Event Notification Report for March 15, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/12/1999 - 03/15/1999 ** EVENT NUMBERS ** 35387 35461 35462 35463 35464 35465 35466 35467 35468 35469 35470 35471 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35387 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/20/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 08:44[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/19/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 10:05[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/12/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |MIKE JORDAN R3 | | DOCKET: 0707001 |CHARLEY HAUGHNEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: K. A. BEASLEY | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | WATER INVENTORY CONTROL SYSTEM ACTIVATION | | | | A water inventory control system (WICS) activation occurred on C-360 | | position 4 autoclave on February 19, 1999, at 1005 CST. A high level drain | | primary alarm was received during a cylinder sampling heat cycle. The | | safety system did operate as required (shuts off steam to the autoclave | | which reduces the amount of condensation in the autoclave). The purpose of | | the WICS is to limit the amount of condensate in the autoclave. The cause | | of this actuation is being investigated. The certificate holder thinks that | | this event might have been caused by an invalid signal, and if it is | | determined that this event was caused by an invalid signal, this event | | notification will be retracted at a later time. | | | | The safety system actuation is reportable per Safety Analysis Report, | | Section 6.9, Table 1, Criteria J.2, Safety System Actuation due to a Valid | | Signal, as a 24-hour event notification. | | | | The NRC resident inspector was notified of this event. | | | | ***RETRACTION on 03/12/99 at 1324 EST from W. F. Cage taken by | | MacKinnon**** | | | | Subsequent investigation and troubleshooting of the autoclave systems has | | concluded that the WICS actuated due to an invalid signal. This condition | | is supported by the following: | | | | 1. The actuation occurred at a point in the heating cycle after the maximum | | steam demand and resulting highest condensate load has passed. Past history | | has shown that valid actuations occur during maximum steam and condensate | | load, not afterward at lower loads. | | | | 2. The actuation was initiated by the primary condensate probe only. The | | secondary condensate probe did not alarm until after the steam supply had | | been isolated by the WICS actuation, which caused a drop in autoclave | | pressure supplying the motive force, driving the condensate out into the | | drain. This, and testing subsequent to the event, proved that both probes | | were operable and would have alarmed had water in the drain actually risen | | to the probe level. | | | | 3. The drain line was inspected, and no obstruction was noted that could | | have caused a blockage or disruption of condensate flow. | | | | 4. Inspection of the autoclave electrical systems indicated that some of | | the condensate probe wires were not properly, or firmly, grounded. These | | loose connections are considered to be the most likely cause of the WICS | | actuation. This would be an actuation from an invalid signal, i.e., not | | what the safety system is designed to protect against. | | | | The NRC resident inspector was not notified of this event by the certificate | | holder. The NRC Region 3 (Ron Gardner) and NMSS EO (Fred Combs) were | | notified by the NRC operations officer. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35461 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 03/12/1999| | UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 00:07[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/11/1999| +------------------------------------------------+EVENT TIME: 11:30[CST]| | NRC NOTIFIED BY: KLIMPLE |LAST UPDATE DATE: 03/12/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT DOES NOT MEET THE DESIGN BASIS REQUIREMENT FOR RHR HEAT EXCHANGER | | CONTROL VALVES TO BE SECURED IN A SAFE POSITION. | | | | DURING A REVIEW OF THE OPERATING PROCEDURES FOR THE RESIDUAL HEAT REMOVAL | | (RHR) HEAT EXCHANGER SYSTEM, NO STEPS OR LINEUPS WERE FOUND TO IMPLEMENT THE | | DESIGN BASIS REQUIREMENT FOR THE RHR HEAT EXCHANGER FLOW AND BYPASS CONTROL | | VALVES TO BE SECURED IN THEIR SAFE POSITION. | | | | THE RHR HEAT EXCHANGER FLOW AND BYPASS CONTROL VALVES WERE FOUND TO BE | | CONFIGURED WITH THE SOLENOID VENT VALVES IN AN ENERGIZED CONDITION, | | THEREFORE, POTENTIALLY ALLOWING THE NON-SAFETY-RELATED POSITIONER TO CONTROL | | THE VALVE. | | FAILURE OF ONE OF THE NON-SAFETY POSITIONERS (DUE TO ADVERSE CONDITIONS) | | COULD HAVE DRIVEN THE VALVES TO THEIR NON-SAFETY POSITION AT THE ONSET OF | | A POSTULATED ACCIDENT, THEREBY PREVENTING THE IMMEDIATE AVAILABILITY OF THE | | LOW HEAD SAFETY INJECTION FLOW. | | | | THIS CONDITION WAS RESOLVED AS SOON AS IT WAS IDENTIFIED BY DE-ENERGIZING | | AND REMOVING THE FUSES FOR THE VALVES. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35462 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 03/12/1999| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 09:48[EST]| | RXTYPE: [1] W-3-LP |EVENT DATE: 03/12/1999| +------------------------------------------------+EVENT TIME: 06:39[EST]| | NRC NOTIFIED BY: KEITH HOLBROOK |LAST UPDATE DATE: 03/12/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |EDWARD MCALPINE R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP DUE TO TURBINE TRIP AND MAIN FEEDWATER ISOLATION | | CAUSED BY HIGH STEAM GENERATOR WATER LEVEL. | | | | This is a report of the following actuations: ESF-P-14, Turbine Trip and | | Main Feedwater Isolation; auxiliary feedwater actuation; and a reactor | | trip. | | | | A loss of control of the "C" feed regulating valve caused steam generator | | water level to increase. Operators attempted to take manual control but had | | very little control from the main control room. The steam generator water | | level exceeded the 82.4% high steam generator water level trip setpoint | | causing a P-14 (steam generator high level override) actuation. This | | actuation resulted in a turbine trip/reactor trip and a loss of both running | | main feedwater pumps. It also caused all main feedwater isolation valves to | | close. All control rods fully inserted. No primary/secondary plant code | | safety valves or power-operated relief valves opened. Both motor-driven and | | the turbine-driven auxiliary feedwater pumps automatically started on low | | steam generator water level following the reactor trip. The steam dump | | bypass control system is operating properly and is maintaining a T(ave) of | | 557�F. At the present time, steam generator water levels are being | | maintained by one operating motor-driven auxiliary feedwater pump. | | Troubleshooting is in progress to determine the failure of "C" feedwater | | regulating valve (air-operated valve). | | | | The offsite electrical grid is stable, and all emergency core cooling | | systems and the emergency diesel generators are fully operable if needed. | | | | The NRC resident inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35463 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 03/12/1999| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 12:24[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/11/1999| +------------------------------------------------+EVENT TIME: 15:00[EST]| | NRC NOTIFIED BY: MIKE WILDER |LAST UPDATE DATE: 03/12/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |EDWARD MCALPINE R2 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 82 Power Operation |82 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Discrepancies between Plant Fire Protection Program and 10CFR50, Appendix | | R, Safety Evaluation Report - | | | | A self initiated technical audit of the McGuire Fire Protection Program | | identified apparent deviations from the approved Fire Protection Program. A | | potential discrepancy exists between the McGuire Fire Protection Program and | | the NRC description provided in Safety Evaluation Report (SER), Supplement | | 6, regarding Appendix R, Section III.G.3. Additional deviations from | | certain licensee commitments regarding testing were also identified in the | | audit. | | | | The licensee's engineering staff has evaluated deviations identified by the | | audit team and has determined that the fire protection related systems are | | fully operable. In addition, these deviations have no impact on achieving | | and maintaining safe shutdown following a design bases fire event. | | | | McGuire Facility Operating License (FOL) NPF-9 (Unit 1) and NPF-17 (Unit 2) | | require 24-hour notification to the NRC for deviations from the approved | | Fire Protection Program. The above deviations are being reported under that | | license condition criterion. A follow-up report describing the cause of the | | deviations and corrective actions will be submitted to the NRC within 14 | | days. | | | | The licensee notified the NRC resident inspector | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35464 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 03/12/1999| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 15:08[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 03/12/1999| +------------------------------------------------+EVENT TIME: 13:14[CST]| | NRC NOTIFIED BY: PHIL SHORT |LAST UPDATE DATE: 03/12/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 73 Power Operation |73 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - AUXILIARY FEEDWATER SYSTEM FOR BOTH UNITS INOPERABLE FOR 4 MINUTES - | | | | UNIT 1 IS OPERATING AT 100% POWER, AND UNIT 2 IS OPERATING AT 73% POWER. | | | | ON 03/12/99, DURING AN ENGINEERING EVALUATION, LICENSEE ENGINEERING | | DEPARTMENT PERSONNEL DETERMINED THAT THE UNIT 2 TURBINE-DRIVEN (TD) | | AUXILIARY FEEDWATER (AFW) | | PUMP FLOW RATE HAD BEEN SET INCORRECTLY DURING A PREVIOUSLY PERFORMED TEST. | | LICENSEE PERSONNEL DETERMINED THAT THIS CONDITION AFFECTED THE ENTIRE AFW | | SYSTEM. (PORTIONS OF THE AFW SYSTEM ARE SHARED BY BOTH UNITS.) | | | | AT 1314 CST ON 03/12/99, THE LICENSEE ADMINISTRATIVELY DECLARED THE UNIT 1 | | TD AFW PUMP, THE UNIT 2 TD AFW PUMP, AND THE TWO SHARED MOTOR-DRIVEN (MD) | | AFW PUMPS INOPERABLE (AND THUS, THE ENTIRE AFW SYSTEM) AND ENTERED TECHNICAL | | SPECIFICATION LIMITING CONDITION FOR OPERATION ACTION STATEMENT 15.3.0.B | | (a.k.a. 3.0.3). ALL FOUR AFW PUMPS REMAINED FUNCTIONAL. THIS CONDITION IS | | CONSIDERED TO BE OUTSIDE THE DESIGN BASES OF THE PLANT. | | | | AT 1318 CST ON 03/12/99, THE LICENSEE TRIPPED THE UNIT 2 TD AFW PUMP AND | | DECLARED IT INOPERABLE, ENTERED TECH SPEC LCO A/S 15.3.4.C.1 (72 HOUR | | SHUTDOWN LCO), DECLARED THE OTHER THREE AFW PUMPS OPERABLE, AND EXITED TECH | | SPEC LCO A/S 15.3.0.B. THUS, ONLY THE UNIT 2 PORTION OF THE AFW SYSTEM IS | | INOPERABLE. | | | | THE LICENSEE IS DETERMINING CORRECTIVE ACTIONS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35465 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 03/12/1999| | UNIT: [] [3] [] STATE: PA |NOTIFICATION TIME: 16:23[EST]| | RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 03/12/1999| +------------------------------------------------+EVENT TIME: 12:34[EST]| | NRC NOTIFIED BY: PHIL BREIDENBAUGH |LAST UPDATE DATE: 03/12/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - RCIC SYSTEM VALVES CLOSED TO ISOLATE CONTAINMENT DURING MAINTENANCE | | ACTIVITIES - | | | | AT 1234 ON 03/12/99, WITH UNIT 3 AT 100% POWER, A PRIMARY CONTAINMENT | | ISOLATION OCCURRED FOR THE REACTOR CORE ISOLATION COOLING (RCIC) SYSTEM | | DURING RESTORATION FROM MAINTENANCE ACTIVITIES. THE ISOLATION OCCURRED WHEN | | THE OUTBOARD STEAM ISOLATION VALVE WAS JOGGED OPEN TO REPRESSURIZE THE STEAM | | LINE TO THE RCIC TURBINE. WHEN THE VALVE WAS JOGGED OPEN, A MOMENTARY HIGH | | STEAM FLOW SIGNAL OCCURRED AND BOTH INBOARD AND OUTBOARD ISOLATION VALVES | | CLOSED TO THEIR ISOLATION POSITION. | | | | AT 1620 ON 03/12/99, THE LICENSEE RESET ALL SYSTEMS TO NORMAL. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35466 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: COOPER ENERGY SERVICES |NOTIFICATION DATE: 03/12/1999| |LICENSEE: COOPER ENERGY SERVICES |NOTIFICATION TIME: 16:27[EST]| | CITY: GROVE CITY REGION: 1 |EVENT DATE: 03/12/1999| | COUNTY: STATE: PA |EVENT TIME: 12:00[EST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 03/12/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |TOM MOSLAK R1 | | |RONALD GARDNER R3 | +------------------------------------------------+GARY SANBORN R4 | | NRC NOTIFIED BY: JOHN M. HORNE |VERN HODGE NRR | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CDEG 21.21(c)(3)(i) DEFECTS/NONCOMPLIANCE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Amendment to 10 CFR Part 21 - Cooper-Bessemer KSV Emergency Diesel | | Generator Power Piston Failure - | | (Refer to event #32416 for additional information.) | | | | Following the failure of a KSV power piston due to a hydraulic lock at | | Commonwealth Edison Zion Station in January, 1997, Cooper Cameron | | Corporation issued a Part 21 notification letter dated May 29, 1997, | | reference QCG-10389. The piston which failed had a minimum crown thickness | | of 0.040 inches, but had operated successfully for several years, and failed | | only because of the unusual hydraulic lock event. That letter recommended | | that KSV pistons be inspected for crown thickness by ultrasonic or other | | methods when the pistons were exposed in the course of normal maintenance | | activities. A conservative minimum thickness limit of 0.100 inches was | | established. | | | | In the 2 years since the Zion failure, a total of 198 or more pistons have | | been measured at seven different sites. Of these, one was found initially | | in our plant with a thickness of 0.070 inches and was destroyed. All other | | pistons checked have been above the 0.100-inch limit, and the actual | | measured thickness was recorded for 157 of these. All but seven of those | | documented have had a minimum thickness of 0.150 inch or greater. The | | distribution of minimum thickness for the pistons has been documented to be | | from 0.100 to >0.400 inches. These results, in combination with the | | successful operating history of the KSV engine, provide reasonable assurance | | that all potentially defective pistons have been removed from service. | | | | Based on this information, Cooper-Bessemer believes it is not necessary to | | continue to measure the thickness of piston crowns during other maintenance | | activities. | | | | This 10 CFR Part 21 Amendment applies to the following plants: | | Region 1 - Nine Mile Point and Susquehanna | | Region 3 - Byron and Zion | | Region 4 - Cooper, Palo Verde, Waterford, South Texas and Grand Gulf. | | | | (Call the NRC Operations Center for a contact telephone number.) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35467 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 03/12/1999| | UNIT: [1] [2] [] STATE: CA |NOTIFICATION TIME: 16:37[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/12/1999| +------------------------------------------------+EVENT TIME: 13:00[PST]| | NRC NOTIFIED BY: ART WELLS |LAST UPDATE DATE: 03/12/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - PLANT SECURITY REPORT - | | | | A SAFEGUARDS SYSTEM DEGRADATION RELATED TO PERIMETER MONITORING OCCURRED. | | COMPENSATORY MEASURES IMMEDIATELY WERE TAKEN UPON DISCOVERY. REFER TO THE | | HOO LOG FOR ADDITIONAL DETAILS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35468 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 03/12/1999| | UNIT: [] [] [3] STATE: CT |NOTIFICATION TIME: 17:39[EST]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 03/12/1999| +------------------------------------------------+EVENT TIME: 17:31[EST]| | NRC NOTIFIED BY: JOE RUTTAR |LAST UPDATE DATE: 03/12/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | -Control room personnel access door latch mechanism may not withstand HELB | | pressure in the turbine building- | | | | A licensee preliminary review of an error in an analysis assumption for the | | pressure applied to a control room personnel access door due to a high | | energy line break (HELB) in the turbine building indicates that the door | | latch mechanism may not withstand the applied pressure. | | | | The control room door has been latched with an alternative latching | | mechanism and will remain closed against this pressure so there are no | | current operability concerns. | | | | This situation results in a historical condition where Unit 3 may have | | operated outside its design basis. Engineering evaluation is continuing. A | | conservative decision has been made to report this condition as a condition | | outside the design basis of Unit 3 pursuant to 10CFR50.72(b)(1)(ii)(B) | | pending the results of this evaluation. | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35469 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 03/12/1999| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 19:02[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/12/1999| +------------------------------------------------+EVENT TIME: 14:12[CST]| | NRC NOTIFIED BY: TIM FRAWLEY |LAST UPDATE DATE: 03/13/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GARY SANBORN R4 | |10 CFR SECTION: |WILLIAM BECKNER, EO NRR | |AESF 50.72(b)(2)(ii) ESF ACTUATION |ROSEMARY HOGAN IRO | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - PARTIAL LOSS OF OFFSITE POWER DUE TO A FAULT IN A SWITCHYARD CIRCUIT | | BREAKER - | | | | AT 1412 CST ON 03/12/99, DURING PLANT SWITCHYARD ACTIVITIES, UNIT 2 | | EXPERIENCED A LOSS OF POWER TO THE #2 STANDBY TRANSFORMER DUE TO A FAULT IN | | A SWITCHYARD CIRCUIT BREAKER. THIS CONDITION CAUSED TRAIN 'B' AND TRAIN 'C' | | 4160-VOLT ESF BUSES TO ACTUATE ON A LOSS OF OFFSITE POWER. THE FOLLOWING | | ESF SYSTEMS ACTUATED: TRAIN 'B' AND TRAIN 'C' ESF EDGs, ESSENTIAL COOLING | | WATER SYSTEM, ESSENTIAL CHILLED WATER SYSTEM, COMPONENT COOLING WATER | | SYSTEM, CONTROL ROOM HVAC SYSTEM, AND AUXILIARY FEEDWATER SYSTEM (ON RECIRC | | MODE). | | | | DURING THIS EVENT, THE SPENT FUEL POOL TEMPERATURE INCREASED APPROXIMATELY | | 1.5�F, AND THE TRAIN 'B' ESF EDG (#22) OUTPUT BREAKER FAILED TO CLOSE | | AUTOMATICALLY. THE LICENSEE DECLARED THE TRAIN 'B' ESF EDG (#22) | | INOPERABLE, EVEN THOUGH IT IS FUNCTIONAL (72-HOUR LCO). | | | | THERE WAS NO FIRE, AND NO PERSONNEL WERE INJURED. THE LICENSEE RESTORED ALL | | SYSTEMS TO NORMAL. UNIT 2 IS STABLE AND OPERATING AT 100% POWER. | | | | THE LICENSEE IS INVESTIGATING THE CAUSE OF THE FAULT IN THE SWITCHYARD | | CIRCUIT BREAKER AND THE TRAIN 'B' ESF EDG (#22) OUTPUT BREAKER FAILING TO | | CLOSE AUTOMATICALLY. | | | | THE LICENSEE PLANS TO SUBMIT A LICENSEE EVENT REPORT ON THIS EVENT TO THE | | NRC. | | | | THIS EVENT HAD NO IMPACT ON UNIT 1. | | | | THE NRC RESIDENT INSPECTOR WAS ON SITE DURING THIS EVENT AND REPORTED IT TO | | REGION 4. | | REGION 4 PERSONNEL WERE AWARE OF THIS EVENT PRIOR TO THE LICENSEE REPORTING | | IT TO THE NRC OPERATIONS OFFICER. | | | | | | * * * UPDATE AT 1207 ON 03/13/99 FROM TIM FRAWLEY TO JOLLIFFE * * * | | | | AT 1412 CST ON 03/12/99, DURING THE LOSS OF POWER TO #2 STANDBY TRANSFORMER, | | THE LICENSEE ENTERED TECH SPEC 3.0.3 FOR UNIT 2 DUE TO THE LOSS OF POWER TO | | TWO 13.8-KV STANDBY BUSES AND THE INOPERABLE CONDITION OF THE TRAIN 'B' ESF | | EDG (#22); THIS CONDITION IS NOT COVERED UNDER THE ACTIONS OF TECH SPEC | | 3.8.1.1 (AC ELECTRICAL POWER SOURCES). | | | | AT 1530 CST ON 03/12/99, THE LICENSEE RESTORED POWER TO THE TWO 13.8-KV | | STANDBY BUSES. | | | | AT 1553 CST ON 03/12/99, THE LICENSEE EXITED TECH SPEC 3.0.3 FOLLOWING | | SATISFACTORY PERFORMANCE OF SURVEILLANCE REQUIREMENT 4.8.1.1.1.a. THIS | | CONDITION IS REPORTABLE TO THE NRC UNDER SECTION 2.G OF FACILITY OPERATING | | LICENSE NPF-80. | | | | UNIT 2 IS STABLE AND OPERATING AT 100% POWER. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. THE NRC OPERATIONS | | OFFICER NOTIFIED THE R4DO (GARY SANBORN), NRR EO (BILL BECKNER), AND IRO MGR | | (ROSEMARY HOGAN). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35470 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 03/13/1999| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 16:31[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 03/13/1999| +------------------------------------------------+EVENT TIME: 10:32[EST]| | NRC NOTIFIED BY: PATRICK CYR |LAST UPDATE DATE: 03/13/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM MOSLAK R1 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A CONTRACTOR SUPERVISOR WAS DETERMINED TO BE UNDER THE INFLUENCE OF ALCOHOL | | DURING A RANDOM TEST. THE CONTRACTOR'S ACCESS AUTHORIZATION TO THE PLANT | | HAS BEEN TERMINATED. REFER TO THE HOO LOG FOR ADDITIONAL DETAILS. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35471 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 03/15/1999| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 03:57[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 03/15/1999| +------------------------------------------------+EVENT TIME: 01:05[CST]| | NRC NOTIFIED BY: TIM HOLLAND |LAST UPDATE DATE: 03/15/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RONALD GARDNER R3 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNANTICIPATED REACTOR CORE ISOLATION COOLING (RCIC) SUCTION VALVE ISOLATION | | DURING PERFORMANCE OF A REVISED TEST PROCEDURE | | | | The following text is a portion of a facsimile received from the licensee: | | | | "During the performance of CPS No. 9054.04 (RCIC Automatic Suction Shift | | Test), the RCIC suction valve from the suppression pool (1E51-F031) | | automatically isolated on a valid low steam line pressure signal. This | | isolation was not intended to occur during the performance of this | | procedure." | | | | "The isolation occurred following the removal of a simulated RCIC steam line | | pressure signal of > 60 psig. When the current steam line pressure of 0 | | psig was picked up by the logic, the 1E51-F031 isolated as designed." Upon | | receipt of the valid low steam line pressure signal, all systems functioned | | as required and there was nothing unusual or not understood. | | | | The licensee stated that the test procedure was newly revised and that some | | of the steps had been swapped. The steps should have requested opening of | | the other suction source, closure of this suction source, and then removal | | the simulator. | | | | The licensee notified the NRC resident inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021