IN THIS CONDITION IS UNANALYZED, AND MAY DEGRADE THE | | CAPABILITY OF ALL 4 CONTAINMENT RECIRC FAN UNITS. THE UNITS ARE NOT | | REQUIRED IN THE PRESENT MODE. IT HAS NOT YET BEEN DETERMINED HOW LONG THE | | SEPARATORS HAVE BEEN INSTALLED BACKWARDS, BUT THEY ARE INVESTIGATING. | | | | THE RESIDENT INSPECTOR WILL BE INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35586 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 04/13/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 05:55[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/13/1999| +------------------------------------------------+EVENT TIME: 04:27[EDT]| | NRC NOTIFIED BY: CHRIS HYNES |LAST UPDATE DATE: 04/13/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAN HOLODY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R N 0 Hot Standby |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO ROD CONTROL URGENT FAILURE ALARM | | | | During a planned plant shutdown, with the reactor already subcritical, | | control bank 'A' group 2 did not move as rods were being inserted. As a | | result, the rod control system received an "Urgent Alarm" which inhibited | | manual control rod motion. The licensee performed a manual trip and all | | rods fully inserted. The problem is being investigated. | | | | Heat removal was and is by steam dump to the main condenser with feedwater | | from the main feedwater system. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021