Event Notification Report for March 25, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/24/1999 - 03/25/1999 ** EVENT NUMBERS ** 35434 35464 35468 35501 35503 35504 35505 35506 35507 35508 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35434 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 03/02/1999| | UNIT: [] [2] [] STATE: WI |NOTIFICATION TIME: 18:21[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 03/02/1999| +------------------------------------------------+EVENT TIME: 16:45[CST]| | NRC NOTIFIED BY: SHORT |LAST UPDATE DATE: 03/24/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JAMES CREED R3 | |10 CFR SECTION: | | |ADEG 50.72(b)(1)(ii) DEGRAD COND DURING OP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 1 Startup |1 Startup | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUXILIARY FEEDWATER LEAKING BACK INTO MAIN FEEDWATER SYSTEM | | | | THE LICENSEE DISCOVERED THAT THE AUXILIARY FEEDWATER SYSTEM WAS LEAKING BACK | | INTO THE MAIN FEED SYSTEM ("B" FEED LINE) PAST TWO IN-SERIES CHECK VALVES. | | THESE CHECK VALVES ARE CONSIDERED CONTAINMENT ISOLATION VALVES. LEAKAGE IS | | IN EXCESS OF THEIR ALLOWABLE LIMITS. AUXILIARY FEEDWATER IS CURRENTLY | | FEEDING THE STEAM GENERATORS. THE LEAKAGE HAS BEEN ISOLATED USING MANUAL | | VALVES. THE UNIT WAS IN STARTUP FOLLOWING A REFUELING OUTAGE WHEN THE | | CONDITION WAS FOUND. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED. | | | | | | ***RETRACTION ON 03/24/99 AT 1132ET BY RANDY HASTINGS TAKEN BY MACKINNON*** | | | | Subsequent evaluation has clarified that only one of the series check valves | | performs a containment isolation function, 2CS-476AA (Reference PBNP FSAR | | Figure 5.2-3). The main steam and feed water system are considered a closed | | system inside containment and the piping is part of the containment | | boundary. That boundary remained intact during this event. Accordingly, | | the integrity of the containment boundary was never in question and this | | condition did not result in a principal safety barrier being seriously | | degraded. | | | | An engineering evaluation has also been completed to assess whether the | | leakage observed past these check valves would have resulted in less than | | the required auxiliary feed water flow to be available for decay heat | | removal. This evaluation concluded that even with check valve leakage in | | excess of that observed during this event, the auxiliary feed water system | | was capable of providing sufficient flow to the steam generators to meet the | | design basis for decay heat removal. R3DO (Pat Hiland) notified. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35464 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 03/12/1999| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 15:08[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 03/12/1999| +------------------------------------------------+EVENT TIME: 13:14[CST]| | NRC NOTIFIED BY: PHIL SHORT |LAST UPDATE DATE: 03/24/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 73 Power Operation |73 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - AUXILIARY FEEDWATER SYSTEM FOR BOTH UNITS INOPERABLE FOR 4 MINUTES - | | | | UNIT 1 IS OPERATING AT 100% POWER, AND UNIT 2 IS OPERATING AT 73% POWER. | | | | ON 03/12/99, DURING AN ENGINEERING EVALUATION, LICENSEE ENGINEERING | | DEPARTMENT PERSONNEL DETERMINED THAT THE UNIT 2 TURBINE-DRIVEN (TD) | | AUXILIARY FEEDWATER (AFW) | | PUMP FLOW RATE HAD BEEN SET INCORRECTLY DURING A PREVIOUSLY PERFORMED TEST. | | LICENSEE PERSONNEL DETERMINED THAT THIS CONDITION AFFECTED THE ENTIRE AFW | | SYSTEM. (PORTIONS OF THE AFW SYSTEM ARE SHARED BY BOTH UNITS.) | | | | AT 1314 CST ON 03/12/99, THE LICENSEE ADMINISTRATIVELY DECLARED THE UNIT 1 | | TD AFW PUMP, THE UNIT 2 TD AFW PUMP, AND THE TWO SHARED MOTOR-DRIVEN (MD) | | AFW PUMPS INOPERABLE (AND THUS, THE ENTIRE AFW SYSTEM) AND ENTERED TECHNICAL | | SPECIFICATION LIMITING CONDITION FOR OPERATION ACTION STATEMENT 15.3.0.B | | (a.k.a. 3.0.3). ALL FOUR AFW PUMPS REMAINED FUNCTIONAL. THIS CONDITION IS | | CONSIDERED TO BE OUTSIDE THE DESIGN BASES OF THE PLANT. | | | | AT 1318 CST ON 03/12/99, THE LICENSEE TRIPPED THE UNIT 2 TD AFW PUMP AND | | DECLARED IT INOPERABLE, ENTERED TECH SPEC LCO A/S 15.3.4.C.1 (72 HOUR | | SHUTDOWN LCO), DECLARED THE OTHER THREE AFW PUMPS OPERABLE, AND EXITED TECH | | SPEC LCO A/S 15.3.0.B. THUS, ONLY THE UNIT 2 PORTION OF THE AFW SYSTEM IS | | INOPERABLE. | | | | THE LICENSEE IS DETERMINING CORRECTIVE ACTIONS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | | | ***RETRACTION ON 03/24/99 AT 1128ET BY RANDY HASTINGS TAKEN BY MACKINNON*** | | | | An engineering evaluation has subsequently been completed to assess whether | | the error in adjustment of the 2P-29 discharge throttle valves, which could | | have accelerated the drain down of supply water to the AFW pumps in the | | event of an external event induced break in the AFW suction line from the | | condensate storage tanks, could have resulted in the AFW pumps being | | inoperable once the pumps were switched to the alternate source of water | | (service water). This evaluation concludes that the postulated air | | entrainment mechanism does not result in operation of the AFW pumps outside | | their design basis before, during or after the pump's suctions are switched | | to service water. Accordingly, it was not necessary to declare the AFW | | system out of service and this condition was not reportable pursuant to 10 | | CFR 50.72. R3DO (Pat Hiland) notified. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35468 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 03/12/1999| | UNIT: [] [] [3] STATE: CT |NOTIFICATION TIME: 17:39[EST]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 03/12/1999| +------------------------------------------------+EVENT TIME: 17:31[EST]| | NRC NOTIFIED BY: JOE RUTTAR |LAST UPDATE DATE: 03/24/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | -Control room personnel access door latch mechanism may not withstand HELB | | pressure in the turbine building- | | | | A licensee preliminary review of an error in an analysis assumption for the | | pressure applied to a control room personnel access door (#C-49-1) due to a | | high energy line break (HELB) in the turbine building indicates that the | | door latch mechanism might not withstand the applied pressure. | | | | The control room door has been latched with an alternative latching | | mechanism and will remain closed against this pressure so there are no | | current operability concerns. | | | | This situation results in a historical condition where Unit 3 may have | | operated outside its design basis. Engineering evaluation is continuing. A | | conservative decision has been made to report this condition as a condition | | outside the design basis of Unit 3 pursuant to 10CFR50.72(b)(1)(ii)(B) | | pending the results of this evaluation. | | | | The Licensee informed the NRC Resident Inspector. | | | | * * * UPDATE at 1237 on 03/24/99 by DALE BRODSKY to JOLLIFFE * * * | | | | A mockup test of the door latch and hinges was conducted on 03/19/99 at the | | door manufacturer's facility. This test determined that the door hinges and | | latch will withstand a total pressure in excess of that resulting from a | | HELB in the turbine building. Additionally, the pressure on this door will | | actually be less than the pressure in the turbine building due to its remote | | location and tortuous path. | | | | Therefore, this condition is not reportable to the NRC pursuant to | | 10CFR50.72(b)(1)(ii)(B) as a condition outside the design basis of Unit 3 | | and thus, the Licensee desires to retract this event. | | | | The Licensee informed the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R1DO Jack McFadden. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35501 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 03/23/1999| |LICENSEE: J & M TESTING, INC |NOTIFICATION TIME: 13:01[EST]| | CITY: CHIPLEY REGION: 2 |EVENT DATE: 03/10/1999| | COUNTY: STATE: FL |EVENT TIME: 14:15[EST]| |LICENSE#: 1763-1 AGREEMENT: Y |LAST UPDATE DATE: 03/24/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MARK LESSER R2 | | |DON COOL, NMSS EO | +------------------------------------------------+ | | NRC NOTIFIED BY: CHARLES ADAMS | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - AGREEMENT STATE REPORT - TWO LOST PORTABLE NUCLEAR SOIL MOISTURE DENSITY | | GAUGES - | | | | At 1415 on 03/10/99, during a Florida state inspection of J & M Testing, | | Inc., two portable nuclear soil moisture density gauges were determined to | | be missing. These are old gauges that were not being used and were last | | seen during an inventory taken on 12/28/98. The Chipley, FL police | | department has been notified. | | | | Specifications of the gauges are as follows: | | 1. Manufacturer: CPN, Model: BRC (1977); Serial No C7304NE147; Isotopes: 8 | | mCi Cs-137; 50 mCi Am-241/Be | | 2. Manufacturer: CPN, Model: BRC (1974); Serial No C7404NE50; Isotopes: 8 | | mCi Cs-137; 50 mCi Am-241/Be | | | | Charles Adams, FL Bureau of Radiation Control, notified NRC Region 2 (FL | | Radiological Incident No. FL99-07). | | | | ******************** UPDATE AT 0745 ON 03/24/99 FROM CHARLES ADAMS TO | | TROCINE ******************** | | | | The State of Florida Bureau of Radiation Control called to correct the FL | | Radiological Incident No. The number should have been FL99-037. | | | | The NRC operations officer notified the R2DO (Lesser) and NMSS EO (Cool). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35503 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 03/24/1999| | UNIT: [3] [] [] STATE: LA |NOTIFICATION TIME: 10:50[EST]| | RXTYPE: [3] CE |EVENT DATE: 03/24/1999| +------------------------------------------------+EVENT TIME: 00:00[CST]| | NRC NOTIFIED BY: GREGORY SCOTT |LAST UPDATE DATE: 03/24/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | Discovery of false information provided by a contract employee granted | | access to the site. | | Immediate compensatory measures taken upon discovery. | | | | The licensee notified the NRC Resident Inspector. | | | | Call HOO for more information. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35504 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 03/24/1999| | UNIT: [1] [2] [3] STATE: SC |NOTIFICATION TIME: 17:37[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 03/24/1999| +------------------------------------------------+EVENT TIME: 13:00[EST]| | NRC NOTIFIED BY: THERESA MELTER |LAST UPDATE DATE: 03/24/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK LESSER R2 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 99 Power Operation |99 Power Operation | |2 N Y 99 Power Operation |99 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT SECURITY REPORT - | | | | PLANT SECURITY COMPUTER SYSTEM DEGRADATION. COMPENSATORY MEASURES | | IMMEDIATELY TAKEN UPON DISCOVERY. REFER TO THE HOO LOG FOR ADDITIONAL | | DETAILS. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35505 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 03/24/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 22:12[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 03/24/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 13:26[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/24/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |PATRICK HILAND R3 | | DOCKET: 0707001 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: KEVIN BEASLEY | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Power to C-746-Q Building Criticality Accident Alarm System lost when a | | bird contacted an overhead electrical line - | | | | At 1326 CST on 03/24/99, air circuit breaker #23B5B tripped due to a bird | | contacting an energized portion of the overhead electrical line. As a | | result of this breaker tripping, power was lost to the C-746-Q Building | | Criticality Accident Alarm (CAA) System beacons. CAA System audibility for | | the C-746-Q Building was lost,. However, the breaker tripping did not | | affect the detectability of the CAA System. Power to the C-746-Q Building | | was restored and the CAA System was declared operable at 1337 CST. | | | | The inaudibility of the CAA Systems is reportable as a 24-hour event report | | per 10CFR76.120(c)(2). (Paducah Problem Report No ATR-99-1691; Paducah | | Event Report No PAD-1999-022). | | | | The NRC Resident Inspector has been notified of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35506 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 03/25/1999| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 00:18[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 03/24/1999| +------------------------------------------------+EVENT TIME: 21:00[CST]| | NRC NOTIFIED BY: DAVID H. HANKS |LAST UPDATE DATE: 03/25/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CHARLES CAIN R4 | |10 CFR SECTION: | | |AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | High Pressure Core Spray (HPCS) Division 3 Diesel Generator declared | | inoperable. | | | | | | HPCS (Division 3) EDG oil level was discovered to be out of specification | | low during normal rounds. The Division 3 EDG was conservatively declared | | inoperable until further evaluations can be performed to determine final | | disposition of oil leakage from its inspection cover. The licensee entered | | Technical Specification 3.8.1 (72 hour limiting conditioning of operation). | | All Emergency Core Cooling systems including HPCS are fully operable. | | Earlier in the day an undervoltage spike on the electrical grid caused the | | Division 3 EDG to start. The diesel was properly secured. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35507 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 03/25/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 01:36[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 03/24/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 19:00[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/25/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |PATRICK HILAND R3 | | DOCKET: 0707002 |ROBERT PIERSON NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ERIC SPAETH | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | | |OCBC 76.120(c)(2)(iii) REDUNDANT EQUIP INOP | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TSR allowed one of two smoke detectors to be inoperable during withdrawal | | operations when both smoke detectors have to be operable during withdrawal | | operations. | | | | On March 10, 1999, Operations personnel identified a deficiency in a TSR | | requirement for the Pigtail line Isolation System at ERP (extended range | | product), LAW (low assay withdrawal), and TAILS, (TSR 2.5.3.4). The TSR | | required action allowed continued withdrawal operations if one (1) smoke | | detector was inoperable. The Pigtail Line Isolation System requires two (2) | | Pyrotronics Smoke Detectors to actuate for the isolation valve to close. | | Operation personnel initiated a Compensatory Action (CA-99-009) for this | | anomaly to isolate the withdrawal cylinder and manifold per TSR 2.5.3.4b if | | one smoke detector is declared inoperable. | | | | Initially there was no evidence that the Pigtail Line Isolation System had | | been allowed to operate any applicable mode (modes II or III) with one or | | more inoperable smoke head. As a follow up investigation to this | | deficiency, a search of the BPS system (problem report database) was | | conducted. This search identified that on July 8, 1998, a Pyrotronic smoke | | head at the Law IA withdrawal position had been declared inoperable and | | cylinder filling operations had been allowed to continue. | | | | This event is reportable due to a Safety System required by the TSR not | | being available or operable and no redundant equipment was available to | | perform the required safety function. | | | | The NRC Resident Inspector was notified of this event by the certificate | | holder. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35508 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 03/25/1999| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 02:34[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/25/1999| +------------------------------------------------+EVENT TIME: 01:30[EST]| | NRC NOTIFIED BY: GRANT FERNSLER |LAST UPDATE DATE: 03/25/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JACK MCFADDEN R1 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOCAL LEAK RATE TEST PERFORMED ON THE "A" LOOP FEEDWATER CONTAINMENT | | PENETRATION FAILED. | | | | | | An Appendix "J" Local Leak Rate Test was performed on the "A" Loop | | Feedwater containment penetration. The penetration piping was unable to be | | pressurized and therefore the leakrate exceeded Tech Spec limits. The | | penetration is isolated and the condition does not represent an immediate | | threat to the public health or safety. | | | | The NRC Resident Inspector will notified of this event by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021