Event Notification Report for March 4, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/03/1999 - 03/04/1999 ** EVENT NUMBERS ** 35327 35365 35418 35426 35435 35436 35437 35438 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35327 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 01/29/1999| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 13:57[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 01/29/1999| +------------------------------------------------+EVENT TIME: 12:03[EST]| | NRC NOTIFIED BY: FIELDER |LAST UPDATE DATE: 03/03/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID SILK R1 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT ENTERED A 14 DAY LCO DUE TO HPCI BEING DECLARED INOPERABLE. | | | | THE HPCI SYSTEM WAS ISOLATED AND DECLARED INOPERABLE DUE TO A SUSPECTED | | PROBLEM WITH STEAMLINE FLOW SWITCH TRIP SETPOINT. IT WAS DETERMINED THERE | | WAS A POSSIBILITY THAT THE SETSCREW INTERNAL TO THE BARTON DIFFERENTIAL | | PRESSURE SWITCH HAD NOT BEEN TIGHTEN AFTER PERFORMANCE OF THE LAST | | CALIBRATION. THIS CONDITION COULD CAUSE EXCESSIVE DRIFT. | | | | A SECOND CONCERN IS THE SWITCH'S RESPONSE DURING A SEISMIC EVENT MAY BE | | AFFECTED WITH A LOOSE SCREW. HPCI WAS ISOLATED TO MAINTAIN PRIMARY | | CONTAINMENT INTEGRITY AND A MAINTENANCE REQUEST HAS BEEN SUBMITTED. THIS | | CONCERN MAY ALSO BE APPLICABLE TO OTHER SAFETY RELATED SYSTEMS AND THEY WILL | | BE CHECKED TO ENSURE THE SETSCREW IS APPROPRIATELY TIGHTENED. RCIC IS | | OPERABLE. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | * * * RETRACTED AT 1021 EST ON 3/3/99 BY KEN GRACIA TO FANGIE JONES * * * | | | | The licensee has determined that the as-found trip setting for the steamline | | flow switch was satisfactory. Also, the as-found setting of the steamline | | flow switch was greater than the indication that occurs when the HPCI | | turbine is initiated and was greater than the indication that occurs during | | HPCI turbine operation. The HPCI system was operable before the | | surveillance and was returned to service within the Technical Specification | | timeframe for HPCI. The steamline flow switch was replaced because its | | performance, based on previous calibrations, was degrading. The steamline | | flow switch was, in fact, operable and therefore, there was no violation of | | Technical Specifications. | | | | The instrument plate screw(s) protrude through the instrument scale because | | that feature is a calibration convenience only. The seismic qualification | | of the steamline flow switch was not affected by the screws that did | | protrude through the scale plate. | | | | Therefore, this event notification is retracted as not reportable. | | | | The licensee notified the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R1DO (Michael Modes). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35365 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 02/11/1999| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 23:56[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 02/11/1999| +------------------------------------------------+EVENT TIME: 22:49[EST]| | NRC NOTIFIED BY: DAVID JENKINS |LAST UPDATE DATE: 03/03/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM DECLARED INOPERABLE DUE TO | | INABILITY TO ESTABLISH REFERENCE FLOW CONDITIONS. | | | | HPCI SYSTEM WAS DECLARED INOPERABLE DUE TO INABILITY TO ESTABLISH REFERENCE | | FLOW CONDITIONS DURING PERFORMANCE OF THE QUARTERLY OPERABILITY TEST. THESE | | CONDITIONS ARE NORMALLY ESTABLISHED AT 2,500 REVOLUTIONS/MINUTE AND 4,550 | | GALLONS/MINUTE. DURING THIS PERFORMANCE OF THE TEST, A FLOW OF 4,450 | | GALLONS/MINUTE WAS OBTAINED WITH REFERENCE TURBINE SPEED. | | | | THE HPCI SYSTEM IS A SINGLE TRAIN EMERGENCY CORE COOLING SYSTEM. | | ACCORDINGLY, EMERGENCY HIGH PRESSURE INJECTION IS NOT AVAILABLE AT THIS | | TIME. THE HIGH PRESSURE REACTOR CORE ISOLATION COOLING (RCIC) REMAINS | | OPERABLE, AND THE AUTOMATIC DEPRESSURIZATION SYSTEM (BACKUP SYSTEM FOR | | HPCI) ALSO REMAINS OPERABLE. PLANT TECHNICAL SPECIFICATIONS SECTION 3.5 | | ALLOWS CONTINUED OPERATION FOR 14 DAYS WITH HPCI SYSTEM INOPERABLE. | | | | ENGINEERING AND MAINTENANCE PERSONNEL ARE WORKING TO DETERMINE THE CAUSE OF | | THIS EVENT. ONCE THE CAUSE IS UNDERSTOOD, A CORRECTIVE ACTION PLAN WILL BE | | DEVELOPED. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED OF THIS EVENT BY THE LICENSEE. | | | | * * * RETRACTED AT 1123 EST ON 3/3/99 BY STEVE TABOR TO FANGIE JONES * * * | | | | The licensee has determined that the HPCI system was capable of performing | | its design basis function. The declaration on inoperability was | | conservative based on initial indications. However, after a calibration | | check of the flow instrumentation, which indicated the need for calibration, | | the flow instrument was calibrated. The HPCI flow test was performed again | | with satisfactory results, showing that no flow degradation had occurred. | | Thus, this event notification is retracted. | | | | The licensee notified the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R2DO (Claude Julian). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35418 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 02/27/1999| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 13:37[EST]| | RXTYPE: [1] W-2-LP |EVENT DATE: 02/27/1999| +------------------------------------------------+EVENT TIME: 11:39[EST]| | NRC NOTIFIED BY: DOUGLAS GOMEZ |LAST UPDATE DATE: 03/03/1999| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 70 Power Operation |70 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTAINMENT VENTILATION ISOLATION DURING I&C WORK ON RADIATION MONITOR | | | | "During Instrument and Control (I/C) activities on radiation channel R-12, | | an unexpected Containment Ventilation Isolation (CVI) occurred. The planning | | activities for this maintenance recognized the potential of generating a CVI | | signal and directed the technicians to install a jumper to prevent the | | actuation. Even with the jumper installed an unexpected CVI occurred when | | the R-12 drawer was deenergized. The CVI was therefore due to maintenance | | activities and was not the result of an actual high radiation condition. | | | | "No plant system other than the containment ventilation monitoring system | | was affected by this event. The plant is stable at approximately 70% power | | with a plant coastdown in progress. | | | | "This event is reportable under lOCFR50.72(b)(2)(ii), 'Any condition that | | results in a manual or automatic actuation an Engineered Safety Feature.'" | | | | The NRC resident inspector has been informed of this notification. | | | | * * * RETRACTED AT 0905 EST ON 3/3/99 BY KEVIN McLAUGHLIN TO FANGIE JONES * | | * * | | | | The licensee, RG&E, is retracting this event notification. RG&E has | | confirmed that the Containment Ventilation Isolation (CVI) signal that was | | generated on 02/27/99 was an invalid actuation and involved only the system | | equivalent to the reactor building ventilation system. Further evaluation | | confirmed that the CVI signal was due to a temporary electrical jumper that | | was connected, but did not make adequate electrical contact with the | | terminal board. The CVI was not in response to any radiation condition. | | | | The NRC Resident Inspector was notified of this retraction by the licensee. | | | | The NRC Headquarters Operations Officer notified the R1DO (Michael Modes). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35426 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 03/01/1999| | UNIT: [1] [2] [] STATE: GA |NOTIFICATION TIME: 20:18[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/01/1999| +------------------------------------------------+EVENT TIME: 19:29[EST]| | NRC NOTIFIED BY: BUTLER |LAST UPDATE DATE: 03/03/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Shutdown |0 Hot Shutdown | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BOTH MAIN AND BACKUP PROMPT NOTIFICATION SYSTEMS WERE OUT OF SERVICE. | | | | THE NOAA WEATHER RADIO SIGNALS WERE NOT BEING RECEIVED AT HATCH FOR | | APPROXIMATELY 6 MINUTES. IT APPEARS THAT DUE TO A LOOSE WIRE ON THE | | MICROPHONE, NOAA HAD NOT RECORDED ANYTHING ON THE TAPE THAT IS TRANSMITTED | | TO THE LICENSEE. THE PROBLEM WAS CORRECTED AT 1935. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED. | | | | * * * UPDATE 1200 EST 3/3/99 FROM BARRY COLEMAN TO S.SANDIN * * * | | | | THE LICENSEE IN RESPONSE TO PUBLIC INQUIRIES REGARDING INADVERTENT RADIO | | TEST SIGNALS NOTIFIED BOTH STATE AND LOCAL AGENCIES. ALSO, A LOCAL TV | | STATION CONTACTED THE LICENSEE BASED ON PUBLIC INTEREST. NOTIFIED | | R2DO(CAUDLE JULIAN). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35435 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 03/03/1999| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 17:01[EST]| | RXTYPE: [1] W-3-LP |EVENT DATE: 03/03/1999| +------------------------------------------------+EVENT TIME: 16:13[EST]| | NRC NOTIFIED BY: MACKENZIE |LAST UPDATE DATE: 03/03/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | GREATER THAN 20% OF THE SIRENS ARE OUT OF SERVICE | | | | DUE TO SEVERE WEATHER IN THE AREA OF THE SITE MORE THAN 20% OF THE | | LICENSEE'S SIRENS ARE INOPERABLE. THE PLANT HAD RECEIVED A SEVERE STORM | | WARNING WITH HIGH WINDS FROM THE WEATHER SERVICE AT 1400. REPAIR EFFORTS | | WILL BE INITIATED IMMEDIATELY. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED ALONG WITH STATE AND LOCAL | | AGENCIES. | | | | ***UPDATE ON 3/3/99 @ 2006 BY HOLBROOK TO GOULD *** | | | | THE NUMBER OF INOPERABLE SIRENS IS 5 OUT OF 62 WHICH IS WITHIN THE 20% LIMIT | | AS OF 1813. | | THE RESIDENT INSPECTOR WILL BE INFORMED. | | | | REG 2 RDO(JULIAN) WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35436 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: AUTOMATIC SWITCH CO. |NOTIFICATION DATE: 03/03/1999| |LICENSEE: AUTOMATIC SWITCH CO. |NOTIFICATION TIME: 15:51[EST]| | CITY: FLORHAM PARK REGION: 1 |EVENT DATE: 03/03/1999| | COUNTY: STATE: NJ |EVENT TIME: [EST]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 03/03/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MICHAEL MODES R1 | | |VERN HODGES NRR | +------------------------------------------------+ | | NRC NOTIFIED BY: YAOUANC(FAX) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC SWITCH CO (ASCO) REPORTED A MANUFACTURING DEFICIENCY . | | | | CERTAIN PUMP AND AMPLIFIER ASSEMBLIES USED IN ASCO GENERAL CONTROLS | | HYDRAMOTOR ACTUATORS COULD HAVE A MANUFACTURING DEFICIENCY WHICH MAY AFFECT | | THE OPERATION OF THE ACTUATORS. ASCO WAS ALERTED TO THIS PROBLEM UPON | | EXAMINATION OF A HYDRAMOTOR ACTUATOR, THAT WAS RECENTLY RETURNED TO ASCO | | FROM NINE MILE POINT 2 AFTER IT HAD FAILED DURING THE POST INSTALLATION | | TESTING. THIS CONDITION MAY RESULT IN THE FAILURE OF THE ACTUATOR PISTON TO | | RETRACT WHEN THE HYDRAMOTOR IS POWERED, OR THE ACTUATOR PISTON RETURNING TO | | THE SPRING EXTENDED POSITION WHILE THE HYDRAMOTOR IS POWERED. THEY ARE | | CONTINUING THE INVESTIGATION AND WILL PROVIDE A COMPLETE LIST OF POTENTIALLY | | AFFECTED ACTUATORS, ALONG WITH THEIR PURCHASERS. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35437 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 03/03/1999| | UNIT: [1] [] [] STATE: CA |NOTIFICATION TIME: 20:31[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/03/1999| +------------------------------------------------+EVENT TIME: 15:01[PST]| | NRC NOTIFIED BY: MAGRUDER |LAST UPDATE DATE: 03/03/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |PHIL HARRELL R4 | |10 CFR SECTION: |ELINOR ADENSAM NRR | |AESF 50.72(b)(2)(ii) ESF ACTUATION |JOSEPH GIITTER IRO | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUXILIARY OFFSITE POWER TRIPPED DURING MAINTENANCE WORK DUE TO A PROCEDURAL | | DISCREPANCY. | | | | THE AUXILIARY OFFSITE POWER TRIP RESULTED IN THE AUTO START AND LOADING OF | | THE 1-2 DIESEL GENERATOR ON A BUS UNDERVOLTAGE SIGNAL. THE OPERATING RHR | | PUMP TRIPPED, BUT WAS MANUALLY RESTARTED WITHIN 39 SEC, WITHOUT ANY | | NOTICEABLE TEMPERATURE INCREASE OCCURRING IN THE PRIMARY SYSTEM. THE TRIP | | OF THE OFFSITE POWER OCCURRED DURING MAIN TURBINE WORK WHICH CAUSED A THRUST | | BEARING TRIP SIGNAL. THE THRUST BEARING TRIP WAS NOT CUT OUT AT THE TIME, | | THUS THE INITIATION OF A UNIT TRIP SIGNAL OCCURRED, TRIPPING OFFSITE | | AUXILIARY POWER. | | | | ONE OF THE THREE VITAL BUSES WAS ALIGNED WITH ITS STARTUP FEEDER BREAKER IN | | THE TEST POSITION FOR PLANNED TESTING. WHEN AUXILIARY POWER TRIPPED, THE | | BUS COULD THEREFORE NOT TRANSFER TO OFFSITE STARTUP POWER AND THE DIESEL | | GENERATOR STARTED ON BUS UNDERVOLTAGE. THE RUNNING RHR PUMP WAS SHED FROM | | THE BUS DURING THE TRANSFER. THE OTHER TWO BUSES SUCCESSFULLY TRANSFERRED | | TO THE STARTUP POWER SOURCE. | | | | THE VITAL BUS ON THE DIESEL WAS TRANSFERRED AT 1549 PST TO THE STARTUP POWER | | SOURCE AND THE DIESEL WAS SECURED AT 1551 PST. ALL OFFSITE POWER SOURCES | | WERE RESTORED AT 1800 PST. | | | | THE PROCEDURE DISCREPANCY WILL BE CORRECTED. | | | | THE RESIDENT INSPECTOR WAS INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35438 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 03/04/1999| | UNIT: [] [2] [] STATE: SC |NOTIFICATION TIME: 01:15[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/04/1999| +------------------------------------------------+EVENT TIME: 00:28[EST]| | NRC NOTIFIED BY: BILL RUDD |LAST UPDATE DATE: 03/04/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |CAUDLE JULIAN R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | IMPROVED TECHNICAL SPECIFICATION REVIEW FOUND SUSPECT SURVEILLANCE | | | | The licensee identified a suspect surveillance during a programatic review | | of Improved Technical Specifications Surveillances. The surveillance | | involved the timers for the hydrogen skimmer suction isolation valves. The | | acceptance criteria in the surveillance procedure was higher than allowed by | | the acceptance criteria of the Updated Final Safety Analysis Report Table | | 7-15. The licensee entered LCO 3.0.3 due to both trains being out of | | tolerance. The licensee exited LCO 3.0.3 at 0059 EST after one of the | | timers was recalibrated and that train was declared operable. | | | | The licensee also verified unit 1 hydrogen skimmer suction valve timers were | | in specification. One of unit 1's valves was out of specification and will | | be reported as a 30 day written report. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021