Event Notification Report for February 22, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/19/1999 - 02/22/1999 ** EVENT NUMBERS ** 35359 35378 35384 35385 35386 35387 35388 35389 35390 35391 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35359 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 02/09/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 18:37[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 02/09/1999| +------------------------------------------------+EVENT TIME: 18:20[EST]| | NRC NOTIFIED BY: JEFF SHIPE |LAST UPDATE DATE: 02/19/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAURIE PELUSO R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 98 Power Operation |98 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - Non-conservative dose calculation methodology is a condition outside the | | design basis of Unit 1 - | | | | As a result of LER 2-97-008 corrective actions, non-conservative inputs have | | been identified that is associated with the Beaver Valley Power Station | | (BVPS) methodology in calculating radiation doses for accidents which must | | analyze for a concurrent iodine spike as part of their radiological | | analyses. The identified non-conservative factors during past operation, | | could have resulted in the calculated control room personnel dose values | | exceeding 10CFR50 Appendix A, Criterion 19 thyroid limits. Since BVPS no | | longer has reasonable assurance that acceptance criteria for control room | | personnel dose limits per Criterion 19 would have been met during past | | operation, the identified non-conservative dose calculation methodology was | | a condition which was outside the design basis of the plant per | | 10CFR50.72(b)(1)(ii). This condition is also being evaluated for the | | criteria in 10CFR Part 21. | | | | For BVPS, the only Design Basis Accidents (DBAs) which involve a concurrent | | iodine spike analysis are Main Steam Line Break, Small Line Breaks (e.g., | | letdown line break outside containment), and Steam Generator Tube Rupture. | | The most significant of the non-conservative issues is purification (i.e., | | letdown) flow, which was given as 60 gpm. This is the lower limit of the | | plant design flow rate range of 60-120 gpm. Analysis using 60 gpm results | | in a significant underestimation of the concurrent iodine spike source term | | as compared to operation at the upper design limit of 120 gpm. Of lesser | | importance were underestimated demineralizer decontamination factor, | | overestimated reactor coolant system (RCS) mass and inadequate use of RCS | | leakage as an iodine removal mechanism. It has been determined that | | correcting the above identified non-conservative factor would raise | | calculated control room personnel dose values of those events analyzed for | | concurrent iodine spikes by at least 40% and potentially as high as 140%. | | | | Until the BVPS dose calculations can be formally revised to address the | | identified non-conservative factors, the station has placed administrative | | controls on the extent of steady state letdown flow to ensure that plant | | operation remains within past analyzed limits. The influence of the other | | identified non-conservative factors have also been reviewed and determined | | not to be an operability concern at this time. | | | | The licensee plans to notify the NRC Resident Inspector. | | | | * * * UPDATE AT 1110 ON 02/19/99 FROM JIM DAUGHERTY TO JOLLIFFE * * * | | | | The licensee is evaluating the above described issue and at 1600 on | | 02/18/99, they determined that it also meets the reportability criteria | | pursuant to l0CFR Part 21 specifically for Beaver Valley Unit 1. The generic | | issue (Westinghouse issue) is applicable to both Beaver Valley Units I and | | 2. A written report will be supplied pursuant to 10CFR Part 21 and | | I0CFR50.73 in a supplement to LER 2-97-008. | | | | Until the Beaver Valley dose calculations can be formally revised to address | | the identified non-conservative factors, BVPS has implemented administrative | | controls to ensure that plant operation remains within past analyzed | | limits. | | | | The licensee is continuing to evaluate this issue. | | | | The licensee plans to notify the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R1DO Jim Trapp and NRR Vern Hodge. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35378 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 02/17/1999| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 13:05[EST]| | RXTYPE: [1] W-3-LP |EVENT DATE: 02/17/1999| +------------------------------------------------+EVENT TIME: 12:19[EST]| | NRC NOTIFIED BY: MARK PALMER |LAST UPDATE DATE: 02/19/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |7 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECHNICAL SPECIFICATION REQUIRED PLANT SHUTDOWN DUE TO FAILURE OF THE 'A' | | REACTOR TRIP BREAKER TO CLOSE RELIABLY DURING TESTING | | | | The following text is a portion of a facsimile received from the licensee: | | | | "During [technical specification] surveillance testing [with the unit] at | | 100% power, a testing failure occurred on the train 'A' reactor trip | | breaker. The test in progress was MST-I001, Train 'A' Solid State | | Protection System Actuation Logic and Master Relay Test. During this test, | | the 'A' reactor trip breaker failed to close with the test pushbutton. The | | following timeline occurred:" | | | | "0821- [The] train 'A' reactor trip bypass breaker [was racked in and | | closed]. This began a 2-hour time | | limit allowed for surveillance testing. | | 0916 - Reactor trip breaker 'A' failed to close with the test pushbutton. | | At this point, the 2-hour limit for | | surveillance testing ended, and [Technical Specification] 3.3.1, action 8, | | was entered. This action | | required the plant to be in Mode 3 within 6 hours. The time to enter Mode 3 | | is 1516. | | 1026 - NRC Region II representative, George MacDonald, [was] notified of | | [limiting condition for operation] | | and necessity to be in Mode 3 by 1516. Mr. MacDonald was notified because | | [the] Harris resident | | inspectors are out of town. | | 1219 - [A generator] load reduction for plant shutdown [was commenced]. | | Maintenance and engineering | | personnel are investigating the problem." | | | | The licensee emphasized that the train 'A' reactor trip breaker did not fail | | to open, which is its safety function. The breaker only failed to re-close. | | It has since been opened and re-closed several times during ongoing | | troubleshooting activities. The licensee currently believes that the | | failure of the breaker to re-close reliably may be the result of a possible | | problem with the test circuitry allowing the test signal to stay in. | | | | Although all of the emergency diesel generators and emergency core cooling | | systems are operable and available if needed, the licensee stated that the | | emergency response data system is not available due to a Y2K problem. (The | | Y2K problem is not related to the breaker problem.) | | | | | | *** UPDATE ON 2/19/99 @ 1356 BY FLEMING TO GOULD *** | | | | THE PLANT EXITED TS 3.3.1 ACTION 8 AT 1452 ON 2/17/99 WHILE AT 7% POWER. | | THE UNIT DID NOT DROP FROM THE GRID OR ENTER MODE 3 PRIOR TO DECLARING THE | | "A" REACTOR TRIP BREAKER OPERABLE AND IN-SERVICE WITH ITS BYPASS BREAKER | | OPEN. AFTER EXITING THE LCO, POWER LEVEL WAS INCREASED AND THE REACTOR IS | | CURRENTLY AT 100% POWER. | | | | THE ORIGINAL REPORT STATED THAT "ERDS NOT AVAILABLE DUE TO Y2K PROBLEM." A | | SUBSEQUENT INVESTIGATION HAS REVEALED THAT ERDS REMAINED AVAILABLE | | IMMEDIATELY PRIOR TO AND DURING THE REPORTED EVENT. CONTROL ROOM STAFF WAS | | UNDER A MISTAKEN IMPRESSION THAT THE ERDS LINK WAS UNAVAILABLE DUE TO Y2K | | TESTING BY THE NRC. A SERIES OF INCOMPLETE COMMUNICATIONS LED THEM TO THAT | | CONCLUSION. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | REG2 RDO(BOLAND) WAS INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35384 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 02/19/1999| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 13:33[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 02/19/1999| +------------------------------------------------+EVENT TIME: 09:51[EST]| | NRC NOTIFIED BY: BREADY |LAST UPDATE DATE: 02/19/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JIM TRAPP R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SEVERAL ESF ACTUATIONS OCCURRED DUE TO THE UNEXPECTED DE-ENERGIZATION OF THE | | "D" 4.16KV VITAL BUS. | | | | DURING THE CONDUCT OF AN 18 MONTH DEGRADED VOLTAGE TEST OF THE "D" 4.16KV | | VITAL BUS INFEED BREAKER, THE BUS WAS INADVERTENTLY DE-ENERGIZED RESULTING | | IN A BUS UNDERVOLTAGE CONDITION. THE RELAY TECHNICIAN CONDUCTING THE TEST | | STATED THAT THE NORMAL INFEED BREAKER TRIPPED OPEN AS HE WITHDREW HIS | | VOLTMETER LEADS UPON COMPLETING THE DEGRADED VOLTAGE RELAY STATUS CHECK. | | THE CAUSE OF THIS BREAKER TRIP IS UNKNOWN AND BEING INVESTIGATED. THE | | ALTERNATE FEED BREAKER DID NOT CLOSE WHEN THE NORMAL INFEED TRIPPED, AND THE | | "D" VITAL BUS WAS DE-ENERGIZED AS A RESULT. AT THE TIME OF THE EVENT, THE | | PLANT WAS IN OPERATIONAL CONDITION 5 WITH CORE OFF LOAD IN PROGRESS. "A" | | AND "C" CHANNELS OF ELECTRICAL POWER AND SAFETY RELATED EQUIPMENT WERE | | PROTECTED AND AVAILABLE. THE "D" EMERGENCY DIESEL GENERATOR HAD BEEN | | CLEARED AND TAGGED FOR SCHEDULED MAINTENANCE, AND THE "DD447" 125 VDC | | BATTERY WAS ALSO CLEARED AND TAGGED FOR SCHEDULED MAINTENANCE. THE LOSS OF | | THE 4.16 KV BUS DE-ENERGIZED THE ASSOCIATED "D" CHANNEL 480 VAC UNIT | | SUBSTATION, MOTOR CONTROL CENTERS, AND UNINTERRUPTIBLE POWER SUPPLIES. THE | | LOSS OF THIS ASSOCIATED EQUIPMENT CAUSED A LOSS OF THE CONTROL ROD POSITION | | INDICATION, REACTOR BUILDING VENTILATION, AND REACTOR WATER CLEANUP PUMPS. | | THE "A" RHR PUMP REMAINED IN SHUTDOWN COOLING AND WAS NOT AFFECTED BY THE | | LOSS OF THE "D" BUS. THE FRVS SYSTEM WAS PLACED IN SERVICE TO RESTORE THE | | REACTOR BUILDING TO A NEGATIVE PRESSURE. ONE OF TWO COMMON SHUTDOWN COOLING | | SUCTION ISOLATION VALVES WAS DE-ENERGIZED IN THE OPEN POSITION, AS WELL AS | | THE "A" SHUTDOWN COOLING RETURN TO THE REACTOR VESSEL. CORE ALTERATIONS | | WERE TERMINATED AT THE TIME OF THE EVENT, AND THERE WAS NO IMPACT TO PLANT | | SAFETY. BUS RESTORATION AND ROOT CAUSE INVESTIGATION IS IN PROGRESS. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35385 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: COGEMA MINING INC. |NOTIFICATION DATE: 02/19/1999| |LICENSEE: COGEMA MINING INC. |NOTIFICATION TIME: 17:07[EST]| | CITY: LINCH REGION: 4 |EVENT DATE: 02/17/1999| | COUNTY: CAMPBELL STATE: WY |EVENT TIME: 12:00[MST]| |LICENSE#: SUA-1341 AGREEMENT: N |LAST UPDATE DATE: 02/19/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LAWRENCE YANDELL R4 | | |CHARLEY HAUGHNEY NMSS | +------------------------------------------------+JOE HOLONICH NMSS | | NRC NOTIFIED BY: VASELIN (RSO) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MONITOR WELL PLACED ON EXCURSION STATUS | | | | A ROUTINE BI-WEEKLY WATER SAMPLE COLLECTED ON 02/17/99 FROM MONITOR WELL | | "6MW40", EXCEEDED ALL 3 OF ITS UPPER CONTROL LIMITS UCLs. A CONFIRMATION | | SAMPLE WAS COLLECTED 2/19/99, WHICH ALSO EXCEEDED ALL 3 UCLs. MONITOR WELL | | "6MW40" WAS THEN PLACED ON EXCURSION STATUS AS PER LICENSE SECTION 11.2 AND | | ITS SAMPLING FREQUENCY INCREASED TO WEEKLY. "6MW40" IS A PERIMETER ORE ZONE | | MONITOR WELL LOCATED APPROXIMATELY 180 FEET (MAX. CAN BE 300 FT) EAST OF THE | | MINE UNIT 6 BOUNDARY AT THE CHRISTENSEN MINE, CAMPBELL COUNTY, WYOMING. THE | | NEAREST COMMUNITY IS LINCH, WYOMING, APPROXIMATELY 15 MILES TO THE | | SOUTHEAST. | | | | | | ANALYSIS DATA: | | | | DATE CHLORIDE mg/l CONDUCTIVITY �mhos/cm� ALKALINITY | | mg/l URANIUM mg/l U3O8 | | SAMPLED UCL 20.0 UCL 1576 | | UCL 95.2 NO UCL | | ---------------------------------------------------------------------------- | | ------------------------------------------------------------------------ | | 2/17/99 39.2 1861 | | 386.2 <0.4 | | | | 2/19/99 25.9 1660 | | 260.8 <0.4 | | | | THERE ARE NO HEALTH OR ENVIRONMENTAL HAZARDS FROM THE RESULTS OF THIS | | EXCURSION. | | | | CORRECTIVE ACTION: OVER-RECOVERY PUMPING OF 50 GPM HAS BEGUN IN THE | | WELLFIELD AREA NEAREST MONITOR WELL "6MW40". | | | | A WRITTEN NOTIFICATION WILL BE SUBMITTED TO NRC URANIUM RECOVERY BRANCH | | WITHIN 7 DAYS. | | | | HOO NOTE: SEE EVENT #35190 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35386 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 02/20/1999| | UNIT: [] [] [3] STATE: IL |NOTIFICATION TIME: 06:02[EST]| | RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 02/20/1999| +------------------------------------------------+EVENT TIME: 04:14[CST]| | NRC NOTIFIED BY: SALGADO |LAST UPDATE DATE: 02/20/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE JORDAN R3 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | |3 A N 0 Cold Shutdown |0 Cold Shutdown | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A FULL REACTOR SCRAM OCCURRED DURING RESTORATION LINEUP AFTER A HYDROSTATIC | | TEST | | | | Unit 3 experienced a full reactor scram (no rod motion), group 2 (Reactor | | Water Cleanup, drywell atmosphere) isolation and group 3 (shutdown cooling) | | isolation while in mode 4 (cold shutdown). Actual reactor vessel water | | level was plus 32 inches (scram/isolation setpoint is approximately plus 15 | | inches). This event occurred during the restoration from the hydrostatic | | test lineup (probably a pressure spike on a instrument line during the | | restoration lineup caused this event). Shutdown cooling was lost for | | approximately 10 minutes. There was no discernable rise in reactor vessel | | water temperature during the time period shutdown cooling was inoperable. | | The licensee is investigating the cause of the reactor scram and the group | | isolations. | | | | The NRC resident inspector will be informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35387 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/20/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 08:44[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/19/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 10:05[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 02/20/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |MIKE JORDAN R3 | | DOCKET: 0707001 |CHARLEY HAUGHNEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: K. A. BEASLEY | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | WATER INVENTORY CONTROL SYSTEM ACTIVATION | | | | A water inventory control system (WICS) activation occurred on C-360 | | position 4 autoclave on February 19, 1999 at 1005 CST. A high level drain | | primary alarm was received during a cylinder sampling heat cycle. The | | safety system did operate as required (shuts off steam to the autoclave | | which reduces the amount of condensation in the autoclave). The purpose of | | the WICS is to limit the amount of condensate in the autoclave. The cause of | | this actuation is being investigated. The certificate holder thinks that | | this event might have been caused by an invalid signal and if it is | | determined that this event was caused by an invalid signal this event | | notification will be retracted at a later time. | | | | The safety system actuation is reportable per Safety Analysis Report, | | section 6.9 Table 1, criteria J.2, Safety System actuation due to a valid | | signal as a 24-hour event notification. | | | | | | The NRC resident inspector was notified of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35388 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 02/20/1999| | UNIT: [1] [2] [3] STATE: AZ |NOTIFICATION TIME: 10:30[EST]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 02/20/1999| +------------------------------------------------+EVENT TIME: 06:48[MST]| | NRC NOTIFIED BY: DANN R. DAILEY |LAST UPDATE DATE: 02/22/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAWRENCE YANDELL R4 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | |3 N Y 100 Power Operation |100 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE OFFSITE EMERGENCY SIREN SYSTEM SILENT AND BACKUP TEST FAILED. | | | | On 02/20/99 at approximately 0648 MST, Palo Verde was notified by the | | Maricopa County Sheriff's Office (MCSO) of a failure of the Offsite Siren | | System in the Emergency Planning Zone. The discovery was during a scheduled | | silent test of the sirens by MCSO personnel. At approximately 0720 MST, the | | Department of Public Safety performed a back-up test of the Offsite Siren | | System that also failed. Emergency Planning personnel have been notified | | and are responding to correct the problem. Investigation of the above | | problem is in progress. | | | | The NRC resident inspector was notified of this event by the licensee. | | | | | | ***Update by Dann R. Dailey on 02/20/99 at 1034 EST taken by MacKinnon*** | | | | The Offsite Siren System was successfully tested and returned to service at | | 0820 MST. R4DO (Larry Yandell) notified. | | | | The NRC resident inspector will be notified of this update by the licensee. | | | | | | **** UPDATE ON 2/20/99 @ 1428 BY MARKS TO GOULD *** | | | | ALL 39 SIRENS WERE RETURNED TO SERVICE AT 0820 MST. CAUSE OF FAILURE WAS | | DUE TO PERSONNEL ERROR. A TEST TONE WAS INADVERTENTLY LEFT ON THE PHONE | | LINE AND IT INTERFERED WITH THE ABILITY TO ACTIVATE THE OFF-SITE SIRENS. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. THE REG 4 RDO(YANDELL) WAS INFORMED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35389 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/20/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 21:38[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/19/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 23:00[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 02/20/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |MIKE JORDAN R3 | | DOCKET: 0707002 |CHARLEY HAUGHNEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SPAETH | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NCFR NON CFR REPORT REQMNT | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CRITICALITY ACCIDENT ALARM SYSTEM (CAAS) "SLAVE" SYSTEM DECLARED | | INOPERABLE. | | | | AT 2300 ON 2/19/99, AN INSTRUMENT MAINTENANCE WORK CREW DISCOVERED THE | | NITROGEN BOTTLE VALVED OFF WHILE RESPONDING TO A TROUBLESHOOT AND REPAIR | | WORK PACKAGE FOR THE X-700 CAAS "SLAVE" SYSTEM. THE REQUIRED ACTIONS FOR | | THIS LCO WERE NOT IMPLEMENTED UNTIL THE CAAS "SLAVE" SYSTEM WAS DECLARED | | INOPERABLE AT 2234 | | | | THIS DISCOVERY RESULTED IN A NONCOMPLIANCE WITH TECHNICAL SAFETY REQUIREMENT | | (TSR) 2.8.3.1b LIMITING CONDITION OF OPERATION (LCO), WHICH STATES THE | | CRITICALITY ACCIDENT ALARM SHALL BE OPERABLE (AUDIBLE). | | | | THE X-700 BUILDING IS PROVIDED WITH BOTH A CAAS CLUSTER WITH ITS ASSOCIATED | | NITROGEN BOTTLE AND A "SLAVE" NITROGEN-DRIVEN HORN SYSTEM (INCLUDES 3 HORNS) | | TO PROVIDE ADEQUATE AUDIBILITY WITHIN THE BUILDING IN THE UNLIKELY EVENT OF | | A NUCLEAR CRITICALITY. | | | | THE CAAS CLUSTER AND ITS ASSOCIATED NITROGEN HORN REMAINED OPERABLE | | THROUGHOUT THIS EVENT, THEREFORE, TSR COMPLIANCE WITH THE LCO. CRITICALITY | | ACCIDENT DETECTION WAS MAINTAINED. | | | | THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. | | | | THE NRC RESIDENT INSPECTOR WAS INFORMED AND THE DOE REPRESENTATIVE WILL BE | | NOTIFIED | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35390 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 02/21/1999| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 11:28[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 02/20/1999| +------------------------------------------------+EVENT TIME: 21:00[EST]| | NRC NOTIFIED BY: STEVE MORRISSEY |LAST UPDATE DATE: 02/21/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JIM TRAPP R1 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ELEVEN DEAD SEA DUCKS FOUND IN CIRCULATING WATER SCREEN WASH DEBRIS | | | | Eleven dead sea ducks were observed in Seabrook station's circulating water | | screen wash debris on February 20, 1999 at approximately 2100 hours. It is | | not known at this time whether the ducks were alive or dead upon entering | | the offshore intake structure. Sea ducks are diving birds which feed | | underwater. This is a 24 hour notification in accordance with section 4.1 | | of the environmental protection plan, appendix B of the operating license. | | | | The NRC resident inspector was notified of this event report by the | | licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35391 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 02/21/1999| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 22:25[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 02/21/1999| +------------------------------------------------+EVENT TIME: 20:50[CST]| | NRC NOTIFIED BY: HANKS |LAST UPDATE DATE: 02/21/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAWRENCE YANDELL R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR WAS MANUALLY SCRAMMED FROM 100% POWER DUE TO LOSS OF CONDENSER | | VACUUM. | | | | THE "A" MAIN CONDENSER HAD A SEAL FAILURE ON THE EXPANSION JOINT WHICH | | RESULTED IN A DECREASE AND LOSS OF CONDENSER VACUUM. DUE TO THIS | | CONDITION, A MANUAL SCRAM WAS INITIATED FOLLOWED BY A MAIN TURBINE TRIP. | | THE CONTROLLED SHUTDOWN HAD NO IMMEDIATE PROBLEMS. ALL RODS FULLY INSERTED. | | NO ECCS ACTUATIONS OCCURRED. THE LICENSEE ANTICIPATES THAT REACTOR VESSEL | | PRESSURE MAY BE LATER CONTROLLED VIA THE RELIEF VALVES DEPENDING ON THE | | COOLDOWN RATE (REACTOR VESSEL PRESSURE IS CURRENTLY 550 LBS). THE CURRENT | | HEAT SINK IS THE MAIN CONDENSER, BUT THE LICENSEE IS PREPARING TO SHUT THE | | MSIVs AND SHIFT THE HEAT SINK TO THE SUPPRESSION POOL. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+
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