The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for March 15, 1999

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           03/12/1999 - 03/15/1999

                              ** EVENT NUMBERS **

35387  35461  35462  35463  35464  35465  35466  35467  35468  35469  35470  35471 


!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!
+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   35387       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 02/20/1999|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 08:44[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        02/19/1999|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        10:05[CST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  03/12/1999|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |MIKE JORDAN          R3      |
|  DOCKET:  0707001                              |CHARLEY HAUGHNEY     NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  K. A. BEASLEY                |                             |
|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|NCFR                     NON CFR REPORT REQMNT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| WATER INVENTORY CONTROL SYSTEM ACTIVATION                                    |
|                                                                              |
| A water inventory control system (WICS) activation occurred on C-360         |
| position 4 autoclave on February 19, 1999, at 1005 CST.  A high level drain  |
| primary alarm was received during a cylinder sampling heat cycle.  The       |
| safety system did operate as required (shuts off steam to the autoclave      |
| which reduces the amount of condensation in the autoclave).  The purpose of  |
| the WICS is to limit the amount of condensate in the autoclave.  The cause   |
| of this actuation is being investigated.  The certificate holder thinks that |
| this event might have been caused by an invalid signal, and if it is         |
| determined that this event was caused by an invalid signal, this event       |
| notification will be retracted at a later time.                              |
|                                                                              |
| The safety system actuation is reportable per Safety Analysis Report,        |
| Section 6.9, Table 1, Criteria J.2, Safety System Actuation due to a Valid   |
| Signal, as a 24-hour event notification.                                     |
|                                                                              |
| The NRC resident inspector was notified of this event.                       |
|                                                                              |
| ***RETRACTION on 03/12/99 at 1324 EST from W. F. Cage taken by               |
| MacKinnon****                                                                |
|                                                                              |
| Subsequent investigation and troubleshooting of the autoclave systems has    |
| concluded that the WICS actuated due to an invalid signal.  This condition   |
| is supported by the following:                                               |
|                                                                              |
| 1. The actuation occurred at a point in the heating cycle after the maximum  |
| steam demand and resulting highest condensate load has passed.  Past history |
| has shown that valid actuations occur during maximum steam and condensate    |
| load, not afterward at lower loads.                                          |
|                                                                              |
| 2.  The actuation was initiated by the primary condensate probe only.  The   |
| secondary condensate probe did not alarm until after the steam supply had    |
| been isolated by the WICS actuation, which caused a drop in autoclave        |
| pressure supplying the motive force, driving the condensate out into the     |
| drain.  This, and testing subsequent to the event, proved that both probes   |
| were operable and would have alarmed had water in the drain actually risen   |
| to the probe level.                                                          |
|                                                                              |
| 3.  The drain line was inspected, and no obstruction was noted that could    |
| have caused a blockage or disruption of condensate flow.                     |
|                                                                              |
| 4.  Inspection of the autoclave electrical systems indicated that some of    |
| the condensate probe wires were not properly, or firmly, grounded.  These    |
| loose connections are considered to be the most likely cause of the WICS     |
| actuation.  This would be an actuation from an invalid signal, i.e., not     |
| what the safety system is designed to protect against.                       |
|                                                                              |
| The NRC resident inspector was not notified of this event by the certificate |
| holder.  The NRC Region 3 (Ron Gardner) and NMSS EO (Fred Combs) were        |
| notified by the NRC operations officer.                                      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35461       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS              REGION:  4  |NOTIFICATION DATE: 03/12/1999|
|    UNIT:  [1] [2] []                STATE:  TX |NOTIFICATION TIME: 00:07[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        03/11/1999|
+------------------------------------------------+EVENT TIME:        11:30[CST]|
| NRC NOTIFIED BY:  KLIMPLE                      |LAST UPDATE DATE:  03/12/1999|
|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |GARY SANBORN         R4      |
|10 CFR SECTION:                                 |                             |
|NINF                     INFORMATION ONLY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| THE PLANT DOES NOT MEET THE DESIGN BASIS REQUIREMENT FOR RHR HEAT EXCHANGER  |
| CONTROL VALVES TO BE SECURED IN A SAFE POSITION.                             |
|                                                                              |
| DURING A REVIEW OF THE OPERATING PROCEDURES FOR THE RESIDUAL HEAT REMOVAL    |
| (RHR) HEAT EXCHANGER SYSTEM, NO STEPS OR LINEUPS WERE FOUND TO IMPLEMENT THE |
| DESIGN BASIS REQUIREMENT FOR THE RHR HEAT EXCHANGER FLOW AND BYPASS CONTROL  |
| VALVES TO BE SECURED IN THEIR SAFE POSITION.                                 |
|                                                                              |
| THE RHR HEAT EXCHANGER FLOW AND BYPASS CONTROL VALVES WERE FOUND TO BE       |
| CONFIGURED WITH THE SOLENOID VENT VALVES IN AN ENERGIZED CONDITION,          |
| THEREFORE, POTENTIALLY ALLOWING THE NON-SAFETY-RELATED POSITIONER TO CONTROL |
| THE VALVE.                                                                   |
| FAILURE OF ONE OF THE NON-SAFETY POSITIONERS (DUE TO ADVERSE CONDITIONS)     |
| COULD HAVE DRIVEN THE VALVES TO THEIR NON-SAFETY  POSITION  AT THE ONSET OF  |
| A POSTULATED ACCIDENT, THEREBY PREVENTING THE IMMEDIATE AVAILABILITY OF THE  |
| LOW HEAD SAFETY INJECTION FLOW.                                              |
|                                                                              |
| THIS CONDITION WAS RESOLVED AS SOON AS IT WAS IDENTIFIED BY DE-ENERGIZING    |
| AND REMOVING THE FUSES FOR THE VALVES.                                       |
|                                                                              |
| THE NRC RESIDENT INSPECTOR WAS NOTIFIED BY THE LICENSEE.                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35462       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HARRIS                   REGION:  2  |NOTIFICATION DATE: 03/12/1999|
|    UNIT:  [1] [] []                 STATE:  NC |NOTIFICATION TIME: 09:48[EST]|
|   RXTYPE: [1] W-3-LP                           |EVENT DATE:        03/12/1999|
+------------------------------------------------+EVENT TIME:        06:39[EST]|
| NRC NOTIFIED BY:  KEITH HOLBROOK               |LAST UPDATE DATE:  03/12/1999|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |EDWARD MCALPINE      R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       100      Power Operation  |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AUTOMATIC REACTOR TRIP DUE TO TURBINE TRIP AND MAIN FEEDWATER ISOLATION      |
| CAUSED BY HIGH STEAM GENERATOR WATER LEVEL.                                  |
|                                                                              |
| This is a report of the following actuations:  ESF-P-14, Turbine Trip and    |
| Main Feedwater Isolation; auxiliary feedwater actuation; and a reactor       |
| trip.                                                                        |
|                                                                              |
| A loss of control of the "C"  feed regulating valve caused steam generator   |
| water level to increase.  Operators attempted to take manual control but had |
| very little control from the main control room.  The  steam generator water  |
| level exceeded the 82.4% high steam generator water level trip setpoint      |
| causing a P-14 (steam generator high level override) actuation.  This        |
| actuation resulted in a turbine trip/reactor trip and a loss of both running |
| main feedwater pumps.  It also caused all main feedwater isolation valves to |
| close.  All control rods fully inserted.  No primary/secondary plant code    |
| safety valves or power-operated relief valves opened.  Both motor-driven and |
| the turbine-driven auxiliary feedwater pumps automatically started on low    |
| steam generator water level following the reactor trip.  The steam dump      |
| bypass control system is operating properly and is maintaining a T(ave) of   |
| 557�F.  At the present time, steam generator water levels are being          |
| maintained by one operating motor-driven auxiliary feedwater pump.           |
| Troubleshooting is in progress to determine the failure of "C" feedwater     |
| regulating valve (air-operated valve).                                       |
|                                                                              |
| The offsite electrical grid is stable, and all emergency core cooling        |
| systems and the emergency diesel generators are fully operable if needed.    |
|                                                                              |
| The NRC resident inspector was notified of this event by the licensee.       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35463       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MCGUIRE                  REGION:  2  |NOTIFICATION DATE: 03/12/1999|
|    UNIT:  [1] [2] []                STATE:  NC |NOTIFICATION TIME: 12:24[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        03/11/1999|
+------------------------------------------------+EVENT TIME:        15:00[EST]|
| NRC NOTIFIED BY:  MIKE WILDER                  |LAST UPDATE DATE:  03/12/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |EDWARD MCALPINE      R2      |
|10 CFR SECTION:                                 |                             |
|NLTR                     LICENSEE 24 HR REPORT  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       82       Power Operation  |82       Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - Discrepancies between Plant Fire Protection Program and 10CFR50, Appendix  |
| R, Safety Evaluation Report -                                                |
|                                                                              |
| A self initiated technical audit of the McGuire Fire Protection Program      |
| identified apparent deviations from the approved Fire Protection Program.  A |
| potential discrepancy exists between the McGuire Fire Protection Program and |
| the NRC description provided in Safety Evaluation Report (SER), Supplement   |
| 6, regarding Appendix R, Section III.G.3.  Additional deviations from        |
| certain licensee commitments regarding testing were also identified in the   |
| audit.                                                                       |
|                                                                              |
| The licensee's engineering staff has evaluated deviations identified by the  |
| audit team and has determined that the fire protection related systems are   |
| fully operable.  In addition, these deviations have no impact on achieving   |
| and maintaining safe shutdown following a design bases fire event.           |
|                                                                              |
| McGuire Facility Operating License (FOL) NPF-9 (Unit 1) and NPF-17 (Unit 2)  |
| require 24-hour notification to the NRC for deviations from the approved     |
| Fire Protection Program. The above deviations are being reported under that  |
| license condition criterion.  A follow-up report describing the cause of the |
| deviations and corrective actions will be submitted to the NRC within 14     |
| days.                                                                        |
|                                                                              |
| The licensee notified the NRC resident inspector                             |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35464       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: POINT BEACH              REGION:  3  |NOTIFICATION DATE: 03/12/1999|
|    UNIT:  [1] [2] []                STATE:  WI |NOTIFICATION TIME: 15:08[EST]|
|   RXTYPE: [1] W-2-LP,[2] W-2-LP                |EVENT DATE:        03/12/1999|
+------------------------------------------------+EVENT TIME:        13:14[CST]|
| NRC NOTIFIED BY:  PHIL SHORT                   |LAST UPDATE DATE:  03/12/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |RONALD GARDNER       R3      |
|10 CFR SECTION:                                 |                             |
|AOUT 50.72(b)(1)(ii)(B)  OUTSIDE DESIGN BASIS   |                             |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       73       Power Operation  |73       Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - AUXILIARY FEEDWATER SYSTEM FOR BOTH UNITS INOPERABLE FOR 4 MINUTES -       |
|                                                                              |
| UNIT 1 IS OPERATING AT 100% POWER, AND UNIT 2 IS OPERATING AT 73% POWER.     |
|                                                                              |
| ON 03/12/99, DURING AN ENGINEERING EVALUATION, LICENSEE ENGINEERING          |
| DEPARTMENT PERSONNEL DETERMINED THAT THE UNIT 2 TURBINE-DRIVEN (TD)          |
| AUXILIARY FEEDWATER (AFW)                                                    |
| PUMP FLOW RATE HAD BEEN SET INCORRECTLY DURING A PREVIOUSLY PERFORMED TEST.  |
| LICENSEE PERSONNEL DETERMINED THAT THIS CONDITION AFFECTED THE ENTIRE AFW    |
| SYSTEM.  (PORTIONS OF THE AFW SYSTEM ARE SHARED BY BOTH UNITS.)              |
|                                                                              |
| AT 1314 CST ON 03/12/99, THE LICENSEE ADMINISTRATIVELY DECLARED THE UNIT 1   |
| TD AFW PUMP, THE UNIT 2 TD AFW PUMP, AND THE TWO SHARED MOTOR-DRIVEN (MD)    |
| AFW PUMPS INOPERABLE (AND THUS, THE ENTIRE AFW SYSTEM) AND ENTERED TECHNICAL |
| SPECIFICATION LIMITING CONDITION FOR OPERATION ACTION STATEMENT 15.3.0.B     |
| (a.k.a. 3.0.3).  ALL FOUR AFW PUMPS REMAINED FUNCTIONAL.  THIS CONDITION IS  |
| CONSIDERED TO BE OUTSIDE THE DESIGN BASES OF THE PLANT.                      |
|                                                                              |
| AT 1318 CST ON 03/12/99, THE LICENSEE TRIPPED THE UNIT 2 TD AFW PUMP AND     |
| DECLARED IT INOPERABLE, ENTERED TECH SPEC LCO A/S 15.3.4.C.1 (72 HOUR        |
| SHUTDOWN LCO), DECLARED THE OTHER THREE AFW PUMPS OPERABLE, AND EXITED TECH  |
| SPEC LCO A/S 15.3.0.B.  THUS, ONLY THE UNIT 2 PORTION OF THE AFW SYSTEM IS   |
| INOPERABLE.                                                                  |
|                                                                              |
| THE LICENSEE IS DETERMINING CORRECTIVE ACTIONS.                              |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35465       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PEACH BOTTOM             REGION:  1  |NOTIFICATION DATE: 03/12/1999|
|    UNIT:  [] [3] []                 STATE:  PA |NOTIFICATION TIME: 16:23[EST]|
|   RXTYPE: [2] GE-4,[3] GE-4                    |EVENT DATE:        03/12/1999|
+------------------------------------------------+EVENT TIME:        12:34[EST]|
| NRC NOTIFIED BY:  PHIL BREIDENBAUGH            |LAST UPDATE DATE:  03/12/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |TOM MOSLAK           R1      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|3     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - RCIC SYSTEM VALVES CLOSED TO ISOLATE CONTAINMENT DURING MAINTENANCE        |
| ACTIVITIES -                                                                 |
|                                                                              |
| AT 1234 ON 03/12/99, WITH UNIT 3 AT 100% POWER, A PRIMARY CONTAINMENT        |
| ISOLATION OCCURRED FOR THE REACTOR CORE ISOLATION COOLING (RCIC) SYSTEM      |
| DURING RESTORATION FROM MAINTENANCE ACTIVITIES.  THE ISOLATION OCCURRED WHEN |
| THE OUTBOARD STEAM ISOLATION VALVE WAS JOGGED OPEN TO REPRESSURIZE THE STEAM |
| LINE TO THE RCIC TURBINE.  WHEN THE VALVE WAS JOGGED OPEN, A MOMENTARY HIGH  |
| STEAM FLOW SIGNAL OCCURRED AND BOTH INBOARD AND OUTBOARD ISOLATION VALVES    |
| CLOSED TO THEIR ISOLATION POSITION.                                          |
|                                                                              |
| AT 1620 ON 03/12/99, THE LICENSEE RESET ALL SYSTEMS TO NORMAL.               |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   35466       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  COOPER ENERGY SERVICES               |NOTIFICATION DATE: 03/12/1999|
|LICENSEE:  COOPER ENERGY SERVICES               |NOTIFICATION TIME: 16:27[EST]|
|    CITY:  GROVE CITY               REGION:  1  |EVENT DATE:        03/12/1999|
|  COUNTY:                            STATE:  PA |EVENT TIME:        12:00[EST]|
|LICENSE#:                        AGREEMENT:  N  |LAST UPDATE DATE:  03/12/1999|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |TOM MOSLAK           R1      |
|                                                |RONALD GARDNER       R3      |
+------------------------------------------------+GARY SANBORN         R4      |
| NRC NOTIFIED BY:  JOHN M. HORNE                |VERN HODGE           NRR     |
|  HQ OPS OFFICER:  DICK JOLLIFFE                |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|CDEG 21.21(c)(3)(i)      DEFECTS/NONCOMPLIANCE  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - Amendment to 10 CFR Part 21 - Cooper-Bessemer KSV Emergency Diesel         |
| Generator Power Piston Failure -                                             |
| (Refer to event #32416 for additional information.)                          |
|                                                                              |
| Following the failure of a KSV power piston due to a hydraulic lock at       |
| Commonwealth Edison Zion Station in January, 1997, Cooper Cameron            |
| Corporation issued a Part 21 notification letter dated May 29, 1997,         |
| reference QCG-10389.  The piston which failed had a minimum crown thickness  |
| of 0.040 inches, but had operated successfully for several years, and failed |
| only because of the unusual hydraulic lock event.  That letter recommended   |
| that KSV pistons be inspected for crown thickness by ultrasonic or other     |
| methods when the pistons were exposed in the course of normal maintenance    |
| activities.  A conservative minimum thickness limit of 0.100 inches was      |
| established.                                                                 |
|                                                                              |
| In the 2 years since the Zion failure, a total of 198 or more pistons have   |
| been measured at seven different sites.  Of these, one was found initially   |
| in our plant with a thickness of 0.070 inches and was destroyed.  All other  |
| pistons checked have been above the 0.100-inch limit, and the actual         |
| measured thickness was recorded for 157 of these.  All but seven of those    |
| documented have had a minimum thickness of 0.150 inch or greater.  The       |
| distribution of minimum thickness for the pistons has been documented to be  |
| from 0.100 to >0.400 inches.  These results, in combination with the         |
| successful operating history of the KSV engine, provide reasonable assurance |
| that all potentially defective pistons have been removed from service.       |
|                                                                              |
| Based on this information, Cooper-Bessemer believes it is not necessary to   |
| continue to measure the thickness of piston crowns during other maintenance  |
| activities.                                                                  |
|                                                                              |
| This 10 CFR Part 21 Amendment applies to the following plants:               |
| Region 1 - Nine Mile Point and Susquehanna                                   |
| Region 3 - Byron and Zion                                                    |
| Region 4 - Cooper, Palo Verde, Waterford, South Texas and Grand Gulf.        |
|                                                                              |
| (Call the NRC Operations Center for a contact telephone number.)             |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35467       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DIABLO CANYON            REGION:  4  |NOTIFICATION DATE: 03/12/1999|
|    UNIT:  [1] [2] []                STATE:  CA |NOTIFICATION TIME: 16:37[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        03/12/1999|
+------------------------------------------------+EVENT TIME:        13:00[PST]|
| NRC NOTIFIED BY:  ART WELLS                    |LAST UPDATE DATE:  03/12/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |GARY SANBORN         R4      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Hot Shutdown     |0        Hot Shutdown     |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - PLANT SECURITY REPORT -                                                    |
|                                                                              |
| A SAFEGUARDS SYSTEM DEGRADATION RELATED TO PERIMETER MONITORING OCCURRED.    |
| COMPENSATORY MEASURES IMMEDIATELY WERE TAKEN UPON DISCOVERY.  REFER TO THE   |
| HOO LOG FOR ADDITIONAL DETAILS.                                              |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35468       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MILLSTONE                REGION:  1  |NOTIFICATION DATE: 03/12/1999|
|    UNIT:  [] [] [3]                 STATE:  CT |NOTIFICATION TIME: 17:39[EST]|
|   RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP           |EVENT DATE:        03/12/1999|
+------------------------------------------------+EVENT TIME:        17:31[EST]|
| NRC NOTIFIED BY:  JOE RUTTAR                   |LAST UPDATE DATE:  03/12/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |TOM MOSLAK           R1      |
|10 CFR SECTION:                                 |                             |
|AOUT 50.72(b)(1)(ii)(B)  OUTSIDE DESIGN BASIS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|                                                   |                          |
|3     N          Y       100      Power Operation  |100      Power Operation  |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| -Control room personnel access door latch mechanism may not withstand HELB   |
| pressure in the turbine building-                                            |
|                                                                              |
| A licensee preliminary review of an error in an analysis assumption for the  |
| pressure applied to a control room personnel access door due to a high       |
| energy line break (HELB) in the turbine building indicates that the door     |
| latch mechanism may not withstand the applied pressure.                      |
|                                                                              |
| The control room door has been latched with an alternative latching          |
| mechanism and will remain closed against this pressure so there are no       |
| current operability concerns.                                                |
|                                                                              |
| This situation results in a historical condition where Unit 3 may have       |
| operated outside its design basis.  Engineering evaluation is continuing.  A |
| conservative decision has been made to report this condition as a condition  |
| outside the design basis of Unit 3 pursuant to 10CFR50.72(b)(1)(ii)(B)       |
| pending the results of this evaluation.                                      |
|                                                                              |
| The licensee informed the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35469       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS              REGION:  4  |NOTIFICATION DATE: 03/12/1999|
|    UNIT:  [] [2] []                 STATE:  TX |NOTIFICATION TIME: 19:02[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        03/12/1999|
+------------------------------------------------+EVENT TIME:        14:12[CST]|
| NRC NOTIFIED BY:  TIM FRAWLEY                  |LAST UPDATE DATE:  03/13/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |GARY SANBORN         R4      |
|10 CFR SECTION:                                 |WILLIAM BECKNER, EO  NRR     |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |ROSEMARY HOGAN       IRO     |
|NLCO                     TECH SPEC LCO A/S      |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| - PARTIAL LOSS OF OFFSITE POWER DUE TO A FAULT IN A SWITCHYARD CIRCUIT       |
| BREAKER -                                                                    |
|                                                                              |
| AT 1412 CST ON 03/12/99, DURING PLANT SWITCHYARD ACTIVITIES, UNIT 2          |
| EXPERIENCED A LOSS OF POWER TO THE #2 STANDBY TRANSFORMER DUE TO A FAULT IN  |
| A SWITCHYARD CIRCUIT BREAKER.  THIS CONDITION CAUSED TRAIN 'B' AND TRAIN 'C' |
| 4160-VOLT ESF BUSES TO ACTUATE ON A LOSS OF OFFSITE POWER.  THE FOLLOWING    |
| ESF SYSTEMS ACTUATED: TRAIN 'B' AND TRAIN 'C' ESF EDGs, ESSENTIAL COOLING    |
| WATER SYSTEM, ESSENTIAL CHILLED WATER SYSTEM, COMPONENT COOLING WATER        |
| SYSTEM, CONTROL ROOM HVAC SYSTEM, AND AUXILIARY FEEDWATER SYSTEM (ON RECIRC  |
| MODE).                                                                       |
|                                                                              |
| DURING THIS EVENT, THE SPENT FUEL POOL TEMPERATURE INCREASED APPROXIMATELY   |
| 1.5�F, AND THE TRAIN 'B' ESF EDG (#22) OUTPUT BREAKER FAILED TO CLOSE        |
| AUTOMATICALLY.  THE LICENSEE DECLARED THE TRAIN 'B' ESF EDG (#22)            |
| INOPERABLE, EVEN THOUGH IT IS FUNCTIONAL (72-HOUR LCO).                      |
|                                                                              |
| THERE WAS NO FIRE, AND NO PERSONNEL WERE INJURED.  THE LICENSEE RESTORED ALL |
| SYSTEMS TO NORMAL.  UNIT 2 IS STABLE AND OPERATING AT 100% POWER.            |
|                                                                              |
| THE LICENSEE IS INVESTIGATING THE CAUSE OF THE FAULT IN THE SWITCHYARD       |
| CIRCUIT BREAKER AND THE TRAIN 'B' ESF EDG (#22) OUTPUT BREAKER FAILING TO    |
| CLOSE AUTOMATICALLY.                                                         |
|                                                                              |
| THE LICENSEE PLANS TO SUBMIT A LICENSEE EVENT REPORT ON THIS EVENT TO THE    |
| NRC.                                                                         |
|                                                                              |
| THIS EVENT HAD NO IMPACT ON UNIT 1.                                          |
|                                                                              |
| THE NRC RESIDENT INSPECTOR WAS ON SITE DURING THIS EVENT AND REPORTED IT TO  |
| REGION 4.                                                                    |
| REGION 4 PERSONNEL WERE AWARE OF THIS EVENT PRIOR TO THE LICENSEE REPORTING  |
| IT TO THE NRC OPERATIONS OFFICER.                                            |
|                                                                              |
|                                                                              |
| * * * UPDATE AT 1207 ON 03/13/99 FROM TIM FRAWLEY TO JOLLIFFE * * *          |
|                                                                              |
| AT 1412 CST ON 03/12/99, DURING THE LOSS OF POWER TO #2 STANDBY TRANSFORMER, |
| THE LICENSEE ENTERED TECH SPEC 3.0.3 FOR UNIT 2 DUE TO THE LOSS OF POWER TO  |
| TWO 13.8-KV STANDBY BUSES AND THE INOPERABLE CONDITION OF THE TRAIN 'B' ESF  |
| EDG (#22); THIS CONDITION IS NOT COVERED UNDER THE ACTIONS OF TECH SPEC      |
| 3.8.1.1 (AC ELECTRICAL POWER SOURCES).                                       |
|                                                                              |
| AT 1530 CST ON 03/12/99, THE LICENSEE RESTORED POWER TO THE TWO 13.8-KV      |
| STANDBY BUSES.                                                               |
|                                                                              |
| AT 1553 CST ON 03/12/99, THE LICENSEE EXITED TECH SPEC 3.0.3 FOLLOWING       |
| SATISFACTORY PERFORMANCE OF SURVEILLANCE REQUIREMENT 4.8.1.1.1.a.  THIS      |
| CONDITION IS REPORTABLE TO THE NRC UNDER SECTION 2.G OF FACILITY OPERATING   |
| LICENSE NPF-80.                                                              |
|                                                                              |
| UNIT 2 IS STABLE AND OPERATING AT 100% POWER.                                |
|                                                                              |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR.  THE NRC OPERATIONS        |
| OFFICER NOTIFIED THE R4DO (GARY SANBORN), NRR EO (BILL BECKNER), AND IRO MGR |
| (ROSEMARY HOGAN).                                                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35470       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SEABROOK                 REGION:  1  |NOTIFICATION DATE: 03/13/1999|
|    UNIT:  [1] [] []                 STATE:  NH |NOTIFICATION TIME: 16:31[EST]|
|   RXTYPE: [1] W-4-LP                           |EVENT DATE:        03/13/1999|
+------------------------------------------------+EVENT TIME:        10:32[EST]|
| NRC NOTIFIED BY:  PATRICK CYR                  |LAST UPDATE DATE:  03/13/1999|
|  HQ OPS OFFICER:  DICK JOLLIFFE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |TOM MOSLAK           R1      |
|10 CFR SECTION:                                 |                             |
|HFIT 26.73               FITNESS FOR DUTY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| A CONTRACTOR SUPERVISOR WAS DETERMINED TO BE UNDER THE INFLUENCE OF ALCOHOL  |
| DURING A RANDOM TEST.  THE CONTRACTOR'S ACCESS AUTHORIZATION TO THE PLANT    |
| HAS BEEN TERMINATED.  REFER TO THE HOO LOG FOR ADDITIONAL DETAILS.           |
|                                                                              |
| THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR.                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   35471       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CLINTON                  REGION:  3  |NOTIFICATION DATE: 03/15/1999|
|    UNIT:  [1] [] []                 STATE:  IL |NOTIFICATION TIME: 03:57[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        03/15/1999|
+------------------------------------------------+EVENT TIME:        01:05[CST]|
| NRC NOTIFIED BY:  TIM HOLLAND                  |LAST UPDATE DATE:  03/15/1999|
|  HQ OPS OFFICER:  LEIGH TROCINE                +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |RONALD GARDNER       R3      |
|10 CFR SECTION:                                 |                             |
|AESF 50.72(b)(2)(ii)     ESF ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNANTICIPATED REACTOR CORE ISOLATION COOLING (RCIC) SUCTION VALVE ISOLATION  |
| DURING PERFORMANCE OF A REVISED TEST PROCEDURE                               |
|                                                                              |
| The following text is a portion of a facsimile received from the licensee:   |
|                                                                              |
| "During the performance of CPS No. 9054.04 (RCIC Automatic Suction Shift     |
| Test), the RCIC suction valve from the suppression pool (1E51-F031)          |
| automatically isolated on a valid low steam line pressure signal.  This      |
| isolation was not intended to occur during the performance of this           |
| procedure."                                                                  |
|                                                                              |
| "The isolation occurred following the removal of a simulated RCIC steam line |
| pressure signal of > 60 psig.  When the current steam line pressure of 0     |
| psig was picked up by the logic, the 1E51-F031 isolated as designed."  Upon  |
| receipt of the valid low steam line pressure signal, all systems functioned  |
| as required and  there was nothing unusual or not understood.                |
|                                                                              |
| The licensee stated that the test procedure was newly revised and that some  |
| of the steps had been swapped.  The steps should have requested opening of   |
| the other suction source, closure of this suction source, and then removal   |
| the simulator.                                                               |
|                                                                              |
| The licensee notified the NRC resident inspector.                            |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Wednesday, March 24, 2021