Event Notification Report for February 3, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/02/1999 - 02/03/1999 ** EVENT NUMBERS ** 35295 35339 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35295 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 01/21/1999| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 16:59[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 01/21/1999| +------------------------------------------------+EVENT TIME: 15:00[CST]| | NRC NOTIFIED BY: RICK ROBBINS |LAST UPDATE DATE: 02/02/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | Material for deionized water supply valve changed | | | | During storeroom valve stock review, the licensee discovered that valve | | materials for a deionized water supply line containment isolation valve had | | changed. Specifically, the diaphragm material had changed. The design | | value for the original material was 200� F at 200 psi. The new valve was | | rated at 150� F at 300 psi. This valve inside containment and another | | valve outside containment are normally closed during operation. Further | | evaluations are underway. | | | | Containment integrity has been verified by ensuring the valve outside | | containment is locked shut. | | | | The NRC resident inspector will be notified of this event by the licensee. | | | | * * * RETRACTED ON 2/2/99 AT 1122 EST BY MIKE MEYER TO FANGIE JONES * * * | | | | After further investigation, the licensee determined that valve 1DI-11 and | | the outside containment isolation valve (1DI-19) are locked closed during | | times that containment integrity is required. Therefore, even if the | | improper ratings of the valve would have resulted in the valve failing | | during a design bases accident, containment integrity would have been | | maintained by the normally locked closed valve outside containment. | | | | Therefore, this condition does not result in a condition of the plant being | | outside its design basis and this event notification is retracted. | | | | The licensee intends to notify the NRC Resident Inspector. The NRC | | Operations Officer notified the R3DO (Thomas Kozak). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 35339 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNION CAMP CORP |NOTIFICATION DATE: 02/02/1999| |LICENSEE: UNION CAMP CORP |NOTIFICATION TIME: 15:34[EST]| | CITY: FRANKLIN REGION: 2 |EVENT DATE: 02/01/1999| | COUNTY: STATE: VA |EVENT TIME: [EST]| |LICENSE#: 45-11414-01 AGREEMENT: N |LAST UPDATE DATE: 02/02/1999| | DOCKET: 030-0659 |+----------------------------+ | |PERSON ORGANIZATION | | |PAUL FREDRICKSON R2 | | |FRED COMBS EO | +------------------------------------------------+STUART RUBIN IRO | | NRC NOTIFIED BY: HUGH RALSTON | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE REPORTED A LOST AMERICIUM-241 SOURCE DURING SHIPMENT. | | | | "THE SOURCE MATERIAL LOST IN SHIPMENT IS AN AMERICIUM-241 80mCi SEALED | | SOURCE CERAMIC ENCAPSULATED BY WELDED STAINLESS STEEL. THE SOURCE SERIAL | | NUMBER IS 8462LX MOUNTED IN DEVICE NUMBER 2992 MANUFACTURED BY NDC SYSTEMS, | | 5314 NORTH IRWINDALE AVE., IRWINDALE, CALIFORNIA 91706. THE SOURCE IS AN | | INTEGRAL COMPONENT OF AN NDC MODEL 104F PAPER MACHINE FOURDRINIER MASS | | MEASUREMENT GAUGE. | | | | "THE MATERIAL WAS PICKED UP AT OUR FRANKLIN, VIRGINIA, TRANSPORTATION | | DEPARTMENT LOCATION BY UPS COURIER MONDAY, JANUARY 18, 1999 FOR OVERNIGHT | | SHIPMENT TO NDC IN IRWINDALE. THE UPS TRACKING NUMBER ASSIGNED WAS | | 1Z2923930143701285. NDC SYSTEMS WAS CONTACTED ON 1/18/99 AND ADVISED TO | | EXPECT THE PACKAGE ON 1/19/99. NDC PERSONNEL WERE REQUESTED TO ADVISE US | | UPON RECEIPT. NDC PERSONNEL WERE CONTACTED 1/19/99 TO DETERMINE WHETHER THE | | PACKAGE WAS, IN FACT, RECEIVED. IT WAS NOT. NDC WAS CONTACTED ON 1/20/99 | | TO DETERMINE WHETHER THE PACKAGE WAS RECEIVED. IT WAS NOT. SUBSEQUENTLY, | | ON 1/20/99, UPS WAS CONTACTED TO REQUEST THAT THE PACKAGE BE TRACED. UPS | | ASSIGNED TRACING NUMBER 020A0110 TO THE SHIPMENT. THE PACKAGE WAS SCANNED | | UPON ARRIVAL IN THE UPS SYSTEM IN LOUISVILLE INTERNATIONAL IN LOUISVILLE, | | KY. AT 1152 P.M. ON 1/18/99. THE MATERIAL SUBSEQUENTLY BECAME MISSING IN | | THE UPS SHIPPING SYSTEM. | | | | "ANY EXPOSURE TO INDIVIDUALS IS EXTREMELY UNLIKELY. THE MATERIAL WAS | | PACKAGED IN COMPLETE COMPLIANCE WITH DOT REGULATIONS FOR AN EXCEPTED PACKAGE | | LIMITED QUANTITY MATERIAL AND NDC RECOMMENDED PACKAGING GUIDELINES WITH THE | | SOURCE SHUTTER SECURELY CLOSED. THERE IS LESS THAN 0.1mR/HR EXPOSURE RATE | | 50 MILLIMETERS FROM THE FACE OF THE SHUTTERED SENSOR. A SURVEY WAS | | PERFORMED USING A TN TECHNOLOGIES MODEL 200X RADIATION SURVEY METER SERIAL | | NUMBER B587W LAST CALIBRATED 10/19/98 TO CONFIRM EXPOSURE RATE. | | | | "REPRESENTATIVES OF UNION CAMP HAVE BEEN IN DAILY CONTACT WITH | | REPRESENTATIVES OF NDC AND UPS IN ATTEMPTS TO LOCATE THE UNIT. INGLEHART & | | ASSOCIATES WAS CONSULTED FOR ADDITIONAL IDEAS IN LOCATING THE DEVICE. TO | | DATE, THE DEVICE HAS NOT BEEN LOCATED. | | | | "FROM A UNION CAMP PROCEDURES STANDPOINT, THERE IS NO KNOWN METHOD OR | | MEASURE THAT CAN BE ADOPTED TO ENSURE AGAINST A RECURRENCE OF A LOSS SUCH AS | | THIS. " | +------------------------------------------------------------------------------+
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